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| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 92-014-oo September 24, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (iv). This report is required to be issued within thirty (30) days of event discovery. | | SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 92-014-oo September 24, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (iv). This report is required to be issued within thirty (30) days of event discovery. |
| * MJP:pc Distribution | | * MJP:pc Distribution |
| (" r.c -. 0 .:Jv 9210020224 920924 PDR ADOCK 05000311 PDR s Sincerely yours, . // /1 Z/ //' //_. / (/tv11!U c. A. Vondra General Manager -Salem Operations NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150*0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). | | (" r.c -. 0 .:Jv 9210020224 920924 PDR ADOCK 05000311 PDR s Sincerely yours, . // /1 Z/ //' //_. / (/tv11!U c. A. Vondra General Manager -Salem Operations NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150*0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). |
| OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) I DOCKET NUMBER (2) I PAGE 131 Salem Statcbon -tJni t 2 o I 5 I o I o I o I 3 11 I 1 1 OF 016 TITLE (4) Reactor trip from 100% power upon opening of the 2A Reactor Trip Breaker. EVENT DATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED 18) MONTH DAY YEAR YEAR HI SEQUENTIAL H? AEV1SION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER o1s1010101 I I q 013 9 2 91 2 -011 14 -0 10 019 214 91 2 0151010101 I I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RtOUIREMENTS OF 10 CFR §:(Chock one or more of the following! | | OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) I DOCKET NUMBER (2) I PAGE 131 Salem Statcbon -tJni t 2 o I 5 I o I o I o I 3 11 I 1 1 OF 016 TITLE (4) Reactor trip from 100% power upon opening of the 2A Reactor Trip Breaker. EVENT DATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED 18) MONTH DAY YEAR YEAR HI SEQUENTIAL H? AEV1SION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER o1s1010101 I I q 013 9 2 91 2 -011 14 -0 10 019 214 91 2 0151010101 I I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RtOUIREMENTS OF 10 CFR §:(Chock one or more of the following! |
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| REPORTABLE | | REPORTABLE |
| ;:; .. :*: *::::-:::;:; | | ;:; .. :*: *::::-:::;:; |
| MANUFAC* REPORTABLE | | MANUFAC* REPORTABLE |
| :*: .. :* "" CAUSE SYSTEM COMPONENT TUR ER TO NPRDS I*>'.'.*'.* | | :*: .. :* "" CAUSE SYSTEM COMPONENT TUR ER TO NPRDS I*>'.'.*'.* |
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| SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION I YES (If yes. comp/ere EXPECTED SUBMISSION DATE! DATE 1151 ' I I I ABSTRACT (Limit ro 1400 spaces. i.e., approximately fifteen single-space typewritten | | SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION I YES (If yes. comp/ere EXPECTED SUBMISSION DATE! DATE 1151 ' I I I ABSTRACT (Limit ro 1400 spaces. i.e., approximately fifteen single-space typewritten |
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| The plant remained in Mode 3 (Hot standby) pending results of investigations into the reactor trip and subsequent plant transient. | | The plant remained in Mode 3 (Hot standby) pending results of investigations into the reactor trip and subsequent plant transient. |
| The Nuclear Regulatory Commission (NRC) was notified of the events as.sociated with the reactor trip, main steamline isolation and the declared Unusual Event in accordance with Code of Federal Regulations lOCFR 50.72. APPARENT CAUSE OF OCCURRENCE: | | The Nuclear Regulatory Commission (NRC) was notified of the events as.sociated with the reactor trip, main steamline isolation and the declared Unusual Event in accordance with Code of Federal Regulations lOCFR 50.72. APPARENT CAUSE OF OCCURRENCE: |
| Investigation of this event included testing of the "2A" RTB. This testing included: | | Investigation of this event included testing of the "2A" RTB. This testing included: |
| : 1) physical manipulation of the breaker to cause it to trip; 2) performing portions_ | | : 1) physical manipulation of the breaker to cause it to trip; 2) performing portions_ |
