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| | issue date = 03/05/1993 | | | issue date = 03/05/1993 |
| | title = LER 93-004-00:on 930206,both Main Turbine first-stage Impulse Pressure Indication Channels Indicated False Readings.Caused by Inadequate Sensing Line Protection. Failed Heat Tracing Will Be repaired.W/930305 Ltr | | | title = LER 93-004-00:on 930206,both Main Turbine first-stage Impulse Pressure Indication Channels Indicated False Readings.Caused by Inadequate Sensing Line Protection. Failed Heat Tracing Will Be repaired.W/930305 Ltr |
| | author name = PASTVA M J, VONDRA C A | | | author name = Pastva M, Vondra C |
| | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY |
| | addressee name = | | | addressee name = |
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| =Text= | | =Text= |
| {{#Wiki_filter:e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U.S. Nuclear*Regulatory Commission Document Control Desk Washington, DC 20555 | | {{#Wiki_filter:e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station March 5, 1993 U.S. Nuclear*Regulatory Commission Document Control Desk Washington, DC 20555 |
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| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-004-00 March 5, 1993 This Licensee Event requirements of the 50. 73 (a) (2) (i) (B). thirty (30) days of Report is being submitted pursuant to the Code of Federal Regulations lOCFR MJP:pc Distribution This report is required to be issued within event discovery.
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| 110032 Sincerely
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| : yours, A. Vondra General Manager -Salem Operations The Energy People 9303110188 930305 PDR ADOCK 05000311 ;}eJ} I I 95-2189 ( 1 OM) 12-89 S PDR t NRC FORM 366 (6-89) -U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 LICENSEE EVENT REPORT (LER) FACILITY NAME 111 Salem Generating Station -Unit 2 TITLE 14) EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104).
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| OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. 'DOCKET NUMBER 121 PAGE 13) 0 I 5 I 0 I 0 I 0 13 I 11 l 1 I OF 0 ,s Tech Spec 3.0.3 Entry: Inoperability of Both Turbine First Stage Pressure Channels.
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| EVENT DATE 151 LEA NUMBER 161 REPORT DATE 171 OTHER FACILITIES INVOLVED 18) MONTH DAY YEAR YEAR
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| {)
| |
| MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI d 2 o I E 9 3 91 3 -ol o 14 -o I o o I 3 ol s 9 I 3 OPERATING
| |
| --..---------J MODE (9) 1 I 20.402lbl
| |
| _ 20.405lcl 50.73(111211ivl 73.71(bl 73.711cl ,_ 50.38lcll11 50.7311112llvl
| |
| -'--'--POWER I 20.4051111111il
| |
| -..,L ....
| |
| E..,, ....
| |
| 10-'---20.405(1111 l(iil.
| |
| '--50.38lcll2l x 60.7311ll2llil 50.7311l12llviil
| |
| ....._ 50.7311112llviiillAI
| |
| ....__ OTHER (Specify in Abstroct below and in Text. NRC Form 366Ai ,_ ..__ 60.73(1l12lliil 50.7311l12llviiillBI
| |
| '--....._ 50.7311l12Hiiil 50.731111211*1 LICENSEE CONTACT FOR THIS LER 112) NAME AREA CODE M. J. Pastva, Jr. -LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 CAUSE SYSTEM COMPONENT I I I I I I I I TURER I I I I I I SYSTEM I I COMPONENT MANUFAC* TUR ER I I I I I I I I I I I I TELEPHONE NUMBER SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION DATE (151 n YES (If Y*S. compl*to EXPECTED SUBMISSION DA TEI I hzi NO I ABSTRACT (Limit to 1400 spaces, i.e .* approximately fifteen single-space typewrittsn Jines) (16) At 2105 hours, on 2/6/93, Tech. Spec. 3.0.3 was entered due to operation outside Tech. Spec. Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings.
| |
| PT-505 and PT-506 provide turbine power input for plant control during power operation.
| |
| PT-505 was indicating downscale and PT-506 was indicating upscale. This was first observed via automatic rod insertion.
| |
| Rod motion was stopped by placing rod control in manual. The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased ambient air temperature around the sensing line. Satisfactory channel functional checks showed the instruments operable and at 2109 hours (same day), Tech. Spec. 3.0.3 was exited. The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate.
