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| MODE (9) N 20.2201(b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) 50.73(a)(2)(viii) | | MODE (9) N 20.2201(b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) 50.73(a)(2)(viii) |
| POWER 20.2203(a)(1) 20.2203(a)(3)(i) x 50. 73(a)(2)(ii) 50. 73(a)(2)(x) | | POWER 20.2203(a)(1) 20.2203(a)(3)(i) x 50. 73(a)(2)(ii) 50. 73(a)(2)(x) |
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| LEVEL (10) 000 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)( 4) 50. 73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) S~~in Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) | | LEVEL (10) 000 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)( 4) 50. 73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) S~~in Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) |
| LICENSEE CONTACT FOR THIS LER (12) | | LICENSEE CONTACT FOR THIS LER (12) |
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| \NOUld start, and may cause overa>Oling of the area. In addition, during the revie.v of the SPAV system, dampers that are designed to isolate the area upon COi injection for fire suppression, were noted to fall close on a loss of power. Closure of the COi Isolation dampers upon loss of power could cause a loss of ventilation to the switchgear room, and potentially result in the area temperatures exceeding design temperatures. | | \NOUld start, and may cause overa>Oling of the area. In addition, during the revie.v of the SPAV system, dampers that are designed to isolate the area upon COi injection for fire suppression, were noted to fall close on a loss of power. Closure of the COi Isolation dampers upon loss of power could cause a loss of ventilation to the switchgear room, and potentially result in the area temperatures exceeding design temperatures. |
| The cause of this occurrence is that the SPAV system failure modes were not proper1y established and evaluated during the initial plant design. The interim corrective actions are to install temporary modifications to ensure design temperatures can be maintained. The Switchgear room temperatures are being monitored to ensure that design temperatures are not exceeded. | | The cause of this occurrence is that the SPAV system failure modes were not proper1y established and evaluated during the initial plant design. The interim corrective actions are to install temporary modifications to ensure design temperatures can be maintained. The Switchgear room temperatures are being monitored to ensure that design temperatures are not exceeded. |
| These interim correclive actions will be in place until permanent oorrective actions are installed. The SPAV control logic and the COi isolation damper logic will be revised to ensure that area temperatures can be mainta.ined within design limits. This condition is reportable in accordance with 1OCFR 50. 73(a)(2)QQ(A), any event or condition that resulted in the nuclear power plan+ being operated outside the desigr '1ases. | | These interim correclive actions will be in place until permanent oorrective actions are installed. The SPAV control logic and the COi isolation damper logic will be revised to ensure that area temperatures can be mainta.ined within design limits. This condition is reportable in accordance with 10CFR 50. 73(a)(2)QQ(A), any event or condition that resulted in the nuclear power plan+ being operated outside the desigr '1ases. |
| NRC FORM 366 (4-95) | | NRC FORM 366 (4-95) |
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| NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95) | | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95) |
| LICENSEE EVENT REPORT (LER) | | LICENSEE EVENT REPORT (LER) |
| TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER .NUMBER (6) PAGE (3) 05000272 YEAR | | TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER .NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 3 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| * I SEQUENTIAL NUMBER I REVISION NUMBER 3 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
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| DESCRIPTION OF OCCURRENCE (cont'd) | | DESCRIPTION OF OCCURRENCE (cont'd) |
| Overheating on MAC 11/21 panel failure During the review of the SPAV system, dampers that are designed to isolate upon COiinjection for fire suppression, YJere also noted to fail close on a loss of po.yer. This loss of pcM'er could cause a loss of ventilation, and potentially result in area temperatures exceeding design temperatures. | | Overheating on MAC 11/21 panel failure During the review of the SPAV system, dampers that are designed to isolate upon COiinjection for fire suppression, YJere also noted to fail close on a loss of po.yer. This loss of pcM'er could cause a loss of ventilation, and potentially result in area temperatures exceeding design temperatures. |