| of the procedure for "Reactor Trip Bypass AIR circuit Breaker Semi-Annual Inspection, Lubrication and Testing"; | | of the procedure for "Reactor Trip Bypass AIR circuit Breaker Semi-Annual Inspection, Lubrication and Testing"; |
| : 3) performing the procedure for "Train-A Reactor Trip and Reactor Trip Bypass Breakers P-4 Permissive Test" several times; 4) removing the "2A" RTB from its cubicle and inspecting it relative to recent NPRDS data,; and 5) additional field testing which included monitoring during a breaker trip.* Additional investigations included visual of the Solid State Protection System (SSPS) UV card and megger/resistance tests of the cable from the SSPS to the."2A" RTB cubicle. The above testing and inspections did not identify any RTB problems which would have resu1ted in the breaker opening. | | : 3) performing the procedure for "Train-A Reactor Trip and Reactor Trip Bypass Breakers P-4 Permissive Test" several times; 4) removing the "2A" RTB from its cubicle and inspecting it relative to recent NPRDS data,; and 5) additional field testing which included monitoring during a breaker trip.* Additional investigations included visual of the Solid State Protection System (SSPS) UV card and megger/resistance tests of the cable from the SSPS to the."2A" RTB cubicle. The above testing and inspections did not identify any RTB problems which would have resu1ted in the breaker opening. |
| I I I I | | I I I I |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Public Service Electric and _Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 92-014-oo September 24, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (iv). This report is required to be issued within thirty (30) days of event discovery.
(" r.c -. 0 .:Jv 9210020224 920924 PDR ADOCK 05000311 PDR s Sincerely yours, . // /1 Z/ //' //_. / (/tv11!U c. A. Vondra General Manager -Salem Operations NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150*0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104).
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) I DOCKET NUMBER (2) I PAGE 131 Salem Statcbon -tJni t 2 o I 5 I o I o I o I 3 11 I 1 1 OF 016 TITLE (4) Reactor trip from 100% power upon opening of the 2A Reactor Trip Breaker. EVENT DATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED 18) MONTH DAY YEAR YEAR HI SEQUENTIAL H? AEV1SION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER o1s1010101 I I q 013 9 2 91 2 -011 14 -0 10 019 214 91 2 0151010101 I I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RtOUIREMENTS OF 10 CFR §:(Chock one or more of the following!
1111 MODE 19) 1 20.402lb) 20.4051c)
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LICENSEE CONTACT FOR THIS LER 112) NAME TELEPHONE NUMBER AREA CODE M.J. Pollack -LER Coordinator 610 19 3 13 , -,2 p ,2 ,2 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 ))'.;; ;.; .. ;.; *'.*'. [=}?>
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SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION I YES (If yes. comp/ere EXPECTED SUBMISSION DATE! DATE 1151 ' I I I ABSTRACT (Limit ro 1400 spaces. i.e., approximately fifteen single-space typewritten
_lines) (16) On 9/3/92, at 0917-hours a reactor trip occurred due to the II A II Reactor Trip Breaker (RTB) opening. Following the reactor trip, a cool down occurred.
Auxiliary Feedwater was reduced and the MSlO valves (atmospheric relief valves) were verified closed. However, the cool down continued and manual Main steamline Isolation (MSI) was initiated stopping the cooldown.
After the MSI, Reactor Coolant System (RCS) pressure and temperature reached maximum levels of 2280 psig and 552° F. The Pressurizer Master Controller was taken to manual. Pressurizer SP,ray was initiated and pressure reduced and stabilized at 2235 psig. At 0936 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.56148e-4 months <br />, the 21MS15 and 22MS15 main steam.safety valves lifted. The 21MS10 and 22MS10 valves had not opened. At 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, an "Unusual Event" was declared for, 11 SG Safety Failure to Reseat". The Unusual Event was terminated with the plant in Mode 3. Investigation of this event included testing of the "2A 11.RTB which did not identify any RTB problems.
