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| {{#Wiki_filter:NllC For111 .. (9-831 U.1. NUCLEAll llEOULATOllY COWlllllON APPllOVEO OM9 NO. 31ll0-0104 LICENSEE EVENT REPORT (LER) . EXPIRES: 8/3119& l'ACILITY NAME (11 Salem Generatina Station -Unit 1 I DOCKIT NW9111 IZI I 1:111 o 15 Io Io Io 17 b 1 loF nl 4 TITLE l*J T. S. Surveillance 4.7.S.l.2 Performed Late Due To Inadequate Administrative Control l!VINT OATI! 1111 LEA N..-Ell Ill REl'OllT OATE (7J OTHEll FACILITIEI INVOLVED Ill MONTH QAY YEAR YEAR mt | | {{#Wiki_filter:NllC For111 . . U.1. NUCLEAll llEOULATOllY COWlllllON (9-831 APPllOVEO OM9 NO. 31ll0-0104 EXPIRES: 8/3119& |
| .. L tr :i: MONTH DAY YEAR FACILITY NAME!I DOCKET NUMIEAISI Salem -Unit 2 0 161OI0I013 I 111 ol3 ob s s s ls-olols -olo ol3 219 s ls Ol'lllA TINO MODI Ill THll llEl'OAT 11 IU*UTTED l'UlllUANT TO THE llEQUlllEMENTI OF 1.0 CFll §: (Ch<<k ono or man of lit* followln1J (111 ZO * .all(ol I0.7:1C.ICZIU*I 7U11ltl ---10.a(11111 I0.7Slal1Zllwl 71.71(11 ----llO.*lolCZI l!0.7SColCZllril OTHEll (Sp<<lfy In Abl09ct ---,__ ond In To*r, NRC Fonn Jl ;G.73181121111 i0.73Clllillw11111AI 366AJ -l!0.73CalCZllMi I0.71C.ICZllwlllllll | | LICENSEE EVENT REPORT (LER) . |
| --l!0.73C.llillHll I0.71C.llZll*I LICENIEE CONTACT FOii THll LEll (111 NAME TELEPHONE NUMllER AREA CODE M. J. Pollack -LER Coordinator 61 O 19 3 I 3 I 9 I-I 4 I O 12 I 2 COMPLETE ONE LINE FOR EACH COlll'ONENT FAILUllE DEICllllED IN THll lll!l'OllT 1131 CAUSE SYSTEM COMPONENT I I I I I I I I MANUFAC TUR ER I I I I I I IUWLEMl!NTAL AEl'OllT l!Xl'l!CTED 1141 MYES flf rm. comp-EXl'ECTED SUtlMISSIDN DATEJ A81TllACT (Umlr ID 1"'10 -* I.&, _,.,.1mor.1y 11,_, Ii,.._
| | l'ACILITY NAME (11 DOCKIT NW9111 IZI I r-~~ 1:111 Salem Generatina Station - Unit 1 TITLE l*J Io 15 Io Io Io I~ 17 b 1 loF nl 4 T. S. Surveillance 4.7.S.l.2 Performed Late Due To Inadequate Administrative Control l!VINT OATI! 1111 LEA N..-Ell Ill REl'OllT OATE (7J OTHEll FACILITIEI INVOLVED Ill MONTH QAY YEAR YEAR mt SE~~~:~~.. L tr :i: MONTH DAY YEAR FACILITY NAME!I DOCKET NUMIEAISI Salem - Unit 2 0 161OI0I013 I 111 ol3 ob s s s ls- olols - olo ol3 219 s ls Ol'lllATINO THll llEl'OAT 11 IU*UTTED l'UlllUANT TO THE llEQUlllEMENTI OF 1.0 CFll §: (Ch<<k ono or man of lit* followln1J (111 MODI Ill |
| l/flll} (111 I I I I I I I I MANUFAC TUA ER I I I I I I EXPECTED SUllM18810.N DATE (1111 MONTH DAY Y&:AR I I I On 03/07/88 at 1200 hours,.it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surve.illance. | | - |
| The surveillance was as of 03/01/88. | | -- |
| The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed surveillance concerns (e.g., LER 272/88-004-00). | | ZO*.all(ol 10.a(11111 --- I0.7:1C.ICZIU*I I0.7Slal1Zllwl -- 7U11ltl 71.71(11 Jl llO.*lolCZI |
| *The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work acti_vity system, Managed Maintenance Information System (MMIS). The sealed source leak check surveillance was completed 03/14/88. | | ;G.73181121111 - |
| No leaking sources were found. A manual system for tracking surveillances within the Radiation Protection Department has been implemented. | | -- |
| This will continue until the MMIS is updated to handle this surveillance. | | l!0.7SColCZllril i0.73Clllillw11111AI - OTHEll (Sp<<lfy In Abl09ct |
| The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 is continuing. | | ,__ ond In To*r, NRC Fonn 366AJ |
| | - l!0.73CalCZllMi l!0.73C.llillHll LICENIEE CONTACT FOii THll LEll (111 I0.71C.ICZllwlllllll I0.71C.llZll*I NAME TELEPHONE NUMllER AREA CODE M. J. Pollack - LER Coordinator 61 O 19 3 I 3 I 9 I- I 4 I O 12 I 2 COMPLETE ONE LINE FOR EACH COlll'ONENT FAILUllE DEICllllED IN THll lll!l'OllT 1131 CAUSE SYSTEM COMPONENT MANUFAC MANUFAC TUR ER TUA ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I IUWLEMl!NTAL AEl'OllT l!Xl'l!CTED 1141 MONTH DAY Y&:AR EXPECTED SUllM18810.N DATE (1111 MYES flf rm. comp- EXl'ECTED SUtlMISSIDN DATEJ I I I A81TllACT (Umlr ID 1"'10 - |