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| NRC FORM 366A (4-95) | | NRC FORM 366A (4-95) |
| * LICENSEE EVENT REPORT (LER) | | * LICENSEE EVENT REPORT (LER) |
| TEXT CONTINUATION | | TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 4 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| * U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 4 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
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| SAFETY CONSEQUENCES AND IMPLICATIONS Overcooling The overcooling of the Switchgear rooms would occur only with extremely low outside air temperatures, and would be a concern with the -"C" 125 Vdc battery room. The "C" 125 Vdc battery room has a non-safety related heater installed. While the heater could not be relied upon to maintain temperatures above 65 degrees F, the heater would most likely prevent the room from falling below design temperature. Further, the plant is designed with sufficient redundant DC power sources to safely shutdown with the failure of the "C" 125 Vdc batteries. In addition, other equipment in the area may be adversely effected. | | SAFETY CONSEQUENCES AND IMPLICATIONS Overcooling The overcooling of the Switchgear rooms would occur only with extremely low outside air temperatures, and would be a concern with the -"C" 125 Vdc battery room. The "C" 125 Vdc battery room has a non-safety related heater installed. While the heater could not be relied upon to maintain temperatures above 65 degrees F, the heater would most likely prevent the room from falling below design temperature. Further, the plant is designed with sufficient redundant DC power sources to safely shutdown with the failure of the "C" 125 Vdc batteries. In addition, other equipment in the area may be adversely effected. |
| Overheating on MAC 11/21 Panel failure The maximum room temperature with the C02 Isolation dampers closed has been preliminary determined to exceed 11 O degrees. The maximum room temperature has not been determined, but some safety related equipment may be adversely impacted. The loss of the MAC 11/21 panel is indicated in the Control Room. | | Overheating on MAC 11/21 Panel failure The maximum room temperature with the C02 Isolation dampers closed has been preliminary determined to exceed 11 O degrees. The maximum room temperature has not been determined, but some safety related equipment may be adversely impacted. The loss of the MAC 11/21 panel is indicated in the Control Room. |
Similar Documents at Salem |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
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OPS~G *
- Public Service Electric and Gas Company P.O, Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit MAY 0 9 1997 LR-N97296 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/96-038-01 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 Gentlemen:
This Licensee Event Report (LER) entitled ~switchgear Penetration ,
Area Ventilation Cannot Maintain Design Temperatures" is being submitted as a Supplement to LER 96-038. This LER is submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (ii).
General Manager Salem Operations Attachment DVH C Distribution LER File 3.7 9705190271 970509 PDR ADOCK 05000272 S PDR 190005 Illllll lllll lllll llllll llll llllll Ill llll
- 1ne pcwer is in ~1. x.lf han._k 95-2168 REV. 6/94
NRCFORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPR:OVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04130/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD
'. COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T~ F3~ NUCLEAR (See reverse for required number of REGULATORY COMfllllSSION, WASHINGTON, DC 20 , AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAllE (1) UUCIU:T NUllBER (2) PAGE (3)
SALEM GENERATING STATION UNIT 1 05000272 1 OF 4
~~iI~~~ar Penetration Area Ventilation Cannot Maintain Design Temperatures EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR I SEQUENTIAL NUMBER IREVISION NUMBER MONTH DAY YEAR FACILITY NAME SALEM UNIT2 DOCKET NUMBER 05000311 12 10 96 96 -- 038 -- 01 05 97 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE (9) N 20.2201(b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) x 50. 73(a)(2)(ii) 50. 73(a)(2)(x)
LEVEL (10) 000 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)( 4) 50. 73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) S~~in Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Ar1111 Code)
Brian J. Thomas, LER Coordinator 609-339-2022 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
I ~:::::::~~=:::::::~==~
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS IYES SUPPLEMENTAL REPORT EXPECTED (14)
(If yes, complete EXPECTED SUBMISSION DATE).