The cause of the reactor trip is attributed to personnel error. An NEO exhibited poor judgement resulting in a sequence of events leading to the trip. Appropriate disciplinary action has been taken with the individual involved.
The reactor trip and events following the trip will be reviewed by the Nuclear Training Center. Investigation of a Pressurizer pressure master controller concern is continuing.
The MSlO control concerns have been investigated by engineering and design changes are.planned.
The breaker in the II 2A II RTB cabinet is being sent to Westinghouse to verify that it functions per design. NRC Form 366 (6-891
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION . Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse
-Pressurized Water Reactor . LER NUMBER 92-014-00 PAGE 2 of 6 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE:
Reactor Trip from 100% power upon opening of the 2A Reactor Trip Breaker Event Date: 9/3/92 Report Date: 9/24/92 This report was initiated by Incident Report No.92-567. CONDITIONS PRIOR TO OCCURRENCE:
Mode *1 Reactor Power 100% Unit Load 1150 MWe DESCRIPTION OF OCCURRENCE:
On September 3, 1992, at .0917 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.489185e-4 months <br />, during normal power.operation, a reactor trip occurred with a fiist out alarm of "power range neutron flux rate high". At the time of the event, no maintenance -was in
- progress which could be attributed to the trip. Investigation revealed that the "A" Reactor Trip.Breaker (RTB) had opened resulting in the control rods dropping into the core causing the negative rate reactor trip signal. Per design, the "B" RTB opened approximately 22 cycles after event initiation.
- The turbine/ generator tripped following the reactor trlp. Following the reactor trip, a cooldown occurred.
In accordance with. Emergency Operating Procedure EOP-TRIP.-2, Auxiliary Feedwater was reduced from 44E04 lbm/hr to 22E04 lb /hr and the MSlO valves * (atmospheric relief valves).were verified closed. However, the cooldown continued and, at 0921 hours0.0107 days <br />0.256 hours <br />0.00152 weeks <br />3.504405e-4 months <br />, a_ manual Main Steamline Isolation (MSI) (an Engineered Safety Feature) was initiated stopping the cooldown, in accordance with the EOP procedure.
After.the MSI, Reactor Coolant System (RCS) {AB} pressure and temperature reached maximum levels of '22so psig and 552°F, respectively.
Based upon an elevated Pressurizer Pressure Operated Relief Valve (PORV) tailpipe temperature of 191°F, and pressure spikes observed.in the Pressurizer Relief Tank (PRT), the Pressurizer Master Controller was taken to manual. Pressurizer Spray was initiated and pressure reduced and stabilized at 2235 psig. The Pressurizer Power Operated Relief Valves (PORVs) were not observed to hav*e lifted. *
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 DESCRIPTION OF OCCURRENCE: (cont'd) LER NUMBER 92-014-00 PAGE 3 of 6 At 0936 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.56148e-4 months <br />, the 21MS15 and main steam safety valves . lifted. Main steamline pressure was 1052 psig. This is above the 1000 psig setpoint fo_r the 21MS10 and 22MS10 valves; however, they . did not open. This allowed T. to rise subsequentty causing steam . ,
- avg * . . pressure to rise until the MS15 valve setpoints were reached.
- At 0*952 hours, the two (2) MS15 valves were still open with steamline pressure at 980 psig. consequently at 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, an i*unusual Event" was declared in accordance with Section 2A of the Emergency Classification Guide, "SG Safety Failure to At 1029 a,nd 1041 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.961005e-4 months <br />, respectively, -the 21 & *22MS15 valves were observed closed. Plant heatup was then initiated from an initial of 530°F to minimize risk of safety injection.
The T v 541°F for*safety injection logic of low T a 9 * * * * ,
- a v.g coincident with high steam flow in two of four steamlines.
At 1235 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.699175e-4 months <br />, the plant heatup was terminated due to observed steam release from the 21 and 22MS15 valves. Procedure IOP-6, "Hot Standby to Cold Shutdown" was initiated.
_At 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, a plant cooldown commenced.
