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| {{#Wiki_filter:e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 | | {{#Wiki_filter:e PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station October 7, 1993 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
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| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 October 7, 1993 SUPPLEMENTAL LICENSEE EVENT REPORT 92-026-02 This supplemental Licensee Event Report is being submitted pursuant to Code of Federal Regulations 50.73. The report has been modified based upon investigation results and identifies the current status of corrective actions. MJPJ:pc Distribution 150057 931007 s OCK 05000272 . PDR The power is in your hands. Sincerely yours, c. A. Vondra General Manager -Salem Operations | | |
| :rE. z..i. ". 95-2189 REV 7-92
| | SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 SUPPLEMENTAL LICENSEE EVENT REPORT 92-026-02 This supplemental Licensee Event Report is being submitted pursuant to Code of Federal Regulations lOCF~ 50.73. The report has been modified based upon investigation results and identifies the current status of corrective actions. |
| \fl NRC FORM 366 (6-89) U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 LICENSEE EVENT REPORT (LERI ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF M_ANAGEMENT AND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (1) 'DOCKET NUMBER (21 I PAGE 131 Salem Generating Station -Unit 1 o 1s101010121712 1!0F 015 TITLE (4) ESF Actuations Initiated From The Radiation Monitoring System. EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) MONTH DAY YEAR YEAR :::::::::::SEQUENTIAL o::;:;:: REVISION *'.*'.*:*:*:* | | Sincerely yours, |
| NUMBER .;:;:;:::: | | : c. A. Vondra General Manager - |
| NUMBER MONTH DAY YEAR FACI L/TY NAMES DOCKET NUMBER(S) i I 2 i I 3 9 2 9 I 2 -o l 2 l 6 -o I 2 i l o o 17 9 I 3 OPERATING MODE (9) THIS REPORT IS SUBMITTED PURSUANT TO THE OF 10 CFR §: (Check one or more of lh* following) | | Salem Operations MJPJ:pc Distribution 150057 |
| (11) 1 20.402(b) 20,405(c) x 50.73(1)(2)(iv) 73.71(b) '--,_ '----20.406(1)(1 | | ~fiA 0 1~noa14 931007 s OCK 05000272 |
| )(i) 50.36(c)(1) 50.73(1)(2)(v) 73.71(c) ---20.405(1)(1 | | . PDR The power is in your hands. :rE. z..i. |
| )(ji) 50.36(c)(2) 50.73(1J(2)(viil OTHER (Specify in Absrrocl LEVEL l O O 1--POWER I (10) I I ....__ lllilll= ....__ ,__ btJ/ow tJnd in Tt1xt, NRC Form 20.405(1)(1 | | 95-2189 REV 7-92 |
| )(iii) 50.73(1)(2J(i) 50.73(1)(2)(viiil(A) | | |
| '--,..._ 20.405(1)(1)(lv) 50,73(1Jl2llii) 50.73(1) (2) (viii) (B) ....__ ....__ 20.406(1)(1
| | \fl NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF M_ANAGEMENT AND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (1) DOCKET NUMBER (21 I PAGE 131 Salem Generating Station - Unit 1 o 1s101010121712 1!0F 015 TITLE (4) |
| )(v) 50.73(1)(2)(111) 50.73(1)(2)(x)
| | ESF Actuations Initiated From The Radiation Monitoring System. |
| LICENSEE CONTACT FOR THIS LER (12) NAME AREA CODE M. J. Pollack -LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT B I I I I MANUFAC* TUR ER W 11 I 210 I I I y I I I I I I I I MANUFAC* TUR ER I I I I I I 366A) TELEPHONE NUMBER SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR l YES (If yes, compl*le EXPECTED SUBMISSION DA TEI ABSTRACT (Limit to 1400 spactJs, i.tJ., tJpproximtJtBly fiftatJn single*spact1 typ11writt1Jn
| | EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| /int1sl (16) EXPECTED SUBMISSION DATE 1151 I ' This supplemental LER addresses investigation results and identifies the current status of corrective actions associated with 4 Engineered Safety Feature (ESF) actuations initiated by the lRllA Radiation Monitoring system (RMS} channel. The lRllA RMS Channel monitors the Containment atmosphere for particulate activity. | | MONTH DAY YEAR YEAR :::::::::::SEQUENTIAL o::;:;:: REVISION DAY YEAR FACI L/TY NAMES DOCKET NUMBER(S) |
| The ESF signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR)
| | *'.*'.*:*:*:* NUMBER .;:;:;:::: NUMBER MONTH i I2 i I 3 9 2 9 I 2 - o l 2 l6 - oI2 i l o o 17 I 9 3 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE R~QUIREMENTS OF 10 CFR §: (Check one or more of lh* following) (11) |
| System isolation.