I xi NO EXPECTED SUBMISSION DATE(15)
MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
LER 96-038-00 detailed a concern with single failure of the Elecbical Penetration Exhaust Fans. LER 96-038-01 details concerns identified during a revie.v of LER 96-038-00. Specifically, during a revie.v of the Switchgear & Penetration Area Ventlation (SPAV) system performance, PSE&G detennined that the SPAV system may not be able to maintain the minimum design bases temperatures during cold vveather. Upon receipt of an accident signal, all three of the SPAV system supply fans
\NOUld start, and may cause overa>Oling of the area. In addition, during the revie.v of the SPAV system, dampers that are designed to isolate the area upon COi injection for fire suppression, were noted to fall close on a loss of power. Closure of the COi Isolation dampers upon loss of power could cause a loss of ventilation to the switchgear room, and potentially result in the area temperatures exceeding design temperatures.
The cause of this occurrence is that the SPAV system failure modes were not proper1y established and evaluated during the initial plant design. The interim corrective actions are to install temporary modifications to ensure design temperatures can be maintained. The Switchgear room temperatures are being monitored to ensure that design temperatures are not exceeded.
These interim correclive actions will be in place until permanent oorrective actions are installed. The SPAV control logic and the COi isolation damper logic will be revised to ensure that area temperatures can be mainta.ined within design limits. This condition is reportable in accordance with 10CFR 50. 73(a)(2)QQ(A), any event or condition that resulted in the nuclear power plan+ being operated outside the desigr '1ases.
NRC FORM 366 (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 2 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
PLANT AND SYSTEM IDENTIFICATION Westinghouse - Pressurized Water Reactor Switchgear Ventilation System {VF/-}*
DC Power* {EJ/-}
Low Voltage Power System {EC/-}
- Energy Industry Identification System (EllS) codes and component function identifier codes appear as (SS/CC) -
CONDITIONS PRIOR TO OCCURRENCE At the time of identification, Salem Unit 1 was defueled and Unit 2 was in Mode 5. Post modification t~sting was in progress for the Switchgear Penetration Area Ventilation (SPAV) system modification. '
DESCRIPTION OF OCCURRENCE During a design review of the Switchgear Penetration Area Ventilation (SPAV) {VF/-} system performance, PSE&G determined that the potential existed for a single failure of the Electrical Penetration Exhaust Fans
{VF/FAN} to place the unit in an unanalyzed condition. The two Electrical Penetration Exhaust Fans each provide 50 percent of the exhaust flow from the penetration areas. The failure of one fan could result in higher than analyzed temperatures in the Electrical Penetration area, which contains the motor control centers for the three trains of safety-related, motor-operated valves and other Technical Specification required instrumentation.
The SPAV system is currently designed to maintain year-round temperatures between 65 and 110 degrees F within the areas served, with outdoor ambient conditions of 0 degrees F winter and 95 degrees F summer, respectively. The maximum design temperature was recently incre~sed to 110 degrees from 105 degrees F.
The potential for a single failure of the Electrical Penetration Exhaust fan to place the unit in an unanalyzed condition was previously detailed in Revision 0 to LER 96-038. Revision 1 to LER 96-038 will detail two recently identified concerns with the SPAV system: 1) overcooling and 2) overheating on a Miscellaneous Auxiliary Control (MAC) 11 panel failure for Unit 1 or a MAC 21 panel failure for Unit 2.
Overcooling Duling Post Modification Testing for recently completed SPAV system modifications and review of the SPAV system performance, PSE&G determined that the SPAV system may not be able to maintain the minimum design temperabJres during cold weather conditions. Upon receipt of a Safeguards Equipment Cabinet (SEC) signal Q.e., an Engineered Safety Feature start) all three of the SPAV system supply fans would start Wllh all three supply fans running,* and cold outside air temperabJres, area temperatures could drop below the design minimum temperature of 65 degrees F.
NRC FORM 366A (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER .NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 3 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE (cont'd)
Overheating on MAC 11/21 panel failure During the review of the SPAV system, dampers that are designed to isolate upon COiinjection for fire suppression, YJere also noted to fail close on a loss of po.yer. This loss of pcM'er could cause a loss of ventilation, and potentially result in area temperatures exceeding design temperatures.