Upon reaching a T vg of 530°F with the 21 and 22MS15 valves observed to:be fully c1osed, the Unusual Event was terminated.
The plant remained in Mode 3 (Hot standby) pending results of investigations into the reactor trip and subsequent plant transient.
The Nuclear Regulatory Commission (NRC) was notified of the events as.sociated with the reactor trip, main steamline isolation and the declared Unusual Event in accordance with Code of Federal Regulations lOCFR 50.72. APPARENT CAUSE OF OCCURRENCE:
Investigation of this event included testing of the "2A" RTB. This testing included:
- 1) physical manipulation of the breaker to cause it to trip; 2) performing portions_
of the procedure for "Reactor Trip Bypass AIR circuit Breaker Semi-Annual Inspection, Lubrication and Testing";
- 3) performing the procedure for "Train-A Reactor Trip and Reactor Trip Bypass Breakers P-4 Permissive Test" several times; 4) removing the "2A" RTB from its cubicle and inspecting it relative to recent NPRDS data,; and 5) additional field testing which included monitoring during a breaker trip.* Additional investigations included visual of the Solid State Protection System (SSPS) UV card and megger/resistance tests of the cable from the SSPS to the."2A" RTB cubicle. The above testing and inspections did not identify any RTB problems which would have resu1ted in the breaker opening.
I I I I
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station Unit 2 APPARENT CAUSE OF OCCURRENCE:
DOCKET NUMBER 5000311 (cont'd) LER NUMBER 92-01"4-00 -PAGE 4 of 6 Prior to the trip, a Nuclear Equipment Operator (NEO), was assigned to rack-in the Salem Unit 1 "lB" Reactor Trip Bypass Breaker in support of surveillance testing. After entering the Unit 1 switchgear Room, the NEO left the I&C technicians and went to the Unit 2 Switchgear Room to view the Unit 2 "2A 11-RTBB. He did this to reassure himself of the appearance of a racked out breaker. Upon entering the Unit 2 Switchgear Room, he states that he opened the "2A" RTBB door and studied the position of the racked out breaker for several seconds._
While viewing the breaker, he heard the Unit 2 RTBs open. Based on investigation, the cause of the reactor trip is attributed to personnel error. It was determined that the NEO exhibited poor judgement resulting in a sequence of events leading to the trip. The NEO did not inform the Control Room or seek supervisory guidance before going to the 11 2A" RTBB cabinet to open it. The cabinet is clearly marked as a trip hazard. Also, the NEO stated that he was not aware of procedure Sl.OP-SO.RCP-0002, "Reactor Trip or Reactor Trip Bypass Operations".
It details the operation of the RTBs. -Due to the nature of this procedure, it is not required-to be at the job site in support of work since the procedure tasks involve routine equipment operation. --Further review of this event revealeq that the physical arrangement of the Salem Unit 1 and Salem Unit 2RTBB and RTB cabinets are reversed.
This factor contributed to the determination that the NEO opened the n2A 11 RTB _cabinet instead of the "2A RTBB capinet. ANALYSIS OF OCCURRENCE:
There are two (2) reactor trip breakers ("A" and "B") in series, which connect the output of the rod drive motor generator sets to the rod control power cabinets.
- -In the -event of a reactor trip signal, these breakers open, removing power from the control rod drive mechanisms allowing the control rods to drop into the reactor core. The opening of either breaker will cause this to occur. Two (2) RTBBs are provided to allow surveillance testing at power. The sequence of events as recorded by the P-250 computer confirmed that the "2A" RTB opened first. The first out indication would be the "power range neutron flux rate high" and the 11 2B" RTB would open a few cycles later. The reduction in T , re*quiring MSI, has been experienced , -avg , , during other reactor trips Unit 2 LER 311/92-009-00).
Engineering has investigated Tavq reduction (during trips) and design modifications are being assessed. . . A low pressurizer level signal occurred resulting in RCS letdown isolation.
