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{{#Wiki_filter:Commonwec9 Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. # 333 April 20, Mr. James G. Keppler, Regional Directorate of Regulatory Operation | {{#Wiki_filter:Commonwec9 Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. # 333 April 20, Mr. James G. Keppler, Regional Directo~ | ||
-Region I I I U. s: "Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, 111 inois 60137 REGULATORY DDCKEI RLE COPY Enclosed please find Reportable Occurrence 50-249/1977-7. | Directorate of Regulatory Operation - Region I I I U. s: "Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, 111 inois 60137 REGULATORY DDCKEI RLE COPY Enclosed please find Reportable Occurrence rep~rt nu~ber 50-249/1977-7. | ||
This report is being submitted to your office in accordance with the bresden Nuc | This report is being submitted to your office in accordance with the bresden Nuc 1ec;ir Power Station Techn i ca,1 Specif i cat..i ons,. Section 6. 6. B.. | ||
& Enforcement Director of Management | BBS: skm | ||
& Program Control Fil e/NRC APR 2 5 1977 LICENSEE EVENT REPORT CONTROL BLOCK: Lj_** 1 L . , I . I c&sE PRINT ALL,REQUIRED INFORMATION) | *Enclosure cc: Director of Inspection & Enforcement Director of Management lnf~rmation & Program Control Fil e/NRC APR 2 5 1977 | ||
* COMPONENT CoMPONENT | LICENSEE EVENT REPORT CONTROL BLOCK: | ||
* l!U | LICENSEE Lj_** | ||
The defective capaci_tor' was replaced, and the Unit-3 diesel | 1 L ., I . I 6 | ||
c&sE PRINT ALL,REQUIRED INFORMATION) | |||
., | LICENSE EVENT NAME LICENSE NUMBER . TYPE TYPE | ||
* DESCRIPTION II§] J 0 I 0 I | *@El I I I LI DI RI sI 31 1°1°1~1°1°1°1°1°1-1°1°1 ~ 41 1 p 11 11 I I o I 31 1 0*s 14 15 25 26. . 3P 31 32 REPORT REPORT CATEGORY TYPE. SOURCE DOCKET NUMBER EVENT DATE REPORT DATE | ||
@E]coN'.T I I I LJ L':J I 01 51 01~10 12 14 19 I I o I 3 I 2 I .2 I 7 I 7 I 10141 2 1117171 7 .8 57. 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION ffilfil. I During testing of the Unit-3 d)esel generator following maintenance, the engine I lol 3 r I started,.but*the generator field failed to flash. The generator field flashed 7 8 9 80 7 . 8 9 I | |||
__ ""'=" 7 8 9* 11 12 80 * | 80 lol41'1 during a secon.d start-up of the diesel. The diesel was started a third time, I 7 . 8**9 80 IPl51 J . and again the field did not flash. The Unit-3 diesel generator was then shut I 7 0*s 80 lolsl I , down and dee 1a red i noperab 1e. A subsequent attempt to start the Unit-2/3 diesel I | ||
* OFFSITE .. CONSEQUENCES NA 7 8 9 LOSS OR DAMAGE . TO FACILITY TYPE [!El | 1 *0 s PRIME ~foont i nued) | ||
....... ----------------------- | * 80 | ||
PHONE:_.-... | .SYSTEM CAUSE COMPONENT CoMPONENT | ||
_ _.. | [§E] IE IE I* | ||
7 8 9 10 CODE w | |||
. CODE 11 I El COMPONENT CODE NI GI 12 . : .* .*. | |||
II NI El 17 SUPPUER | |||
~ | |||
43 I | |||
44 MANUFACTURER WI 019 17 I 47 VDLATION | |||
* l!U 48 CAUSE DESCRIPTION . < | |||
~ I The failure was 'caused by an intermittent capacitor short in the generator field k | |||
7 8 9 The defective capaci_tor' was replaced, and the Unit-3 diesel 80 | |||
~ll flashing circuitry. | |||
l IT1§J0* 9I 1* | |||
