ML18101B097: Difference between revisions
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| issue date = 11/13/1995 | | issue date = 11/13/1995 | ||
| title = Forwards LER 95-025-00 Re Reportability Criteria,As Defined in 10CFR50.72(b)(2).Attachment a Represents Commitments Made to NRC Re LER 95-025-00 | | title = Forwards LER 95-025-00 Re Reportability Criteria,As Defined in 10CFR50.72(b)(2).Attachment a Represents Commitments Made to NRC Re LER 95-025-00 | ||
| author name = | | author name = Warren C | ||
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | ||
| addressee name = | | addressee name = | ||
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=Text= | =Text= | ||
{{#Wiki_filter:. . | {{#Wiki_filter:.. | ||
* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit NOV 1 3 1995 LR-N95199 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Att: Document Control Desk SALEM GENERATING STATION LICENSE NO: DPR-70 and.DPR-75 DOCKET NO: 50-272 and 50-311 UNIT NOS: 1 and 2 LICENSEE EVENT REPORT NO. 95-025-00 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50. 73 (a) (2) (ii). SORC Mtg. No: 95-131 EHV/tcp C Distribution LER file 3.7 The r!,*hrer m h:=c1,i*. | PS~G | ||
* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit NOV 1 3 1995 LR-N95199 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Att: Document Control Desk SALEM GENERATING STATION LICENSE NO: DPR-70 and.DPR-75 DOCKET NO: 50-272 and 50-311 UNIT NOS: 1 and 2 LICENSEE EVENT REPORT NO. 95-025-00 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50. 73 (a) (2) (ii). | |||
Sincerely, | |||
* f /L, (! cJuw~ | |||
~1-(?' C. Warren General Manager - | |||
Salem Operations SORC Mtg. No: 95-131 EHV/tcp C Distribution LER file 3.7 | |||
* Attachment A The following items represent commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (95-025-00) . The commitments are as follows: 1. Pump NPSH margin is currently protected by the river level/NPSH monitoring instructions contained in the Abnormal Environmental Procedure (SC.OP-AB.ZZ-OOOl(Q)). | /.{j*'l;} i The r!,*hrer i~ m \*~Ju:- h:=c1,i*. ./\Jr:10' l 9511160219 951113 v 95*2168 REV. 6/94 PDR ADOCK 05000272 s PDR | ||
These instructions will be removed when the pump upgrades are completed, which is scheduled to be completed in 1996. There are presently 2 new design (Johnston) | * Attachment A The following items represent commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (95-025-00) . The commitments are as follows: | ||
SW pumps installed | : 1. Pump NPSH margin is currently protected by the river level/NPSH monitoring instructions contained in the Abnormal Environmental Procedure (SC.OP-AB.ZZ-OOOl(Q)). These instructions will be removed when the pump upgrades are completed, which is scheduled to be completed in 1996. | ||
(#12 and 26) . 2. Permanent procedure revisions are being developed (both Normal and Emergency Operating) to address the specific concerns of the Problem Reports. These revisions will be implemented by April 1996. 3. A copy of this LER will be forwarded to the Nuclear Training Center for evaluation and incorporation into the Operability/Reportability training for Design Engineering personnel. | There are presently 2 new design (Johnston) SW pumps installed (#12 and 26) . | ||
: 4. The SW System Configuration Baseline Document (CBD) will be revised to clearly identify the design basis and significance for normal operation in the cross-tied mode. This revision will be completed by May 31, 1996.}} | : 2. Permanent procedure revisions are being developed (both Normal and Emergency Operating) to address the specific concerns of the Problem Reports. These revisions will be implemented by April 1996. | ||
: 3. A copy of this LER will be forwarded to the Nuclear Training Center for evaluation and incorporation into the Operability/Reportability training for Design Engineering personnel. | |||
: 4. The SW System Configuration Baseline Document (CBD) will be revised to clearly identify the design basis and significance for normal operation in the cross-tied mode. | |||
This revision will be completed by May 31, 1996.}} |
Latest revision as of 10:07, 21 October 2019
ML18101B097 | |
Person / Time | |
---|---|
Site: | Salem |
Issue date: | 11/13/1995 |
From: | Warren C Public Service Enterprise Group |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
Shared Package | |
ML18101B098 | List: |
References | |
LR-N95199, NUDOCS 9511160219 | |
Download: ML18101B097 (2) | |
Text
..
PS~G
- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit NOV 1 3 1995 LR-N95199 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Att: Document Control Desk SALEM GENERATING STATION LICENSE NO: DPR-70 and.DPR-75 DOCKET NO: 50-272 and 50-311 UNIT NOS: 1 and 2 LICENSEE EVENT REPORT NO. 95-025-00 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50. 73 (a) (2) (ii).
Sincerely,
- f /L, (! cJuw~
~1-(?' C. Warren General Manager -
Salem Operations SORC Mtg. No: 95-131 EHV/tcp C Distribution LER file 3.7
/.{j*'l;} i The r!,*hrer i~ m \*~Ju:- h:=c1,i*. ./\Jr:10' l 9511160219 951113 v 95*2168 REV. 6/94 PDR ADOCK 05000272 s PDR
- Attachment A The following items represent commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (95-025-00) . The commitments are as follows:
- 1. Pump NPSH margin is currently protected by the river level/NPSH monitoring instructions contained in the Abnormal Environmental Procedure (SC.OP-AB.ZZ-OOOl(Q)). These instructions will be removed when the pump upgrades are completed, which is scheduled to be completed in 1996.
There are presently 2 new design (Johnston) SW pumps installed (#12 and 26) .
- 2. Permanent procedure revisions are being developed (both Normal and Emergency Operating) to address the specific concerns of the Problem Reports. These revisions will be implemented by April 1996.
- 3. A copy of this LER will be forwarded to the Nuclear Training Center for evaluation and incorporation into the Operability/Reportability training for Design Engineering personnel.
- 4. The SW System Configuration Baseline Document (CBD) will be revised to clearly identify the design basis and significance for normal operation in the cross-tied mode.
This revision will be completed by May 31, 1996.