| | * I.&, _,.,.1mor.1y 11,_, Ii,.._ ry~nen l/flll} (111 On 03/07/88 at 1200 hours,.it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surve.illance. The surveillance was over~ue as of 03/01/88. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed surveillance concerns (e.g., LER 272/88-004-00). *The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work acti_vity system, Managed Maintenance Information System (MMIS). The sealed source leak check surveillance was completed 03/14/88. No leaking sources were found. A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance. The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 is continuing. |
| The PSE&G NQA evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00). | | The PSE&G NQA evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00). |
| 8804210047 880413 PDR ADOCK 05000272 S DCD NllCFwm .. (9-83) | | 8804210047 880413 PDR ADOCK 05000272 S DCD NllCFwm . . |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 PLANT AND SYSTEM IDENTIFICATION: | | (9-83) |
| Westinghouse | | |
| -Pressurized Water R;eactor LER NUMBER 88-005-00 PAGE -2 of 4 Energy Industry Identification System (EIIS) codes are identified in the text as {xxl IDENTIFICATION OF OCCURRENCE: | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE - |
| Technical Specification Surveillance 4.7.8.1.2 Performed Late Due To Inadequate Administrative Control Event Date: 03/07/88 Report Date: 03/29/88 This report was initiated by Incident Report No. | | Unit 1 5000272 88-005-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION: |
| | Westinghouse - Pressurized Water R;eactor Energy Industry Identification System (EIIS) codes are identified in the text as {xxl IDENTIFICATION OF OCCURRENCE: |
| | Technical Specification Surveillance 4.7.8.1.2 Performed Late Due To Inadequate Administrative Control Event Date: 03/07/88 Report Date: 03/29/88 This report was initiated by Incident Report No. 88~099. |
| CONDITIONS PRIOR TO OCCURRENCE: | | CONDITIONS PRIOR TO OCCURRENCE: |
| Mode 1 Reactor Power 100% -Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE: | | Mode 1 Reactor Power 100% - Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE: |
| On March 07, 1988 at 1200 hours, it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surveillance. | | On March 07, 1988 at 1200 hours, it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surveillance. The surveillance was overdue as of March 01, 1988. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed sµrveillance concerns (e.g., LER 272/88-004-00). |
| The surveillance was overdue as of March 01, 1988. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed sµrveillance concerns (e.g., LER 272/88-004-00). | | Technicai Specification 3.7.8.1 ~tates: |
| Technicai Specification 3.7.8.1 "Each sealed source containing radioactive material either in excess of 100 microcuries of beta and/or gamma emitting material or 5 microcuries of alpha emitting material shall be free of > 0.005 microcuries of removable contamination." Technical Specification Surveillance 4.7.8.1.2 states: "Test Frequencies | | "Each sealed source containing radioactive material either in excess of 100 microcuries of beta and/or gamma emitting material or 5 microcuries of alpha emitting material shall be free of > |
| -Each category of sealed sources shall be tested at the frequency described below." Technical Specification Surveillances 4.7.'8.l.2.a | | 0.005 microcuries of removable contamination." |
| & b state: "a. Sources in use (excluding startup and fission detectors previously subjected to.core flux) -At least once per six months for all sealed sources containing radioactive materials. | | Technical Specification Surveillance 4.7.8.1.2 states: |
| * -1. With a half life greater than 30 days (excluding Hydrogen 3), and 2. In a*ny form other than gas. | | "Test Frequencies - Each category of sealed sources shall be tested at the frequency described below." |
| r .. LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 DESCRIPTION OF OCCURRENCE (cont'd) LER NUMBER 88-005-00 PAGE 3 of 4 b. Stored sources not in use -Each sealed source and fission detector shall be tested prior to use or transfer to another licensee unless tested within the previous six months. Sealed sources and fission detectors transferred without a certificate i.ndicating | | Technical Specification Surveillances 4.7.'8.l.2.a & b state: |
