ML120810365: Difference between revisions
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| number = ML120810365 | | number = ML120810365 | ||
| issue date = 03/22/2012 | | issue date = 03/22/2012 | ||
| title = | | title = Single Phase Failure | ||
| author name = | | author name = | ||
| author affiliation = Exelon Nuclear | | author affiliation = Exelon Nuclear |
Revision as of 11:29, 12 April 2019
ML120810365 | |
Person / Time | |
---|---|
Site: | Byron |
Issue date: | 03/22/2012 |
From: | Exelon Nuclear |
To: | Office of Nuclear Reactor Regulation |
Mozafari B L | |
References | |
Download: ML120810365 (25) | |
Text
1 Byron Station Single Phase Failure NRC Meeting March 22, 2012 2 Opening Remarks Tim Tulon Byron Site Vice President 3 Purpose Provide overview of loss of offsite power (LOOP) events Summarize failure analysis Discuss identified design vulnerability and extent of condition Describe design and licensing basis Highlight Exelon fleet planned actions and industry activities 4 Overview of Events and Failure Analysis Elmer Hernandez Byron Site Engineering Director 5 Byron Unit 2 Single Line Diagram 6 Recent Events January 30, 2012 Mechanical failure of 345 kV under-hung porcelain insulator on
SAT A-frame structure Open phase condition (primary grounded) LOOP Unusual Event Reactor trip Manual separation of ESF buses February 28, 2012 Mechanical failure of 345 kV under-hung porcelain insulator on
SAT A-frame structure Open phase condition (345 kV faulted) LOOP Switchyard ground fault protective relaying isolated the fault and
transferred BOP power to the UAT Unusual Event No reactor trip Automatic separation of ESF buses Unit 2 Unit 1Key Difference -No Fault versus FaultKey Difference -No Fault versus Fault 7 Byron Unit 2 Insulator FailureBlue BusRed Bus345 kV Lines to Other ComEd Substations SAT 142A-Frame MPT 2A-FrameSAT 242A-Frame MPT 1A-FrameComEd Switchyard at Byron StationTo Byron Station SATs and MPTsBus 6Bus 4Bus 13Bus 11 Resulting Break LocationUnder-HungInsulator FailureS-BusDisconnectSwitchCT/PTRevenueMetering Unit A-Frame StructureTo Station Yard(SAT 242-1/2)
Existing A-Frame Structure Configuration Failed Insulator Stack CollapsedC-Phase Bus Fallen Insulators Unit 2 8 Failed Insulators Unit 2 Failed Insulator Unit 1 Failed Insulator 9 Design Vulnerability Scot Greenlee Corporate Vice President Engineering 10 Design Vulnerability Failure of Unit 2 'C' Phase insulator resulted in an open circuit and voltage imbalance (high impedance ground on
high side of SAT, open phase on the 345 kV side of
disconnect)*Did not result in a fault that ac tuated the existing protective relay scheme Voltage imbalance propagated through the SATs to the ESF buses*Under voltage or degraded voltage relays did not initiate an EDGstart signal because the relays sensed adequate voltage between
'A' and 'B' Phases 11 Impact of Open Phase Due to ground, significant voltage imbalance*4.16 kV safety bus per unit (pu) voltage Vab1.0142 pu (on a 4160 V base)
Vbc0.5912 pu (lasted 12 seconds, then cleared)
Vca0.5870 pu 345 kV Side SAT Feed 12Impact of Open Phase -Not Grounded (Beaver Valley Event Applied to Byron Station) Open phase 4.16 kV safety bus per unit voltage under light loading Vab1.0408 pu (on a 4160 V base)
Vbc1.0407 pu Vca1.0180 pu Cannot detect by voltage magnitude 13 Design Vulnerability Under voltage relay schemes are not always able to detect a single open phase Although the plant was determined to be designed consistent with applicable design and regulatory requirements, it is recognized that additional
actions should be taken to address this vulnerability 14 Exelon Fleet Actions Implemented compensatory measures to minimize operator recognition time for this event Communicated issue to Exelon fleet and industry Implemented changes, as necessary, for annunciation logic to detect and alarm the phase imbalance 15 Exelon Fleet Actions (cont.) Interactions with industry and A/Es identified no design currently exists to resolve this vulnerability Developing modification to detect the phase imbalance (open phase) condition and automatically separate the station busses from the offsite power source for this condition*Evaluated over 30 di fferent potential designs*Prevent unnecessary trip of ESF bus power sources
- Avoid impact on existing coordination scheme*Minimize unintended consequences 16 Industry Actions Industry briefed via INPO webcast to alert the industry to the vulnerability INPO issued Level 2 IER outlining industry actions (based on input from Exelon) NEI established a working group to evaluate vulnerability solutions -Ongoing weekly meetings NRC published Information Notice 2012-03, "Design Vulnerability in Electric Power System" (Byron Station