| | MODE (9) 1 x I ,_ |
| At the time of the events, the associated valves were closed and did not change position.
| | 20.402(b) 20,405(c) 50.73(1)(2)(iv) 73.71(b) |
| Two of the events occurred on 12/13/92, one on 12/30/92, and one on 1/25/93. Investigation determined that the lRllA RMS channel was responding to actual increases in containment airborne radioactivity; i.e., Rb-88 activity (half life of 17.8 minutes) which is a decay product of Kr-88, a fission product. Contributing leakage sources included:
| | POWER LEVEL (10) l I O I O 1-- |
| : 1) lPSl Pressurizer Spray air operated valve bonnet leak; 2) pipe flange leakage, immediately upstream of the Reactor head vent manual isolation valve, 1RC900; 3) Pressurizer manway leakage past its gasket seal; and 4) Pressurizer Relief Tank rupture disk pinhole leakage. NRC Form 366 (6-89) I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 PLANT AND SYSTEM IDENTIFICATION:
| | 20.406(1)(1 )(i) 20.405(1)(1 )(ji) 50.36(c)(1) 50.36(c)(2) 50.73(1)(2)(v) 50.73(1J(2)(viil 73.71(c) |
| Westinghouse
| | OTHER (Specify in Absrrocl btJ/ow tJnd in Tt1xt, NRC Form lllilll= |
| -Pressurized Water Reactor LER NUMBER 92-026-02 PAGE 2 of 5 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE: | | 20.405(1)(1 )(iii) 50.73(1)(2J(i) 50.73(1)(2)(viiil(A) 366A) 20.405(1)(1)(lv) 50,73(1Jl2llii) 50.73(1) (2) (viii) (B) 20.406(1)(1 )(v) 50.73(1)(2)(111) 50.73(1)(2)(x) |
| Engineered Safety Feature actuations initiated from the Radiation Monitoring System Event Dates: 12/13/92, 12/30/92 and 1/25/93 Report Date: 10/7/93 This supplemental LER addresses investigation results and identifies l the current status of corrective actions. The prior LER supplement and original LER addressed events were initiated based on Incident Reports 92-819, 92-865 and 93-067. CONDITIONS PRIOR TO *OCCURRENCE:
| | LICENSEE CONTACT FOR THIS LER (12) |
| 12/13/92 -Mode 1 Reactor Power 100% -Unit Load 1151 MWe On 12/12/92, at 0914 hours, power was reduced to 90% due to Circulating Water System high delta T. At 1812 hours (that day), a power increase to full power commenced and was reached on 12/13/92 at 0650 hours. 12/30/92 -Mode 1 Reactor Power 90% -Unit Load 1010 MWe On 12/30/92, prior to the ESF event, power was being increased from 90% to full power. The Unit had previously been removed from service due to Circulating Water System problems.
| | NAME TELEPHONE NUMBER AREA CODE M. J. Pollack - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| 1/25/93 -Mode 1 Reactor Power 99% -Unit Load 1100 MWe On 1/25/93, prior to the ESF event, power was being increased from 88% to full power. The Unit had been removed from service for planned maintenance and experienced a manual reactor trip (LER 272/93-002-00) during shutdown on 1/16/93. Power ascension had begun on 1/23/93. DESCRIPTION OF OCCURRENCE:
| | MANUFAC* MANUFAC* |
| This LER addresses four (4) Engineered Safety Feature (ESF) actuations initiated through the Radiation Monitoring System (RMS) {IL}. The signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR)
| | CAUSE SYSTEM COMPONENT TUR ER TUR ER B W 11 I 210 y I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED |
| System {BF} isolation. | | ~NO SUBMISSION l YES (If yes, compl*le EXPECTED SUBMISSION DA TEI DATE 1151 I I ABSTRACT (Limit to 1400 spactJs, i.tJ., tJpproximtJtBly fiftatJn single*spact1 typ11writt1Jn /int1sl (16) |
| The associated isolation valves were closed prior to each event, and therefore, did not change
| | This supplemental LER addresses investigation results and identifies the ' |
| / LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DESCRIPTION OF OCCURRENCE:
| | current status of corrective actions associated with 4 Engineered Safety Feature (ESF) actuations initiated by the lRllA Radiation Monitoring system (RMS} channel. The lRllA RMS Channel monitors the Containment atmosphere for particulate activity. The ESF signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR) System isolation. At the time of the events, the associated valves were closed and did not change position. Two of the events occurred on 12/13/92, one on 12/30/92, and one on 1/25/93. Investigation determined that the lRllA RMS channel was responding to actual increases in containment airborne radioactivity; i.e., Rb-88 activity (half life of 17.8 minutes) which is a decay product of Kr-88, a fission product. Contributing leakage sources included: 1) lPSl Pressurizer Spray air operated valve bonnet leak; 2) pipe flange leakage, immediately upstream of the Reactor head vent manual isolation valve, 1RC900; 3) Pressurizer manway leakage past its gasket seal; and 4) Pressurizer Relief Tank rupture disk pinhole leakage. |
| DOCKET NUMBER 5000272 (cont'd) LER NUMBER 92-026-02 PAGE 3 of 5 position.