| *the last test date shall be tested prior to being placed int6 use." APPARENT CAUSE OF OCCURRENCE: | | "a. Sources in use (excluding startup *source~ and fission detectors previously subjected to.core flux) - At least once per six months for all sealed sources containing radioactive materials. * - |
| The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS). When the origianl work activity Inspection Order {IO) system data was transferred to the new MMIS in March 1987, the responsibility to ensure that the data was appropriately formatted resulting in tracking/scheduling of surveillances was not clearly defined. Subsequently, Technical Specification 4 * .7.8.1.2.a was not formatted as required when the MMIS became effective. | | : 1. With a half life greater than 30 days (excluding Hydrogen 3), and |
| Additionally, the Radiation Protection Department was internally reorganized in 1987 resulting in changed assigned departmental superisory responsibilities. | | : 2. In a*ny form other than gas. |
| Sealed source inventory and control resp6nsibility was one of the re-assignments. | | |
| | r |
| | .. |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 3 of 4 DESCRIPTION OF OCCURRENCE (cont'd) |
| | : b. Stored sources not in use - Each sealed source and fission detector shall be tested prior to use or transfer to another licensee unless tested within the previous six months. Sealed sources and fission detectors transferred without a certificate i.ndicating *the last test date shall be tested prior to being placed int6 use." |
| | APPARENT CAUSE OF OCCURRENCE: |
| | The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS). |
| | When the origianl work activity Inspection Order {IO) system data was transferred to the new MMIS in March 1987, the responsibility to ensure that the data was appropriately formatted resulting in tracking/scheduling of surveillances was not clearly defined. |
| | Subsequently, Technical Specification 4 * .7.8.1.2.a was not formatted as required when the MMIS became effective. Additionally, the Radiation Protection Department was internally reorganized in 1987 resulting in changed assigned departmental superisory responsibilities. Sealed source inventory and control resp6nsibility was one of the re-assignments. |
| ANALYSIS OF OCCURRENCE: | | ANALYSIS OF OCCURRENCE: |
| The sealed source leak testing required by Technical Specification Surveillance 4.7.8.2.1.a ensures continued compliance with the limitations as required by Nuclear Regulatory Commission | | The sealed source leak testing required by Technical Specification Surveillance 4.7.8.2.1.a ensures continued compliance with the limitations as required by Nuclear Regulatory Commission {NRC) Code of Federal Regulations. The limitation ensures leakage from byproduct, source, and special nuclear material sources will not exceed allowable intake values. |
| {NRC) Code of Federal Regulations. | | Since the Technical Specification Surveillance requirement *to leak test sealed sources every six months was notmet this event is |
| The limitation ensures leakage from byproduct, source, and special nuclear material sources will not exceed allowable intake values. Since the Technical Specification Surveillance requirement | | * reportable in accordance with the requirements of NRC Code of Federal* |
| *to leak test sealed sources every six months was notmet this event is | | Regulations lOCFR 50.73{a) (2) {i) {B). Subsequent leak.testing of the sealed sources did* not identify any leaking sources, therefore, this event did not affect the health or safety of the public. |
| * reportable in accordance with the requirements of NRC Code of Federal* Regulations lOCFR 50.73{a) (2) {i) {B). Subsequent leak.testing of the sealed sources did* not identify any leaking sources, therefore, this event did not affect the health or safety of the public. CORRECTIVE ACTION: | | CORRECTIVE ACTION: |
| * The sealed source leak check surveillance was completed March 14, 1988. No leaking sources were found. A manual system for tracking surveillances within the Radiation Protection Department has been implemented. | | * The sealed source leak check surveillance was completed March 14, 1988. No leaking sources were found. |
| This will continue until the MMIS is updated to handle this surveillance. | | A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance. |