| |
| When this event occurred, the outside ambient temperature was less than 20°F. Missing insulation from.the channels' transmitter sensing lines (which will be replaced) and the PT-506 heat trace had failed (which will be repaired) was identified.
| |
| An Operations Department Night Order Book entry has been made to preclude chilling the PT-505 and PT-506 transmitter sensing lines. The administrative program for preparing Salem Station for Winter operation will be reviewed.
| |
| Revisions will be incorporated as appropriate.
| |
| NRC Form 366 16-89) I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
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| Westinghouse
| |
| -Pressurized Water Reactor LER NUMBER 93-004-00 PAGE 2 of 5 Energy Industry Identification system (EIIS) codes are identified in the text as {XX} IDENTIFICATION OF OCCURRENCE:
| |
| Technical Specification
| |
|
| |
|
| ====3.0.3 Entry====
| | SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-004-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR |
| Inoperability of Both Turbine First Stage Pressure Channels Event Date: 2/6/93 Report Date: 3/5/93 This report was initiated by Incident Report No. 93-112. CONDITIONS PRIOR TO OCCURRENCE: | | : 50. 73 (a) (2) (i) (B). This report is required to be issued within thirty (30) days of event discovery. |
| Mode 1 Reactor Power 100% -Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE: | | Sincerely yours, o;.~ A. Vondra General Manager - |
| At 2105 hours, on February 6, 1993 Technical Specification 3.0.3 was entered due to operation outside Technical Specification Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings. | | Salem Operations MJP:pc Distribution 110032 The Energy People |
| PT-505 was indicating downscale and PT-506 was indicating upscale. PT-505 and PT-506 provide turbine power input for plant control during power operation. | | ;}eJ} I I 9303110188 930305 95-2189 ( 1OM) 12-89 PDR ADOCK 05000311 S PDR |
| | |
| | t NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) - APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. |
| | FACILITY NAME 111 DOCKET NUMBER 121 PAGE 13) |
| | Salem Generating Station - Unit 2 TITLE 14) 0 I 5 I 0 I 0 I 0 13 I 11 l I 1 OF 0 ,s Tech Spec 3.0.3 Entry: Inoperability of Both Turbine First Stage Pressure Channels. |
| | EVENT DATE 151 LEA NUMBER 161 REPORT DATE 171 OTHER FACILITIES INVOLVED 18) |
| | MONTH DAY YEAR YEAR J~t SE~~~~~~AL {) ~~~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI d 2 oI E 9 3 91 3 - ol o14 - oI o oI3 ol s 9 I 3 OPERATING l-T_H,IS-::R::E-::PO::R::-T:--ls_s_u_eM_l_T_TE_D_P_u_Rs_u,A_NT_TTO:.._T:.._H:..:.E_R:..:.~Q=-U:..:.l:..:.:RE=M:..:.E:..:.NTS:.:....::0:..:.F...:.10:....C::F...:.:R,..:§~:~(C::.::hB=Ck:...:o:::n:....*o::.r.::m=o':.::.*.:of~t::h*~fo::ll.::ow::in~gi:...:1~11~1--..---------J 1 |
| | I MODE (9) I |
| | --------L.~---J 20.402lbl _ 20.405lcl ,_ 50.73(111211ivl |
| | ~ |
| | 73.71(bl 50.38lcll11 50.7311112llvl 73.711cl POWER |
| | ~1v~o L~....1~1_0_1..__ |
| | -..,L.... E..,, 10-'--- |
| | 20.4051111111il 20.405(1111 l(iil. |
| | - 50.38lcll2l |
| | ....._ 50.7311l12llviil |
| | ....__ OTHER (Specify in Abstroct |
| | '-- below and in Text. NRC Form x |
| | 111"4[41~ ~-=::~:::;: |
| | 60.7311ll2llil 50.7311112llviiillAI 366Ai 60.73(1l12lliil |
| | ....._ 50.7311l12llviiillBI 50.7311l12Hiiil 50.731111211*1 LICENSEE CONTACT FOR THIS LER 112) |
| | NAME TELEPHONE NUMBER AREA CODE M. J. Pastva, Jr. - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC- MANUFAC* |
| | CAUSE SYSTEM COMPONENT SYSTEM COMPONENT TURER TUR ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED n YES (If Y*S. compl*to EXPECTED SUBMISSION DA TEI ABSTRACT (Limit to 1400 spaces, i.e.* approximately fifteen single-space typewrittsn Jines) (16) hzi NO SUBMISSION DATE (151 I I I At 2105 hours, on 2/6/93, Tech. Spec. 3.0.3 was entered due to operation outside Tech. Spec. Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings. PT-505 and PT-506 provide turbine power input for plant control during power operation. PT-505 was indicating downscale and PT-506 was indicating upscale. This was first observed via automatic rod insertion. Rod motion was stopped by placing rod control in manual. The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased ambient air temperature around the sensing line. Satisfactory channel functional checks showed the instruments operable and at 2109 hours (same day), Tech. Spec. 3.0.3 was exited. The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate. When this event occurred, the outside ambient temperature was less than 20°F. Missing insulation from.the channels' transmitter sensing lines (which will be replaced) and the PT-506 heat trace had failed (which will be repaired) was identified. An Operations Department Night Order Book entry has been made to preclude chilling the PT-505 and PT-506 transmitter sensing lines. The administrative program for preparing Salem Station for Winter operation will be reviewed. Revisions will be incorporated as appropriate. |