| | NRC Form 366 (6-89) |
| Per Code of Federal Regulations lOCFR 50.72(b) (2) (ii), the Nuclear Regulatory Commission (NRC) was notified of the four (4) events. On December 13, 1992, at 0535 hours, following a power increase from 99% to 100%, the lRllA RMS channel alarmed actuating a CP/P-VR System isolation.
| | |
| It was initially assessed to be the result of a channel instrumentation spike; however, further investigation showed it was due to increased Containment airborne activity.
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 2 of 5 PLANT AND SYSTEM IDENTIFICATION: |
| Fol-lowing the actuation, the alarm was cleared and the channel was left in service. At 0658 hours, that day, the lRllA RMS channel increased from 35,000 cpm to the alarm setpoint (60,000 Qpm) resulting in another CP/P-VR System isolation signal. After this alarm actuation the count level trended back to 35,000 cpm. The lRllA RMS channel monitors the Containment atmosphere for particulate activity by filtering a sample of Containment air. Investigation determined that the lRllA RMS channel was functioning in accordance with its design. Analysis of the sample filter paper showed that the alarm signal was due to Rb-88 activity.
| | Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx} |
| Rb-88 has a half life of 17. 8 minutes. It is a decay product o_f Kr-88 which is a fission product. Investigation to identify the source of the activity was initiated.
| | IDENTIFICATION OF OCCURRENCE: |
| On December 30, 1992, at 1452 hours, during power ascension from 90% to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm the channel count rate trended back to 35,000 cpm. The alarm was again shown to be due to Rb-88. On January 25, 1993, at 1300 hours, during power ascension from 88% to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm, the Containment Fan coil Units were put in low speed reducing containment airborne particulate activity.
| | Engineered Safety Feature actuations initiated from the Radiation Monitoring System Event Dates: 12/13/92, 12/30/92 and 1/25/93 Report Date: 10/7/93 This supplemental LER addresses investigation results and identifies the current status of corrective actions. The prior LER supplement and original LER addressed events were initiated based on Incident l |
| The channel count rate trended back to 25,000 cpm. The alarm was again shown to be due to APPARENT CAUSE OF OCCURRENCE:
| | Reports 92-819, 92-865 and 93-067. |
| | CONDITIONS PRIOR TO *OCCURRENCE: |
| | 12/13/92 - Mode 1 Reactor Power 100% - Unit Load 1151 MWe On 12/12/92, at 0914 hours, power was reduced to 90% due to Circulating Water System high delta T. At 1812 hours (that day), a power increase to full power commenced and was reached on 12/13/92 at 0650 hours. |
| | 12/30/92 - Mode 1 Reactor Power 90% - Unit Load 1010 MWe On 12/30/92, prior to the ESF event, power was being increased from 90% to full power. The Unit had previously been removed from service due to Circulating Water System problems. |
| | 1/25/93 - Mode 1 Reactor Power 99% - Unit Load 1100 MWe On 1/25/93, prior to the ESF event, power was being increased from 88% to full power. The Unit had been removed from service for planned maintenance and experienced a manual reactor trip (LER 272/93-002-00) during shutdown on 1/16/93. Power ascension had begun on 1/23/93. |
| | DESCRIPTION OF OCCURRENCE: |
| | This LER addresses four (4) Engineered Safety Feature (ESF) actuations initiated through the Radiation Monitoring System (RMS) |
| | {IL}. The signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR) System {BF} isolation. The associated isolation valves were closed prior to each event, and therefore, did not change |