generator was satisfact_orily tested and returned to service. eo I | |||
7 8 9 80 FACIUTY {continued) | |||
STATUS 'll. POWER OTHER STATUS DISCOVERY DESCRIPTION Em8 7.; | |||
L:J I 01 913 I NA | |||
.9 10 12 13 80 FORM OF ACTIVITY CONTENT AMOUNT OF ACTIVITY LOCATION OF RELEASE rn w RELEASED OF RELEASE 7 8 9 LlJ 10 | |||
:11I . NA | |||
.__------'---------.....JI 80 | |||
., | |||
PERSONNEL EXPOSURES | |||
. NUMBER TYPE. | |||
* DESCRIPTION II§] J 0 I 0 I 0I .~ . .____NA_ _ _ _ _ _ _ _ _ __;.____;.__;._ _ _ _ _ ___, | |||
7 8 9 . 11* . 12 13 80 PERS'ONNEL INJURIES | |||
. NUMBER 'DESCRIPTION l1E1 I 0 I 0 I 0I ':--__N_A_ _ _ _ _ _ _ _ _ _ _.......:..---...~....-...__;..-__;..__;.._;._ _""'=" | |||
7 8 9* 11 12 80 | |||
** OFFSITE .. CONSEQUENCES | |||
~. NA 7 8 9 80 LOSS OR DAMAGE . TO FACILITY TYPE DESCRIPTION | |||
[!El ~J NA 80 7 8 9 10 PUBLICITY NA ADDITIONAL FACTORS | |||
. 7 | |||
*Elfil8 9I NA 80 | |||
~.L-~~--------------------~--'-~--------~~ | |||
7 B. 9 &O J. B. Martin Ext. 265 | |||
~E:= .......- - - - - - - - - - - - - - - - - - - - - - - PHONE:_.-..._ _..__ __...;_ | |||
GPO 881*087 | |||
* | |||
-. | -. | ||
EVENT DESCR1PTION (continued) | |||
This event was of little safety significance, since the redundant Unit-2/3 di ese 1 .generator was demonstrated to be operab | -generator was-;:::unsuccessful (R. 0. report no. 50~237/1977-11). | ||
This event was of little safety significance, since the redundant Unit-2/3 di ese 1 .generator was demonstrated to be operab 1e short 1y thereafter (within | |||
~5 minutes), and off-site power remained available durin~ this interval. ihe | |||
- Unit-2 diesel generator experienced a similar gen~rator field flashing failure in April, 1975. | |||
(50-249/1977-7) | |||
CAUSE DESCRIPTION (continued) | CAUSE DESCRIPTION (continued) | ||
As a long-term action, the diesel generator maintenance procedure will be revised to include a check of the generator field flashing capacitors. | As a long-term corr~ctive action, the annu~l diesel generator maintenance procedure will be revised to include a check of the generator field flashing circ~it capacitors. The failed capacitot is an 8-microfarad, 150-volt electrolytic unit manufactured by Aerovox: | ||
The failed capacitot is an 8-microfarad, 150-volt electrolytic unit manufactured by Aerovox: ; *-- | ; ~- | ||
l : | |||
*-- | |||
*4: | |||
-* ~'. ...... : | |||
., , ~ | |||
' ... . | |||
- | |||
- ... ,'J.,J | |||
::::1}} |
Revision as of 20:28, 29 October 2019
ML17252A272 | |
Person / Time | |
---|---|
Site: | Dresden ![]() |
Issue date: | 04/20/1977 |
From: | Stephenson B Commonwealth Edison Co |
To: | James Keppler NRC/RGN-III |
References | |
50-249/1977-7 | |
Download: ML17252A272 (3) | |
Text
Commonwec9 Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. # 333 April 20, Mr. James G. Keppler, Regional Directo~
Directorate of Regulatory Operation - Region I I I U. s: "Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, 111 inois 60137 REGULATORY DDCKEI RLE COPY Enclosed please find Reportable Occurrence rep~rt nu~ber 50-249/1977-7.
This report is being submitted to your office in accordance with the bresden Nuc 1ec;ir Power Station Techn i ca,1 Specif i cat..i ons,. Section 6. 6. B..