--This signal was due to the cooldown (prior to MSI) and
- ** ,* LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station :Unit*2. ANALYSIS OF OCCURRENCE:
DOCKET NUMBER 5000311 (cont'd) LER NUMBER 92-014-00 PAGE 5' of 6 the low power history of the core. Charging.
flow remained established resulting in an increase of pressurizer pressure to approximately 2280 psig. The pressurizer spray actuation setpoint is* 2260_psig
.. As stated previously, the operators placed the master pressure controller in manual and initiated pressurizer spray. Investigation of this concern included performance of applicable
The controller was. calibrated and its operability was checked and found satisfactory.
Investigation into the pressurizer master controller concern is continuing.
Following the main steamline isolation, the 21 and 22MS15 valves* lifted with the RCS at a temperature of 552°F. This correlates to a steam generator header pressure of 1051 psig. Recorded steam pressures for the 21 and 22 steamlines were 1030 psig and 1036 psig, respectively.
Each valve lifted at least twice prior to plant stabilization at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />. There are five (5) main steamline safety valves*per steamline with the MS15 valves having the lowest setpoint (1070 psig). These valves operated for approximately one (1) hour during the . event. The steam flow that passed through the_ valves during the time they were open heated the valve* body and springs. This results in . lift set and reset.pressure reduction.
Following the event, the valves* were lift set tested. The as .found data were 1047 psig for 21MS15 and 1017 psig for 22MS15. The 1017 *psig for the 22MS15 is questionable due to a failed air motor. Both valves were recalibrated and left within 1% of set pressure.
Further investigation revealed that the 23MS15 valve reached a .pressure of 1045 psig; however, it did not lift. It was lift set tested with as found readings of 1097 psig. It too was The valve manufacturer (Crosby) was contacted.
No abnormalities or inconsistencies were noted with the MS15 valve operation or subsequent findings.
Main steamline safety valve lifting has occurred previously.
On August 8, 1985 reference LER 311/85-005-00), a similar event occurred where the "2A" RTB opened* followed by the lifting of main steamline safety valves. Following the 1985 event, investigation was conducted to determine why the MSlO valves did not respond preventing the main steamline safety valve lift.' It was determined that the MSlO controllers (set at 1000 psig) experience saturation and a subsequent "reset windup" phenomenon.
Design changes are planned to address this concern. The reactor trip and subsequent opening of the MS15 valves did not affect the health and safety of the public. Operator actions were appropriate to mitigate the subsequent transient.
The reactor trip fl\ ; * ** LICENSEE EVENT REPORT (LER)
CONTINUATION Salem Generating Station Unit 2* DOCKET NUMBER 5000311 ANALYSIS OF OCCURRENCE:
LER.NUMBER 92-014-00 PAGE 6 of 6 and manual main steamline isolation events are reportable to NRC in accordance with Code of Federal Regulations lOCFR 50.73(a) (2) (iv) . . CORRECTIVE ACTION: Operations*
management has reviewed the events associated with the reactor trip. Appropriate disciplinary action is being assessed regarding the individual involved in the event. The reactor trip.and events following the trip will.be reviewed by the Nuclear Training Center. Licensed and Operator training will be enhanced as appropriate.
Administrative procedure NC.NA-AP.ZZ-0005(Q), "Station Operating Practices", will be revised to require shift notification and -approval for accessing equipment posted with "Trip Hazard"_signs.
As identified in the Description of Occurrence
_a Pressurizer pressure control concern occurred.
Investigation included performance of applicable sections of procedure 2PD-2;1.os2, "2PC-455K Pressurizer Pressure Control".
The controller was calibrated and its operability was checked and found satisfactory.
Investigation into the pressurizer master controller concern is continuing.
The MSlO control concerns .have been investigated by engineering.
Modifications are planned for MSlO controls.
The effects of "reset wind-up" phenomenon will be accounted for so that the valves will operate at their proper setpoint.
'The breaker in the 11 2A" RTB cabinet, at the time of the trip, is being sent to Westinghouse to verify that it functions per design. ( MJP:pc SORC Mtg.92-105 //d'./ I General Manager -Salem Operations