| | |
| | / |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 3 of 5 DESCRIPTION OF OCCURRENCE: (cont'd) position. Per Code of Federal Regulations 10CFR 50.72(b) (2) (ii), the Nuclear Regulatory Commission (NRC) was notified of the four (4) events. |
| | On December 13, 1992, at 0535 hours, following a power increase from 99% to 100%, the lRllA RMS channel alarmed actuating a CP/P-VR System isolation. It was initially assessed to be the result of a channel instrumentation spike; however, further investigation showed it was due to increased Containment airborne activity. Fol-lowing the actuation, the alarm was cleared and the channel was left in service. At 0658 hours, that day, the lRllA RMS channel increased from 35,000 cpm to the alarm setpoint (60,000 Qpm) resulting in another CP/P-VR System isolation signal. After this alarm actuation the count level trended back to 35,000 cpm. |
| | The lRllA RMS channel monitors the Containment atmosphere for particulate activity by filtering a sample of Containment air. |
| | Investigation determined that the lRllA RMS channel was functioning in accordance with its design. Analysis of the sample filter paper showed that the alarm signal was due to Rb-88 activity. Rb-88 has a half life of 17. 8 minutes. It is a decay product o_f Kr-88 which is a fission product. Investigation to identify the source of the activity was initiated. |
| | On December 30, 1992, at 1452 hours, during power ascension from 90% |
| | to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm the channel count rate trended back to 35,000 cpm. The alarm was again shown to be due to Rb-88. |
| | On January 25, 1993, at 1300 hours, during power ascension from 88% |
| | to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm, the Containment Fan coil Units were put in low speed reducing containment airborne particulate activity. The channel count rate trended back to 25,000 cpm. The alarm was again shown to be due to Rb~88. |
| | APPARENT CAUSE OF OCCURRENCE: |
| The root cause of the ESF events is equipment failure. Small leaks from various components had led to increased Containment airborne activity. | | The root cause of the ESF events is equipment failure. Small leaks from various components had led to increased Containment airborne activity. |
| Investigation of the first three (3) ESF actuations indicated that a previously identified bonnet leak on the lPSl Pressurizer Spray air operated valve was the probable source of the increased activity. | | Investigation of the first three (3) ESF actuations indicated that a previously identified bonnet leak on the lPSl Pressurizer Spray air operated valve was the probable source of the increased activity. |
| The maintenance valves upstream and downstream of the lPSl valve had been closed isolating the lPSl valve. Also, the lPSl valve was leak repaired. | | The maintenance valves upstream and downstream of the lPSl valve had been closed isolating the lPSl valve. Also, the lPSl valve was leak repaired. Investigation of the fourth ESF actuation identified pipe |
| Investigation of the fourth ESF actuation identified pipe LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 APPARENT CAUSE OF OCCURRENCE: | | |
| DOCKET NUMBER 5000272 (cont'd) LER NUMBER 92-026-02 PAGE 4 of 5 flange leakage immediately upstream of the Reactor head vent manual isolation valve 1RC900 {AB}. The flange leak was stopped with a temporary modification (leak repair clamp). Investigation to identify additional source(s) of Containment gaseous activity has been completed.