| | NRC Form 366 16-89) |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 2 of 5 PLANT AND SYSTEM IDENTIFICATION: |
| | Westinghouse - Pressurized Water Reactor Energy Industry Identification system (EIIS) codes are identified in the text as {XX} |
| | IDENTIFICATION OF OCCURRENCE: |
| | Technical Specification 3.0.3 Entry: Inoperability of Both Turbine First Stage Pressure Channels Event Date: 2/6/93 Report Date: 3/5/93 This report was initiated by Incident Report No. 93-112. |
| | CONDITIONS PRIOR TO OCCURRENCE: |
| | Mode 1 Reactor Power 100% - Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE: |
| | At 2105 hours, on February 6, 1993 Technical Specification 3.0.3 was entered due to operation outside Technical Specification Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings. PT-505 was indicating downscale and PT-506 was indicating upscale. PT-505 and PT-506 provide turbine power input for plant control during power operation. |
| This was first observed, at 2105 hours, via automatic rod insertion. | | This was first observed, at 2105 hours, via automatic rod insertion. |
| Abnormal Operating Procedure, S2.0P-AB.ROD-0003(Q), "Continuous Rod Motion" was entered. Rod motion was stopped after placing rod control in the manual mode of operation and the affected control rods were withdrawn to prior position. | | Abnormal Operating Procedure, S2.0P-AB.ROD-0003(Q), "Continuous Rod Motion" was entered. Rod motion was stopped after placing rod control in the manual mode of operation and the affected control rods were withdrawn to prior position. |
| The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased sensing line ambient air temperature. | | The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased sensing line ambient air temperature. Satisfactory functional checks showed the channels operable and at 2109 hours (same day), Technical Specification 3.0.3 was exited. |
| Satisfactory functional checks showed the channels operable and at 2109 hours (same day), Technical Specification 3.0.3 was exited. In MODES 1, 2, and 3, Technical Specification Table 3.3-3 requires a minimum of one (1) OPERABLE main steam flow indicator. | | In MODES 1, 2, and 3, Technical Specification Table 3.3-3 requires a minimum of one (1) OPERABLE main steam flow indicator. Technical Specification Table 3.3-3 Action 14 states: |
| Technical Specification Table 3.3-3 Action 14 states: | | |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 DESCRIPTION OF OCCURRENCE: (cont'd) LER NUMBER 93-004-00 PAGE 3 of 5 "With the number of OPERABLE Channels one less than the Total Number of Channels, operation may proceed until performance of the next required CHANNEL FUNCTIONAL TEST, provided the inoperable channel is placed in the tripped condition within 1 hour." Technical Specification | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 3 of 5 DESCRIPTION OF OCCURRENCE: (cont'd) |
| | "With the number of OPERABLE Channels one less than the Total Number of Channels, operation may proceed until performance of the next required CHANNEL FUNCTIONAL TEST, provided the inoperable channel is placed in the tripped condition within 1 hour." |
| | Technical Specification 3.0.3 states: |
| | "When a Limiting Condition for Operation is not met except as provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which the specification does not apply by placing it, as applicable, in: |
| | : 1. At least HOT STANDBY within the next 6 hours, |
| | : 2. At least HOT SHUTDOWN within the following 6 hours, and |
| | : 3. At least COLD SHUTDOWN within the subsequent 24 hours. |
| | Where corrective measures are completed that permit operation under the ACTION requirements, the ACTION may be taken in accordance with the specified time limits as measured from the time of failure to meet the Limiting Condition of Operation. |
| | Exceptions to these requirements are stated in the individual specifications." |
| | APPARENT CAUSE OF OCCURRENCE: |
| | The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate. When this event occurred, the outside ambient temperature was less than 20°F. Investigation identified the following concerns: |