| The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 | | The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 *is continuing. This review will resolve and clarify Radiation Protection and c*hemistry schedule requirements as well as |
| *is continuing. | | |
| This review will resolve and clarify Radiation Protection and c*hemistry schedule requirements as well as e e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000272 LER NUMBER 88-005-00 to identify who's responsibility it is to conduct these surveillances. | | e e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 4 of 4 CORRECTIVE ACTION: (cont'd) to identify who's responsibility it is to conduct these surveillances. |
| PAGE 4 of 4 The PSE&G Nuclear Quality Assurance evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00)
| | The PSE&G Nuclear Quality Assurance evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00) |
| MJP:pc SORC Mtgo 88-025 General Manager -Salem Operations}} | | ~IJA~~/1fW General Manager - |
| | Salem Operations MJP:pc SORC Mtgo 88-025}} |
LER 88-005-00:on 880307,identified Tech Spec Surveillance 4.7.8.1.2.a,sealed Source Leak Check Not Performed within 6 Months from Prior Surveillance.Caused by Inadequate Administrative Controls Associated W/Computer SysML18093A797 |
Person / Time |
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Site: |
Salem |
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Issue date: |
03/29/1988 |
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From: |
Pollack M Public Service Enterprise Group |
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To: |
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Shared Package |
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ML18093A794 |
List: |
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References |
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LER-88-005-01, LER-88-5-1, NUDOCS 8804210047 |
Download: ML18093A797 (4) |
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Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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NllC For111 . . U.1. NUCLEAll llEOULATOllY COWlllllON (9-831 APPllOVEO OM9 NO. 31ll0-0104 EXPIRES: 8/3119&
LICENSEE EVENT REPORT (LER) .
l'ACILITY NAME (11 DOCKIT NW9111 IZI I r-~~ 1:111 Salem Generatina Station - Unit 1 TITLE l*J Io 15 Io Io Io I~ 17 b 1 loF nl 4 T. S. Surveillance 4.7.S.l.2 Performed Late Due To Inadequate Administrative Control l!VINT OATI! 1111 LEA N..-Ell Ill REl'OllT OATE (7J OTHEll FACILITIEI INVOLVED Ill MONTH QAY YEAR YEAR mt SE~~~:~~.. L tr :i: MONTH DAY YEAR FACILITY NAME!I DOCKET NUMIEAISI Salem - Unit 2 0 161OI0I013 I 111 ol3 ob s s s ls- olols - olo ol3 219 s ls Ol'lllATINO THll llEl'OAT 11 IU*UTTED l'UlllUANT TO THE llEQUlllEMENTI OF 1.0 CFll §: (Ch<<k ono or man of lit* followln1J (111 MODI Ill
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- l!0.73CalCZllMi l!0.73C.llillHll LICENIEE CONTACT FOii THll LEll (111 I0.71C.ICZllwlllllll I0.71C.llZll*I NAME TELEPHONE NUMllER AREA CODE M. J. Pollack - LER Coordinator 61 O 19 3 I 3 I 9 I- I 4 I O 12 I 2 COMPLETE ONE LINE FOR EACH COlll'ONENT FAILUllE DEICllllED IN THll lll!l'OllT 1131 CAUSE SYSTEM COMPONENT MANUFAC MANUFAC TUR ER TUA ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I IUWLEMl!NTAL AEl'OllT l!Xl'l!CTED 1141 MONTH DAY Y&:AR EXPECTED SUllM18810.N DATE (1111 MYES flf rm. comp- EXl'ECTED SUtlMISSIDN DATEJ I I I A81TllACT (Umlr ID 1"'10 -
- I.&, _,.,.1mor.1y 11,_, Ii,.._ ry~nen l/flll} (111 On 03/07/88 at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />,.it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surve.illance. The surveillance was over~ue as of 03/01/88. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed surveillance concerns (e.g., LER 272/88-004-00). *The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work acti_vity system, Managed Maintenance Information System (MMIS). The sealed source leak check surveillance was completed 03/14/88. No leaking sources were found. A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance. The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 is continuing.
