ML18102A488: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 23: Line 23:
The corrunitments are as follows: 1. The Integrated Operating Procedures "Cold Shutdown to Refueling," and "Defueled to Mode 6" (which contain similar acceptance criteria regarding boron concentration) will be revised to include proper criteria and appropriate controls prior to entering Mode 6 for Salem Units 1 and 2. 2. A Technical Specification Surveillance Improvement Program (TSSIP) has been initiated for Salem Units 1 and 2. The scope and content of the TSSIP program was described previously in LER 311/96-008-00.
The corrunitments are as follows: 1. The Integrated Operating Procedures "Cold Shutdown to Refueling," and "Defueled to Mode 6" (which contain similar acceptance criteria regarding boron concentration) will be revised to include proper criteria and appropriate controls prior to entering Mode 6 for Salem Units 1 and 2. 2. A Technical Specification Surveillance Improvement Program (TSSIP) has been initiated for Salem Units 1 and 2. The scope and content of the TSSIP program was described previously in LER 311/96-008-00.
The TSSIP review is expected to be completed December 31, 1997. 3. This LER will be issued to the Operations and Licensing Departments as required reading by November 1, 1996, to further emphasize the appropriate understanding and implementation of Technical Specifications.
The TSSIP review is expected to be completed December 31, 1997. 3. This LER will be issued to the Operations and Licensing Departments as required reading by November 1, 1996, to further emphasize the appropriate understanding and implementation of Technical Specifications.
: 4. Technical Specification  
: 4. Technical Specification 3.9.1 Bases will be revised to reflect that sampling is required without regard to the amount of water in the refueling canal. This will be completed by March 31, 1997.}}
 
====3.9.1 Bases====
will be revised to reflect that sampling is required without regard to the amount of water in the refueling canal. This will be completed by March 31, 1997.}}

Revision as of 14:58, 5 May 2019

Forwards LER 96-011-00 Regarding Missed Surveillance for Sampling Boron Concentration of Refueling Canal as Required by Ts.Commitments Encl as Attachment a
ML18102A488
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/18/1996
From: GARCHOW D F
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A480 List:
References
LR-N96320, NUDOCS 9610290086
Download: ML18102A488 (2)


Text

... -.. *, e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit OCT 18 7996 LR-N96320 U. s. Nuclear Regulatory Commission Document Control Desk \ Washington, DC 20555 Gentlemen:

LER 311/96-011-00 SALEM GENERATING STATION -UNIT 2 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report entitled "Missed Surveillance For Sampling Boron Concentration of Refueling Canal as Required by Technical Specifications" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (i) (B). Attachment DVH c Distribution LER File 3.7 9610290086 961018 PDR ADOCK 05000311 S PDR The power is in your hands. 0 v '-' -Sincerely, General Manager -Salem Operations 95-2168 REV. 6/94

  • . Document Control Desk
  • LR-N96320 Attachment A The following represents the corrunitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Corrunission (NRC) relative to this LER (311/96-011-00).

The corrunitments are as follows: 1. The Integrated Operating Procedures "Cold Shutdown to Refueling," and "Defueled to Mode 6" (which contain similar acceptance criteria regarding boron concentration) will be revised to include proper criteria and appropriate controls prior to entering Mode 6 for Salem Units 1 and 2. 2. A Technical Specification Surveillance Improvement Program (TSSIP) has been initiated for Salem Units 1 and 2. The scope and content of the TSSIP program was described previously in LER 311/96-008-00.

The TSSIP review is expected to be completed December 31, 1997. 3. This LER will be issued to the Operations and Licensing Departments as required reading by November 1, 1996, to further emphasize the appropriate understanding and implementation of Technical Specifications.

4. Technical Specification 3.9.1 Bases will be revised to reflect that sampling is required without regard to the amount of water in the refueling canal. This will be completed by March 31, 1997.