BBS: skm
- Enclosure cc: Director of Inspection & Enforcement Director of Management lnf~rmation & Program Control Fil e/NRC APR 2 5 1977
LICENSEE EVENT REPORT CONTROL BLOCK:
LICENSEE Lj_**
1 L ., I . I 6
c&sE PRINT ALL,REQUIRED INFORMATION)
LICENSE EVENT NAME LICENSE NUMBER . TYPE TYPE
- @El I I I LI DI RI sI 31 1°1°1~1°1°1°1°1°1-1°1°1 ~ 41 1 p 11 11 I I o I 31 1 0*s 14 15 25 26. . 3P 31 32 REPORT REPORT CATEGORY TYPE. SOURCE DOCKET NUMBER EVENT DATE REPORT DATE
@E]coN'.T I I I LJ L':J I 01 51 01~10 12 14 19 I I o I 3 I 2 I .2 I 7 I 7 I 10141 2 1117171 7 .8 57. 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION ffilfil. I During testing of the Unit-3 d)esel generator following maintenance, the engine I lol 3 r I started,.but*the generator field failed to flash. The generator field flashed 7 8 9 80 7 . 8 9 I
80 lol41'1 during a secon.d start-up of the diesel. The diesel was started a third time, I 7 . 8**9 80 IPl51 J . and again the field did not flash. The Unit-3 diesel generator was then shut I 7 0*s 80 lolsl I , down and dee 1a red i noperab 1e. A subsequent attempt to start the Unit-2/3 diesel I
1 *0 s PRIME ~foont i nued)
- 80
.SYSTEM CAUSE COMPONENT CoMPONENT
[§E] IE IE I*
7 8 9 10 CODE w
. CODE 11 I El COMPONENT CODE NI GI 12 . : .* .*.
II NI El 17 SUPPUER
~
43 I
44 MANUFACTURER WI 019 17 I 47 VDLATION
- l!U 48 CAUSE DESCRIPTION . <
~ I The failure was 'caused by an intermittent capacitor short in the generator field k
7 8 9 The defective capaci_tor' was replaced, and the Unit-3 diesel 80
~ll flashing circuitry.
l IT1§J0* 9I 1*
generator was satisfact_orily tested and returned to service. eo I
7 8 9 80 FACIUTY {continued)
STATUS 'll. POWER OTHER STATUS DISCOVERY DESCRIPTION Em8 7.;
L:J I 01 913 I NA
.9 10 12 13 80 FORM OF ACTIVITY CONTENT AMOUNT OF ACTIVITY LOCATION OF RELEASE rn w RELEASED OF RELEASE 7 8 9 LlJ 10
- 11I . NA
.__------'---------.....JI 80
.,
PERSONNEL EXPOSURES
. NUMBER TYPE.
- DESCRIPTION II§] J 0 I 0 I 0I .~ . .____NA_ _ _ _ _ _ _ _ _ __;.____;.__;._ _ _ _ _ ___,
7 8 9 . 11* . 12 13 80 PERS'ONNEL INJURIES
. NUMBER 'DESCRIPTION l1E1 I 0 I 0 I 0I ':--__N_A_ _ _ _ _ _ _ _ _ _ _.......:..---...~....-...__;..-__;..__;.._;._ _""'="
7 8 9* 11 12 80
- OFFSITE .. CONSEQUENCES
~. NA 7 8 9 80 LOSS OR DAMAGE . TO FACILITY TYPE DESCRIPTION
[!El ~J NA 80 7 8 9 10 PUBLICITY NA ADDITIONAL FACTORS
. 7
- Elfil8 9I NA 80
~.L-~~--------------------~--'-~--------~~
7 B. 9 &O J. B. Martin Ext. 265
~E:= .......- - - - - - - - - - - - - - - - - - - - - - - PHONE:_.-..._ _..__ __...;_
GPO 881*087
-.
EVENT DESCR1PTION (continued)
-generator was-;:::unsuccessful (R. 0. report no. 50~237/1977-11).
This event was of little safety significance, since the redundant Unit-2/3 di ese 1 .generator was demonstrated to be operab 1e short 1y thereafter (within
~5 minutes), and off-site power remained available durin~ this interval. ihe
- Unit-2 diesel generator experienced a similar gen~rator field flashing failure in April, 1975.
(50-249/1977-7)
CAUSE DESCRIPTION (continued)
As a long-term corr~ctive action, the annu~l diesel generator maintenance procedure will be revised to include a check of the generator field flashing circ~it capacitors. The failed capacitot is an 8-microfarad, 150-volt electrolytic unit manufactured by Aerovox:
- ~-
l :
- --
- 4:
-* ~'. ...... :
., , ~
' ... .
-
- ... ,'J.,J
- 1