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 4 of 5 APPARENT CAUSE OF OCCURRENCE: (cont'd) flange leakage immediately upstream of the Reactor head vent manual isolation valve 1RC900 {AB}. The flange leak was stopped with a temporary modification (leak repair clamp). |
| Those other sources identified include leakage past the Pressurizer manway*s gasket seal and several pinhole leaks on the Pressurizer Relief Tank (PRT) rupture disk. Temporary leak repair of the Pressurizer manway was completed. | | Investigation to identify additional source(s) of Containment gaseous activity has been completed. Those other sources identified include leakage past the Pressurizer manway*s gasket seal and several pinhole leaks on the Pressurizer Relief Tank (PRT) rupture disk. |
| This reduced the Containment Rb-88 activity to below the lRllA RMS channel warning setpoint. | | Temporary leak repair of the Pressurizer manway was completed. This reduced the Containment Rb-88 activity to below the lRllA RMS channel warning setpoint. Permanent repairs will include gasket and diaphragm replacement and repair of any identified damage during the Unit 1 eleventh refueling outage (which began on October 2, 1993). |
| Permanent repairs will include gasket and diaphragm replacement and repair of any identified damage during the Unit 1 eleventh refueling outage (which began on October 2, 1993). System Engineering completed a Deficiency Report (930217211) which included a safety evaluation. | | System Engineering completed a Deficiency Report (930217211) which included a safety evaluation. The evaluation concludes that the pinholes do not inhibit the rupture disk from performing its intended function. Based on this assessment, the PRT rupture disk will be replaced during the Unit 1 eleventh refueling outage. |
| The evaluation concludes that the pinholes do not inhibit the rupture disk from performing its intended function. | | ANALYSIS OF OCCURRENCE: |
| Based on this assessment, the PRT rupture disk will be replaced during the Unit 1 eleventh refueling outage. ANALYSIS OF OCCURRENCE: | | The lRllA Containment Particulate Monitor, (a NaI scintillation type detector, model LFE MD5B) monitors air particulate gamma radio-activity in the Containment atmosphere. In Modes 1 through 4, it is used to identify Reactor Coolant System (RCS) {AB} leakage in conjunction with the containment sump level monitoring system, and either the containment fan cooler condensate flow rate or the containment atmosphere gaseous (1R12A) radioactivity monitoring system. In Mode 6, it is used to provide indication of a fuel handling accident and early Containment isolation in the event of an accident. |
| The lRllA Containment Particulate Monitor, (a NaI scintillation type detector, model LFE MD5B) monitors air particulate gamma activity in the Containment atmosphere. | | At the time of these ESF actuations, the lRllA RMS channel provided an alarm signal which caused automatic isolation of the CP/P-VR System. Isolation of the CP/P-VR System is designed to mitigate the release of radioactive material to the environment after a design pasis accident. Since the occurrence of these ESF actuations, an engineering review was conducted to determine the necessity for the lRllA RMS channel to have this function. It was concluded that in Modes 1 - 5 the lRllA channel does not require this function. |
| In Modes 1 through 4, it is used to identify Reactor Coolant System (RCS) {AB} leakage in conjunction with the containment sump level monitoring system, and either the containment fan cooler condensate flow rate or the containment atmosphere gaseous (1R12A) radioactivity monitoring system. In Mode 6, it is used to provide indication of a fuel handling accident and early Containment isolation in the event of an accident. | | Therefore, the ESF function has been disabled during plant operation in Modes 1 - 5. This.eliminates unnecessary challenges of the CP/PV-R ESF System. |
| At the time of these ESF actuations, the lRllA RMS channel provided an alarm signal which caused automatic isolation of the CP/P-VR System. Isolation of the CP/P-VR System is designed to mitigate the release of radioactive material to the environment after a design pasis accident. | | A review of lRllA RMS channel data show the alarms were not the result of spurious channel spiking. Routine containment airborne radioactivity monitoring, by Radiation Protection, confirms the presence of sufficie.nt Rb-88 to cause the alarm. Unidentified leak |
| Since the occurrence of these ESF actuations, an engineering review was conducted to determine the necessity for the lRllA RMS channel to have this function. | | |
| It was concluded that in Modes 1 -5 the lRllA channel does not require this function. | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 5 of 5 ANALYSIS OF OCCURRENCE: (cont'd) rate calculations (conducted by Operations) show a leak rate of 0.2 gpm. The Technical Specification limitation on unidentified leakage is 1 gpm. |
| Therefore, the ESF function has been disabled during plant operation in Modes 1 -5. This.eliminates unnecessary challenges of the CP/PV-R ESF System. A review of lRllA RMS channel data show the alarms were not the result of spurious channel spiking. Routine containment airborne radioactivity monitoring, by Radiation Protection, confirms the presence of sufficie.nt Rb-88 to cause the alarm. Unidentified leak LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 ANALYSIS OF OCCURRENCE: (cont'd) LER NUMBER 92-026-02 PAGE 5 of 5 rate calculations (conducted by Operations) show a leak rate of 0.2 gpm. The Technical Specification limitation on unidentified leakage is 1 gpm. The lRllA RMS channel functioned per design. It has identified J' higher than normal airborne particulate activity in Containment. | | The lRllA RMS channel functioned per design. It has identified J' higher than normal airborne particulate activity in Containment. The channel ESF isolation capability was functional. Therefore, this event did not affect the health or safety of the public; however, due to the automatic actuation signal of an ESF system, it is reportable in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (iv). |