~. there are six COi Isolation dampers in each unit that are designed to close, to control COi flooding in the event of a fire. The control pcM'erforthese COi Isolation dampers sis supplied by the MAC 11 panel for Unit 1, and the MAC 21 panel for Unit 2. A failure of the MAC 11 panel or the MAC 21 panel 'M>Uld cause the COz Isolation dampers for that unit to close. The clOsing of these COz Isolation dampers 'M>llld interrupt ventilation air flow and could result in the area temperatures exceediilg design temperatures.
CAUSE OF OCCURRENCE The cause of this occurrence is that the SPAV system failure modes were not properly established and evaluated during the initial plant design, and the impact of the damper closure due to loss of power was not considefed. Damper closure was assessed in terms of supporting the automatic initiation of the C02 suppression system in response to 10 CFR 50 Appendix R concerns.
PRIOR SIMILAR OCCURRENCES LER 272/95-008-00 reported a similar concern of exceeding 105 degrees if only one of the three Electrical Penetration Supply Fans were operable. This occurrence was caused by the failure of two of the supply fans.
LER corrective actions addressed the supply fans and did not address the exhaust fans.
In the past two years there were eleven LERs that addressed design deficiencies as the cause. These LERs are 272/95-014-00, 272/95-020-00, 272/95-029-00, 272/96-001-00, 272/96-010-00, 272/96-012-00, 272/96-018-00, 272/96-019-00, 272/96-020-00, 272/96-034-00 and 272/96-037-00. Corrective actions for these LERs were specific to the particular issue. As stated in the 50.54(f) response, PSE&G has reason.able assurance that Salem stations are being operated in accordance with their design bases NRC FORM 366A (4-95)
NRC FORM 366A (4-95)
- LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 4 OF 4 SALEM GENERATING STATION UNIT 1 96 -- 038 -- 01 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
SAFETY CONSEQUENCES AND IMPLICATIONS Overcooling The overcooling of the Switchgear rooms would occur only with extremely low outside air temperatures, and would be a concern with the -"C" 125 Vdc battery room. The "C" 125 Vdc battery room has a non-safety related heater installed. While the heater could not be relied upon to maintain temperatures above 65 degrees F, the heater would most likely prevent the room from falling below design temperature. Further, the plant is designed with sufficient redundant DC power sources to safely shutdown with the failure of the "C" 125 Vdc batteries. In addition, other equipment in the area may be adversely effected.
Overheating on MAC 11/21 Panel failure The maximum room temperature with the C02 Isolation dampers closed has been preliminary determined to exceed 11 O degrees. The maximum room temperature has not been determined, but some safety related equipment may be adversely impacted. The loss of the MAC 11/21 panel is indicated in the Control Room.
The Control Room response includes notifying the fire protection personnel. To mitigate the elevated room temperatures, the C02 Isolation dampers would have to be opened, or ttie room doors opened.
The health and safety of the public was not affected.
CORRECTIVE ACTIONS
- 1.
- A design review of the SPAV system in response to LER 96-038-00 has been completed. This review identified the concerns addressed in this LER.
- 2. A 10CFR50.59 Evaluation was completed to increase the maximum design temperature to 110 degrees.
- 3. Administrative controls to address removal from service of an Electrical Penetration Exhaust Fan will be implemented prior to Salem Unit 2 entering Mode 4. The outside air intake dampers were modified to enable them to fully close to preclude reducing area temperatures to below acceptable design minimums.
- 4. A modification to the supply fan start logic, and the outside supply dampers will be implemented to ensure that the minimum design temperature is maintained. This modification is scheduled to be completed for both Units by May 31, 1997.
- 5. As an interim corrective action, the Switchgear room temperature is being routinely monitored to ensure that the_ maximum design temperature is not exceeded, and controls are in place to limit temperature increases in the area.
- 6. As a permanent .corrective action, a modification to the C02 damper logic is scheduled to be completed for both Units Unit by May 31, 1997.
NRC FORM 366A (4-95)