event included) Exelon meeting with NRC to discuss the design vulnerability and industry implications INPO hosting April 2012 industry workshop to evaluate vulnerability solutions 17 Design/Licensing Basis Scot Greenlee Corporate Vice President Engineering 18 GDC 17 Electric power from the transmissi on network to the onsite electric distribution system shall be supplied by:*Two physically independent circuits*Each circuit shall be designed to be available in sufficient time to assure that design conditions of the fuel an d reactor coolant pressure boundary are not exceeded*One of these circuits shall be designed to be available within afew seconds following a loss-of-coolant accident (LOCA)*Onsite electrical power systems were designed to perform their safety function assuming a single failureProvisions shall be included to minimize the probability of losing electric power from any of the rema ining supplies as a result of, or coincident with:*The loss of power generated by the nuclear power unit,*The loss of power from the transmission network, or*The loss of power from the onsite electric power supplies 19 GDC 17 Conformance Byron Station electric power syst ems were designed to meet GDC 17 Byron Station has two SATs per unit, sized to handle normal and accident loadsSecond GDC 17 offsite source is through the other unit's SATs Loss of feed to the unit SATs doe s not impact the other unit's SATsStudies performed address:*Both normal and accident conditions on loss of the unit*Loss of a transmission line feeding the switchyard Ring Bus*Voltage levels down to and including minimum grid voltages, coordinated through transmission system operator*Protection from short circuits 20 Degraded VoltageGrid events at Millstone in July 1976 demonstrated that sustained degraded voltage conditions on the grid can cause adverse effects*Further evaluation revealed that improper voltage protection logic can also cause adverse effects Degraded voltage event at ANO in September 1978 demonstrated that degraded voltage conditions could exis t on Class 1E buses, even with normal grid voltages*NRC issued Information Notice 79-04 to inform the industry*Generic Letter 79-36 issued to identify specific actions to be taken by licenseesRequires utilities to install second level of under voltage relay protection*Branch Technical Position (BTP) PSB-1 was issued in July 1981 Incorporated NRC positions to meet GDC 17 requirements Provides a design approach with respect to the selection of the time delay for the degraded voltage relay circuit Voltage sensors were designed to meet requirements derived from IEEE 279-1971 21 BTP PSB-1 During sustained degraded voltage condition, the degraded voltage relay design should:*Protect Class 1E buses and components*Separate Class 1E buses from the grid within a few seconds if an accident occurs*Automatically separate Class 1E buses from the power supply within a short interval, during normal plant operation*Minimize inadvertent separation from offsite power (e.g., coincident logic) Time delays should be optimized 22 BTP PSB-1 Conformance Byron Station has two distinct under voltage relay schemes*Loss of Power Two out of two, Class 1E, relay logic oDrop out set at 69% of rated voltage*Degraded Voltage Two out of two, Class 1E, relay logicoMinimum drop out se t at 92.5% (3847.5 V)oMaximum reset set at 93.8% (3902.3 V)
Time Delay Byron Station Safety Evaluation Report (NUREG-0876) was issued in February 1982*Chapter 8 of the Byron Station FSAR was reviewed in accordance with the July 1981 edition of the SRP*Subsection 8.2.4 documents the NRC conclusion that the Byron Station design conforms with BTP PSB-1 23 Degraded Voltage Licensing Basis Confirmed that the design of the auxiliary power system meets GDC 17 requirements Confirmed the degraded voltage relay scheme is in compliance with BTP PSB-1 and pertinent requirements of IEEE-279 Event revealed a design vulnerability that was not detected by the existing protective relay scheme*Existing SAT neutral overcurrent protection was not sensitive enough to detect the open phase condition*Detection down to the level of this type of failureis beyond therequirements of GDC 17 or BTP PSB-1 Overall conclusion is that the Byron Station power system and degraded voltage design is consistent with the
licensing basis 24 Summary Tim Tulon Byron Site Vice President 25 Summary Events at Byron Station Units 1 and 2 were caused by an insulator failure in a single phase of offsite power Detection and mitigation of a single phase failure in the offsite power supply to an ESF bus is a
design vulnerability outside scope of current design and licensing basis Exelon is taking aggressive fleet wide actions to address the design vulnerability, including working with the industry