| | PT-505 sensing line - Missing insulation from the entire length of the transmitter sensing line tray. Continuity checks showed the sensing line heat trace was functioning properly. |
| | PT-506 Sensing Line - Burnt open primary and secondary heat trace wiring and controllers with a missing section of transmitter sensing line tray insulation. |
| | It could not be determined how long the insulation has not been in place for either transmitter sensing line. |
| | ANALYSIS OF OCCURRENCE: |
| | Due to the entry into Technical Specification 3.0.3 this event is reportable to the Nuclear Regulatory Commission per Code of Federal Regulations 10CFR 50.73(a) (2) (i) (B). |
| | This event did not affect the health and safety of the public. The PT-505 and PT-506 channels were inoperable for less than five (5) |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 4 of 5 ANALYSIS OF OCCURRENCE: (cont'd) minutes during which time their functions were not challenged. Also, the automatic trip functions and engineered safety features were available. |
| | PT-505 and PT-506 are first-stage turbine pressure sensors which provide inputs for reactor control during power operation. PT-505 provides: input into the Steam Dump System for indication of Reactor Coolant System {AB} reference temperature; input into the Rod Control System {AA} for T v reference values; input into the main steamline flow se~p2int; provides the level setpoint for Steam Generator level control; provides reference main turbine power signal to the turbine electrohydraulic control system; provides input into permissive interlock P-13 which is used for development of the P-7 permissive (the permissive for blocking certain reactor trip functions above 10% power); provides input to P-2 (a permissive to place control rods in automatic operation, above 15% power, for control rod withdrawal); and input into AMSAC (Anticipated Transient Without Scram Mitigation System Actuation Circuitry) |
| | * PT-506 provides input to arm the Steam Dump System in the event of load reject, provides input into the high main steamline flow setpoint, and input into AMSAC. |
| | With PT-505 failing downscale and PT-506 failing upscale, if there was a required automatic actuation of the Steam Dump System due to a valid load rejection signal, the steam dump valves would not automatically open. The MS10 atmospheric relief valves would open at their setpoint of approximately 1037 psi to mitigate the pressure transient. Manual operation of the Steam Dump System valves would remain available. During inoperability of the PT-505 and PT-506 transmitters, automatic reactor trip functions on OTDT remained available and would have functioned in the event that a postulated load rejection went unabated. |
| | As identified in the Description of Occurrence section, with PT-505 failing downscale, automatic control rod insertion began, per design. Rod motion was stopped by placing rod control in the manual mode of operation. Operations personnel had reacted quickly to the event thereby limiting rod movement. There was no observed power reduction. |
| | CORRECTIVE ACTION: |
| | Following this event, an Operations Department Night Order Book entry was made to ensure the Turbine Building ventilation system is aligned to preclude chilling the PT-505 and PT-506 instrument sensing lines. |
| | The failed heat tracing will be repaired, and the missing sensing line insulation will be replaced. |
|
| |
|
| ====3.0.3 states====
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 5 of 5 CORRECTIVE ACTION: (cont'd) |
| "When a Limiting Condition for Operation is not met except as provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which the specification does not apply by placing it, as applicable, in: 1. At least HOT STANDBY within the next 6 hours, 2. At least HOT SHUTDOWN within the following 6 hours, and 3. At least COLD SHUTDOWN within the subsequent 24 hours. Where corrective measures are completed that permit operation under the ACTION requirements, the ACTION may be taken in accordance with the specified time limits as measured from the time of failure to meet the Limiting Condition of Operation.
| | The admin'istrative program for preparing Salem station for Winter operation will be reviewed. Revisions will be incorporated as appropriate. |
| Exceptions to these requirements are stated in the individual specifications." APPARENT CAUSE OF OCCURRENCE:
| | System Engineering is continuing to assess why the PT-505 and PT-506 channels failed in opposite directions. Also, the Salem Unit 1 heat trace configuration will be evaluated. |
| The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate.