| The channel ESF isolation capability was functional. | | -CORRECTIVE ACTION: |
| Therefore, this event did not affect the health or safety of the public; however, due to the automatic actuation signal of an ESF system, it is reportable in accordance with Code of Federal Regulations lOCFR 50.73(a) (2) (iv). -CORRECTIVE ACTION: Maintenance testing of the lRllA RMS channel was completed. | | Maintenance testing of the lRllA RMS channel was completed. No channel failure mechanisms were identified. |
| No channel failure mechanisms were identified. | |
| The lPSl valve leak was stopped via closure of the maintenance valves upstream and downstream of the lPSl valve and insertion of temporary | | The lPSl valve leak was stopped via closure of the maintenance valves upstream and downstream of the lPSl valve and insertion of temporary |
| * sealant. The lPSl valve will be repaired during the Unit 1 eleventh refueling outage. The flange leak upstream of the 1RC900 valve was stopped through installation of a leak repair clamp in accordance with temporary modification procedures. | | * sealant. The lPSl valve will be repaired during the Unit 1 eleventh refueling outage. |
| Permanent repair will be completed during the Unit 1 eleventh refueling outage. Permanent repair of the Pressurizer manway gasket seal and replacement of the PRT rupture disk will be completed during the Unit 1 eleventh refueling outage. Salem Operations MJP:pc SORC Mtg. 93-089}} | | The flange leak upstream of the 1RC900 valve was stopped through installation of a leak repair clamp in accordance with temporary modification procedures. Permanent repair will be completed during the Unit 1 eleventh refueling outage. |
| | Permanent repair of the Pressurizer manway gasket seal and replacement of the PRT rupture disk will be completed during the Unit 1 eleventh refueling outage. |
| | Salem Operations MJP:pc SORC Mtg. 93-089}} |
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MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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e PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station October 7, 1993 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 SUPPLEMENTAL LICENSEE EVENT REPORT 92-026-02 This supplemental Licensee Event Report is being submitted pursuant to Code of Federal Regulations lOCF~ 50.73. The report has been modified based upon investigation results and identifies the current status of corrective actions.
Sincerely yours,
- c. A. Vondra General Manager -
Salem Operations MJPJ:pc Distribution 150057
~fiA 0 1~noa14 931007 s OCK 05000272
. PDR The power is in your hands. :rE. z..i.
95-2189 REV 7-92
\fl NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P*530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF M_ANAGEMENT AND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (1) DOCKET NUMBER (21 I PAGE 131 Salem Generating Station - Unit 1 o 1s101010121712 1!0F 015 TITLE (4)
ESF Actuations Initiated From The Radiation Monitoring System.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR :::::::::::SEQUENTIAL o::;:;:: REVISION DAY YEAR FACI L/TY NAMES DOCKET NUMBER(S)
- '.*'.*:*:*:* NUMBER .;:;:;:::: NUMBER MONTH i I2 i I 3 9 2 9 I 2 - o l 2 l6 - oI2 i l o o 17 I 9 3 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE R~QUIREMENTS OF 10 CFR §: (Check one or more of lh* following) (11)
MODE (9) 1 x I ,_
20.402(b) 20,405(c) 50.73(1)(2)(iv) 73.71(b)
POWER LEVEL (10) l I O I O 1--
20.406(1)(1 )(i) 20.405(1)(1 )(ji) 50.36(c)(1) 50.36(c)(2) 50.73(1)(2)(v) 50.73(1J(2)(viil 73.71(c)
OTHER (Specify in Absrrocl btJ/ow tJnd in Tt1xt, NRC Form lllilll=
20.405(1)(1 )(iii) 50.73(1)(2J(i) 50.73(1)(2)(viiil(A) 366A) 20.405(1)(1)(lv) 50,73(1Jl2llii) 50.73(1) (2) (viii) (B) 20.406(1)(1 )(v) 50.73(1)(2)(111) 50.73(1)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE M. J. Pollack - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
MANUFAC* MANUFAC*
CAUSE SYSTEM COMPONENT TUR ER TUR ER B W 11 I 210 y I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED
~NO SUBMISSION l YES (If yes, compl*le EXPECTED SUBMISSION DA TEI DATE 1151 I I ABSTRACT (Limit to 1400 spactJs, i.tJ., tJpproximtJtBly fiftatJn single*spact1 typ11writt1Jn /int1sl (16)
This supplemental LER addresses investigation results and identifies the '
current status of corrective actions associated with 4 Engineered Safety Feature (ESF) actuations initiated by the lRllA Radiation Monitoring system (RMS} channel. The lRllA RMS Channel monitors the Containment atmosphere for particulate activity. The ESF signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR) System isolation. At the time of the events, the associated valves were closed and did not change position. Two of the events occurred on 12/13/92, one on 12/30/92, and one on 1/25/93. Investigation determined that the lRllA RMS channel was responding to actual increases in containment airborne radioactivity; i.e., Rb-88 activity (half life of 17.8 minutes) which is a decay product of Kr-88, a fission product. Contributing leakage sources included: 1) lPSl Pressurizer Spray air operated valve bonnet leak; 2) pipe flange leakage, immediately upstream of the Reactor head vent manual isolation valve, 1RC900; 3) Pressurizer manway leakage past its gasket seal; and 4) Pressurizer Relief Tank rupture disk pinhole leakage.