The PSE&G NQA evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00).
8804210047 880413 PDR ADOCK 05000272 S DCD NllCFwm . .
(9-83)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE -
Unit 1 5000272 88-005-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water R;eactor Energy Industry Identification System (EIIS) codes are identified in the text as {xxl IDENTIFICATION OF OCCURRENCE:
Technical Specification Surveillance 4.7.8.1.2 Performed Late Due To Inadequate Administrative Control Event Date: 03/07/88 Report Date: 03/29/88 This report was initiated by Incident Report No. 88~099.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100% - Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE:
On March 07, 1988 at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surveillance. The surveillance was overdue as of March 01, 1988. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed sµrveillance concerns (e.g., LER 272/88-004-00).
Technicai Specification 3.7.8.1 ~tates:
"Each sealed source containing radioactive material either in excess of 100 microcuries of beta and/or gamma emitting material or 5 microcuries of alpha emitting material shall be free of >
0.005 microcuries of removable contamination."
Technical Specification Surveillance 4.7.8.1.2 states:
"Test Frequencies - Each category of sealed sources shall be tested at the frequency described below."
Technical Specification Surveillances 4.7.'8.l.2.a & b state:
"a. Sources in use (excluding startup *source~ and fission detectors previously subjected to.core flux) - At least once per six months for all sealed sources containing radioactive materials. * -
- 1. With a half life greater than 30 days (excluding Hydrogen 3), and
- 2. In a*ny form other than gas.
r
..
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 3 of 4 DESCRIPTION OF OCCURRENCE (cont'd)
- b. Stored sources not in use - Each sealed source and fission detector shall be tested prior to use or transfer to another licensee unless tested within the previous six months. Sealed sources and fission detectors transferred without a certificate i.ndicating *the last test date shall be tested prior to being placed int6 use."
APPARENT CAUSE OF OCCURRENCE:
The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS).
When the origianl work activity Inspection Order {IO) system data was transferred to the new MMIS in March 1987, the responsibility to ensure that the data was appropriately formatted resulting in tracking/scheduling of surveillances was not clearly defined.
Subsequently, Technical Specification 4 * .7.8.1.2.a was not formatted as required when the MMIS became effective. Additionally, the Radiation Protection Department was internally reorganized in 1987 resulting in changed assigned departmental superisory responsibilities. Sealed source inventory and control resp6nsibility was one of the re-assignments.
ANALYSIS OF OCCURRENCE:
The sealed source leak testing required by Technical Specification Surveillance 4.7.8.2.1.a ensures continued compliance with the limitations as required by Nuclear Regulatory Commission {NRC) Code of Federal Regulations. The limitation ensures leakage from byproduct, source, and special nuclear material sources will not exceed allowable intake values.
Since the Technical Specification Surveillance requirement *to leak test sealed sources every six months was notmet this event is
- reportable in accordance with the requirements of NRC Code of Federal*
Regulations lOCFR 50.73{a) (2) {i) {B). Subsequent leak.testing of the sealed sources did* not identify any leaking sources, therefore, this event did not affect the health or safety of the public.
CORRECTIVE ACTION:
- The sealed source leak check surveillance was completed March 14, 1988. No leaking sources were found.
A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance.
The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 *is continuing. This review will resolve and clarify Radiation Protection and c*hemistry schedule requirements as well as
e e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 4 of 4 CORRECTIVE ACTION: (cont'd) to identify who's responsibility it is to conduct these surveillances.
The PSE&G Nuclear Quality Assurance evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00)
~IJA~~/1fW General Manager -
Salem Operations MJP:pc SORC Mtgo 88-025