| | Y8&4r |
| When this event occurred, the outside ambient temperature was less than 20°F. Investigation identified the following concerns:
| | ~G(g.eneral Manager - |
| PT-505 sensing line -Missing insulation from the entire length of the transmitter sensing line tray. Continuity checks showed the sensing line heat trace was functioning properly.
| | {,/ Salem Operations MJP:pc SORC Mtg. 93-021}} |
| PT-506 Sensing Line -Burnt open primary and secondary heat trace wiring and controllers with a missing section of transmitter sensing line tray insulation.
| |
| It could not be determined how long the insulation has not been in place for either transmitter sensing line. ANALYSIS OF OCCURRENCE:
| |
| Due to the entry into Technical Specification 3.0.3 this event is reportable to the Nuclear Regulatory Commission per Code of Federal Regulations lOCFR 50.73(a) (2) (i) (B). This event did not affect the health and safety of the public. The PT-505 and PT-506 channels were inoperable for less than five (5)
| |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 ANALYSIS OF OCCURRENCE: | |
| DOCKET NUMBER 5000311 (cont'd) LER NUMBER 93-004-00 PAGE 4 of 5 minutes during which time their functions were not challenged. | |
| Also, the automatic trip functions and engineered safety features were available.
| |
| PT-505 and PT-506 are first-stage turbine pressure sensors which provide inputs for reactor control during power operation.
| |
| PT-505 provides:
| |
| input into the Steam Dump System for indication of Reactor Coolant System {AB} reference temperature; input into the Rod Control System {AA} for T v reference values; input into the main steamline flow provides the level setpoint for Steam Generator level control; provides reference main turbine power signal to the turbine electrohydraulic control system; provides input into permissive interlock P-13 which is used for development of the P-7 permissive (the permissive for blocking certain reactor trip functions above 10% power); provides input to P-2 (a permissive to place control rods in automatic operation, above 15% power, for control rod withdrawal);
| |
| and input into AMSAC (Anticipated Transient Without Scram Mitigation System Actuation Circuitry)
| |
| * PT-506 provides input to arm the Steam Dump System in the event of load reject, provides input into the high main steamline flow setpoint, and input into AMSAC. With PT-505 failing downscale and PT-506 failing upscale, if there was a required automatic actuation of the Steam Dump System due to a valid load rejection signal, the steam dump valves would not automatically open. The MS10 atmospheric relief valves would open at their setpoint of approximately 1037 psi to mitigate the pressure transient.
| |
| Manual operation of the Steam Dump System valves would remain available.
| |
| During inoperability of the PT-505 and PT-506 transmitters, automatic reactor trip functions on OTDT remained available and would have functioned in the event that a postulated load rejection went unabated.
| |
| As identified in the Description of Occurrence section, with PT-505 failing downscale, automatic control rod insertion began, per design. Rod motion was stopped by placing rod control in the manual mode of operation.
| |
| Operations personnel had reacted quickly to the event thereby limiting rod movement.
| |
| There was no observed power reduction.
| |
| CORRECTIVE ACTION: Following this event, an Operations Department Night Order Book entry was made to ensure the Turbine Building ventilation system is aligned to preclude chilling the PT-505 and PT-506 instrument sensing lines. The failed heat tracing will be repaired, and the missing sensing line insulation will be replaced.
| |
| ,, , LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000311 LER NUMBER 93-004-00 PAGE 5 of 5 The admin'istrative program for preparing Salem station for Winter operation will be reviewed.
| |
| Revisions will be incorporated as appropriate. | |
| System Engineering is continuing to assess why the PT-505 and PT-506 channels failed in opposite directions. | |
| Also, the Salem Unit 1 heat trace configuration will be evaluated. | |
| MJP:pc SORC Mtg. 93-021 Y8&4r Manager -{,/ Salem Operations}}
| |
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Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Text
e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station March 5, 1993 U.S. Nuclear*Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-004-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR
- 50. 73 (a) (2) (i) (B). This report is required to be issued within thirty (30) days of event discovery.
Sincerely yours, o;.~ A. Vondra General Manager -
Salem Operations MJP:pc Distribution 110032 The Energy People
- }eJ} I I 9303110188 930305 95-2189 ( 1OM) 12-89 PDR ADOCK 05000311 S PDR
t NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) - APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME 111 DOCKET NUMBER 121 PAGE 13)
Salem Generating Station - Unit 2 TITLE 14) 0 I 5 I 0 I 0 I 0 13 I 11 l I 1 OF 0 ,s Tech Spec 3.0.3 Entry: Inoperability of Both Turbine First Stage Pressure Channels.