NRC Form 366 (6-89)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 2 of 5 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
Engineered Safety Feature actuations initiated from the Radiation Monitoring System Event Dates: 12/13/92, 12/30/92 and 1/25/93 Report Date: 10/7/93 This supplemental LER addresses investigation results and identifies the current status of corrective actions. The prior LER supplement and original LER addressed events were initiated based on Incident l
Reports92-819, 92-865 and 93-067.
CONDITIONS PRIOR TO *OCCURRENCE:
12/13/92 - Mode 1 Reactor Power 100% - Unit Load 1151 MWe On 12/12/92, at 0914 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.47777e-4 months <br />, power was reduced to 90% due to Circulating Water System high delta T. At 1812 hours0.021 days <br />0.503 hours <br />0.003 weeks <br />6.89466e-4 months <br /> (that day), a power increase to full power commenced and was reached on 12/13/92 at 0650 hours0.00752 days <br />0.181 hours <br />0.00107 weeks <br />2.47325e-4 months <br />.
12/30/92 - Mode 1 Reactor Power 90% - Unit Load 1010 MWe On 12/30/92, prior to the ESF event, power was being increased from 90% to full power. The Unit had previously been removed from service due to Circulating Water System problems.
1/25/93 - Mode 1 Reactor Power 99% - Unit Load 1100 MWe On 1/25/93, prior to the ESF event, power was being increased from 88% to full power. The Unit had been removed from service for planned maintenance and experienced a manual reactor trip (LER 272/93-002-00) during shutdown on 1/16/93. Power ascension had begun on 1/23/93.
DESCRIPTION OF OCCURRENCE:
This LER addresses four (4) Engineered Safety Feature (ESF) actuations initiated through the Radiation Monitoring System (RMS)
{IL}. The signals were for Containment Purge/Pressure-Vacuum Relief (CP/P-VR) System {BF} isolation. The associated isolation valves were closed prior to each event, and therefore, did not change
/
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 3 of 5 DESCRIPTION OF OCCURRENCE: (cont'd) position. Per Code of Federal Regulations 10CFR 50.72(b) (2) (ii), the Nuclear Regulatory Commission (NRC) was notified of the four (4) events.
On December 13, 1992, at 0535 hours0.00619 days <br />0.149 hours <br />8.845899e-4 weeks <br />2.035675e-4 months <br />, following a power increase from 99% to 100%, the lRllA RMS channel alarmed actuating a CP/P-VR System isolation. It was initially assessed to be the result of a channel instrumentation spike; however, further investigation showed it was due to increased Containment airborne activity. Fol-lowing the actuation, the alarm was cleared and the channel was left in service. At 0658 hours0.00762 days <br />0.183 hours <br />0.00109 weeks <br />2.50369e-4 months <br />, that day, the lRllA RMS channel increased from 35,000 cpm to the alarm setpoint (60,000 Qpm) resulting in another CP/P-VR System isolation signal. After this alarm actuation the count level trended back to 35,000 cpm.
The lRllA RMS channel monitors the Containment atmosphere for particulate activity by filtering a sample of Containment air.
Investigation determined that the lRllA RMS channel was functioning in accordance with its design. Analysis of the sample filter paper showed that the alarm signal was due to Rb-88 activity. Rb-88 has a half life of 17. 8 minutes. It is a decay product o_f Kr-88 which is a fission product. Investigation to identify the source of the activity was initiated.
On December 30, 1992, at 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br />, during power ascension from 90%
to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm the channel count rate trended back to 35,000 cpm. The alarm was again shown to be due to Rb-88.