EVENT DATE 151 LEA NUMBER 161 REPORT DATE 171 OTHER FACILITIES INVOLVED 18)
MONTH DAY YEAR YEAR J~t SE~~~~~~AL {) ~~~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI d 2 oI E 9 3 91 3 - ol o14 - oI o oI3 ol s 9 I 3 OPERATING l-T_H,IS-::R::E-::PO::R::-T:--ls_s_u_eM_l_T_TE_D_P_u_Rs_u,A_NT_TTO:.._T:.._H:..:.E_R:..:.~Q=-U:..:.l:..:.:RE=M:..:.E:..:.NTS:.:....::0:..:.F...:.10:....C::F...:.:R,..:§~:~(C::.::hB=Ck:...:o:::n:....*o::.r.::m=o':.::.*.:of~t::h*~fo::ll.::ow::in~gi:...:1~11~1--..---------J 1
I MODE (9) I
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- 50.38lcll2l
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111"4[41~ ~-=::~:::;:
60.7311ll2llil 50.7311112llviiillAI 366Ai 60.73(1l12lliil
....._ 50.7311l12llviiillBI 50.7311l12Hiiil 50.731111211*1 LICENSEE CONTACT FOR THIS LER 112)
NAME TELEPHONE NUMBER AREA CODE M. J. Pastva, Jr. - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC- MANUFAC*
CAUSE SYSTEM COMPONENT SYSTEM COMPONENT TURER TUR ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED n YES (If Y*S. compl*to EXPECTED SUBMISSION DA TEI ABSTRACT (Limit to 1400 spaces, i.e.* approximately fifteen single-space typewrittsn Jines) (16) hzi NO SUBMISSION DATE (151 I I I At 2105 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.009525e-4 months <br />, on 2/6/93, Tech. Spec. 3.0.3 was entered due to operation outside Tech. Spec. Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings. PT-505 and PT-506 provide turbine power input for plant control during power operation. PT-505 was indicating downscale and PT-506 was indicating upscale. This was first observed via automatic rod insertion. Rod motion was stopped by placing rod control in manual. The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased ambient air temperature around the sensing line. Satisfactory channel functional checks showed the instruments operable and at 2109 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.024745e-4 months <br /> (same day), Tech. Spec. 3.0.3 was exited. The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate. When this event occurred, the outside ambient temperature was less than 20°F. Missing insulation from.the channels' transmitter sensing lines (which will be replaced) and the PT-506 heat trace had failed (which will be repaired) was identified. An Operations Department Night Order Book entry has been made to preclude chilling the PT-505 and PT-506 transmitter sensing lines. The administrative program for preparing Salem Station for Winter operation will be reviewed. Revisions will be incorporated as appropriate.
NRC Form 366 16-89)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 2 of 5 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification system (EIIS) codes are identified in the text as {XX}
IDENTIFICATION OF OCCURRENCE:
Technical Specification 3.0.3 Entry: Inoperability of Both Turbine First Stage Pressure Channels Event Date: 2/6/93 Report Date: 3/5/93 This report was initiated by Incident Report No.93-112.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100% - Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE:
At 2105 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.009525e-4 months <br />, on February 6, 1993 Technical Specification 3.0.3 was entered due to operation outside Technical Specification Table 3.3-3 Action 14. Both main turbine first stage impulse pressure indication channels (PT-505 and PT-506) were indicating false readings. PT-505 was indicating downscale and PT-506 was indicating upscale. PT-505 and PT-506 provide turbine power input for plant control during power operation.
This was first observed, at 2105 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.009525e-4 months <br />, via automatic rod insertion.
Abnormal Operating Procedure, S2.0P-AB.ROD-0003(Q), "Continuous Rod Motion" was entered. Rod motion was stopped after placing rod control in the manual mode of operation and the affected control rods were withdrawn to prior position.
The PT-505 and PT-506 indications returned to normal within approximately one minute following a change in the building ventilation lineup which increased sensing line ambient air temperature. Satisfactory functional checks showed the channels operable and at 2109 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.024745e-4 months <br /> (same day), Technical Specification 3.0.3 was exited.