On January 25, 1993, at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, during power ascension from 88%
to full power, the lRllA RMS channel indication increased from 35,000 cpm to the alarm setpoint resulting in a CP/P-VR System isolation signal. Following the alarm, the Containment Fan coil Units were put in low speed reducing containment airborne particulate activity. The channel count rate trended back to 25,000 cpm. The alarm was again shown to be due to Rb~88.
APPARENT CAUSE OF OCCURRENCE:
The root cause of the ESF events is equipment failure. Small leaks from various components had led to increased Containment airborne activity.
Investigation of the first three (3) ESF actuations indicated that a previously identified bonnet leak on the lPSl Pressurizer Spray air operated valve was the probable source of the increased activity.
The maintenance valves upstream and downstream of the lPSl valve had been closed isolating the lPSl valve. Also, the lPSl valve was leak repaired. Investigation of the fourth ESF actuation identified pipe
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 4 of 5 APPARENT CAUSE OF OCCURRENCE: (cont'd) flange leakage immediately upstream of the Reactor head vent manual isolation valve 1RC900 {AB}. The flange leak was stopped with a temporary modification (leak repair clamp).
Investigation to identify additional source(s) of Containment gaseous activity has been completed. Those other sources identified include leakage past the Pressurizer manway*s gasket seal and several pinhole leaks on the Pressurizer Relief Tank (PRT) rupture disk.
Temporary leak repair of the Pressurizer manway was completed. This reduced the Containment Rb-88 activity to below the lRllA RMS channel warning setpoint. Permanent repairs will include gasket and diaphragm replacement and repair of any identified damage during the Unit 1 eleventh refueling outage (which began on October 2, 1993).
System Engineering completed a Deficiency Report (930217211) which included a safety evaluation. The evaluation concludes that the pinholes do not inhibit the rupture disk from performing its intended function. Based on this assessment, the PRT rupture disk will be replaced during the Unit 1 eleventh refueling outage.
ANALYSIS OF OCCURRENCE:
The lRllA Containment Particulate Monitor, (a NaI scintillation type detector, model LFE MD5B) monitors air particulate gamma radio-activity in the Containment atmosphere. In Modes 1 through 4, it is used to identify Reactor Coolant System (RCS) {AB} leakage in conjunction with the containment sump level monitoring system, and either the containment fan cooler condensate flow rate or the containment atmosphere gaseous (1R12A) radioactivity monitoring system. In Mode 6, it is used to provide indication of a fuel handling accident and early Containment isolation in the event of an accident.
At the time of these ESF actuations, the lRllA RMS channel provided an alarm signal which caused automatic isolation of the CP/P-VR System. Isolation of the CP/P-VR System is designed to mitigate the release of radioactive material to the environment after a design pasis accident. Since the occurrence of these ESF actuations, an engineering review was conducted to determine the necessity for the lRllA RMS channel to have this function. It was concluded that in Modes 1 - 5 the lRllA channel does not require this function.
Therefore, the ESF function has been disabled during plant operation in Modes 1 - 5. This.eliminates unnecessary challenges of the CP/PV-R ESF System.
A review of lRllA RMS channel data show the alarms were not the result of spurious channel spiking. Routine containment airborne radioactivity monitoring, by Radiation Protection, confirms the presence of sufficie.nt Rb-88 to cause the alarm. Unidentified leak
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-026-02 5 of 5 ANALYSIS OF OCCURRENCE: (cont'd) rate calculations (conducted by Operations) show a leak rate of 0.2 gpm. The Technical Specification limitation on unidentified leakage is 1 gpm.
The lRllA RMS channel functioned per design. It has identified J' higher than normal airborne particulate activity in Containment. The channel ESF isolation capability was functional. Therefore, this event did not affect the health or safety of the public; however, due to the automatic actuation signal of an ESF system, it is reportable in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (iv).
-CORRECTIVE ACTION:
Maintenance testing of the lRllA RMS channel was completed. No channel failure mechanisms were identified.
The lPSl valve leak was stopped via closure of the maintenance valves upstream and downstream of the lPSl valve and insertion of temporary
- sealant. The lPSl valve will be repaired during the Unit 1 eleventh refueling outage.
The flange leak upstream of the 1RC900 valve was stopped through installation of a leak repair clamp in accordance with temporary modification procedures. Permanent repair will be completed during the Unit 1 eleventh refueling outage.
Permanent repair of the Pressurizer manway gasket seal and replacement of the PRT rupture disk will be completed during the Unit 1 eleventh refueling outage.
Salem Operations MJP:pc SORC Mtg.93-089