In MODES 1, 2, and 3, Technical Specification Table 3.3-3 requires a minimum of one (1) OPERABLE main steam flow indicator. Technical Specification Table 3.3-3 Action 14 states:
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 3 of 5 DESCRIPTION OF OCCURRENCE: (cont'd)
"With the number of OPERABLE Channels one less than the Total Number of Channels, operation may proceed until performance of the next required CHANNEL FUNCTIONAL TEST, provided the inoperable channel is placed in the tripped condition within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />."
Technical Specification 3.0.3 states:
"When a Limiting Condition for Operation is not met except as provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which the specification does not apply by placing it, as applicable, in:
- 1. At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
- 2. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- 3. At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Where corrective measures are completed that permit operation under the ACTION requirements, the ACTION may be taken in accordance with the specified time limits as measured from the time of failure to meet the Limiting Condition of Operation.
Exceptions to these requirements are stated in the individual specifications."
APPARENT CAUSE OF OCCURRENCE:
The root cause of this event is equipment failure. Sensing line protection from cold environment conditions was found to not be adequate. When this event occurred, the outside ambient temperature was less than 20°F. Investigation identified the following concerns:
PT-505 sensing line - Missing insulation from the entire length of the transmitter sensing line tray. Continuity checks showed the sensing line heat trace was functioning properly.
PT-506 Sensing Line - Burnt open primary and secondary heat trace wiring and controllers with a missing section of transmitter sensing line tray insulation.
It could not be determined how long the insulation has not been in place for either transmitter sensing line.
ANALYSIS OF OCCURRENCE:
Due to the entry into Technical Specification 3.0.3 this event is reportable to the Nuclear Regulatory Commission per Code of Federal Regulations 10CFR 50.73(a) (2) (i) (B).
This event did not affect the health and safety of the public. The PT-505 and PT-506 channels were inoperable for less than five (5)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 4 of 5 ANALYSIS OF OCCURRENCE: (cont'd) minutes during which time their functions were not challenged. Also, the automatic trip functions and engineered safety features were available.
PT-505 and PT-506 are first-stage turbine pressure sensors which provide inputs for reactor control during power operation. PT-505 provides: input into the Steam Dump System for indication of Reactor Coolant System {AB} reference temperature; input into the Rod Control System {AA} for T v reference values; input into the main steamline flow se~p2int; provides the level setpoint for Steam Generator level control; provides reference main turbine power signal to the turbine electrohydraulic control system; provides input into permissive interlock P-13 which is used for development of the P-7 permissive (the permissive for blocking certain reactor trip functions above 10% power); provides input to P-2 (a permissive to place control rods in automatic operation, above 15% power, for control rod withdrawal); and input into AMSAC (Anticipated Transient Without Scram Mitigation System Actuation Circuitry)
- PT-506 provides input to arm the Steam Dump System in the event of load reject, provides input into the high main steamline flow setpoint, and input into AMSAC.
With PT-505 failing downscale and PT-506 failing upscale, if there was a required automatic actuation of the Steam Dump System due to a valid load rejection signal, the steam dump valves would not automatically open. The MS10 atmospheric relief valves would open at their setpoint of approximately 1037 psi to mitigate the pressure transient. Manual operation of the Steam Dump System valves would remain available. During inoperability of the PT-505 and PT-506 transmitters, automatic reactor trip functions on OTDT remained available and would have functioned in the event that a postulated load rejection went unabated.
As identified in the Description of Occurrence section, with PT-505 failing downscale, automatic control rod insertion began, per design. Rod motion was stopped by placing rod control in the manual mode of operation. Operations personnel had reacted quickly to the event thereby limiting rod movement. There was no observed power reduction.
CORRECTIVE ACTION:
Following this event, an Operations Department Night Order Book entry was made to ensure the Turbine Building ventilation system is aligned to preclude chilling the PT-505 and PT-506 instrument sensing lines.
The failed heat tracing will be repaired, and the missing sensing line insulation will be replaced.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-004-00 5 of 5 CORRECTIVE ACTION: (cont'd)
The admin'istrative program for preparing Salem station for Winter operation will be reviewed. Revisions will be incorporated as appropriate.
System Engineering is continuing to assess why the PT-505 and PT-506 channels failed in opposite directions. Also, the Salem Unit 1 heat trace configuration will be evaluated.
Y8&4r
~G(g.eneral Manager -
{,/ Salem Operations MJP:pc SORC Mtg.93-021