|
|
(2 intermediate revisions by the same user not shown) |
Line 3: |
Line 3: |
| | issue date = 10/15/1997 | | | issue date = 10/15/1997 |
| | title = LER 97-003-00:on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containments Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been revised.W/971014 Ltr | | | title = LER 97-003-00:on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containments Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been revised.W/971014 Ltr |
| | author name = BAKKEN A C, VILLAR E H | | | author name = Bakken A, Villar E |
| | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY |
| | addressee name = | | | addressee name = |
Line 16: |
Line 16: |
|
| |
|
| =Text= | | =Text= |
| {{#Wiki_filter:e Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit OCT 14 1997 LR-N970674 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 SPECIAL REPORT 311/97-003 SALEM GENERATING STATION -UNIT 2 FACILITY OPERATING LICENSE DPR NO 75 DOCKET NO. 50-311 Gentlemen: | | {{#Wiki_filter:e OPS~G Publi~ Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit OCT 14 1997 LR-N970674 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 SPECIAL REPORT 311/97-003 SALEM GENERATING STATION - UNIT 2 FACILITY OPERATING LICENSE DPR NO 75 DOCKET NO. 50-311 Gentlemen: |
| This Special Report addresses the isolation of the Fire Protection Water to the Salem Unit 1 and 2 Auxiliary Buildings and Containments due to the closure of 1FP186 and 1FP187. This report is being submitted pursuant to the requirements of Section 6.9.3 of the Salem Unit 2 Technical Specifications. | | This Special Report addresses the isolation of the Fire Protection Water to the Salem Unit 1 and 2 Auxiliary Buildings and Containments due to the closure of 1FP186 and 1FP187. This report is being submitted pursuant to the requirements of Section 6.9.3 of the Salem Unit 2 Technical Specifications. |
| Attachment EHV/tcp C Distribution LER File 3.7 9710210010 971015 PDR ADOCK 05000311 S PDR Tl]*'"*)\'.'":. | | Sincerely, A. C. Bakken, III General Manager - |
| ''1\'1ll'' | | Salem Operations Attachment EHV/tcp C Distribution LER File 3.7 9710210010 971015 PDR ADOCK 05000311 S PDR Illllll lllll lllll lllll llllllc llll ,llll llll. |
| ii *1**1 1.. \C! ll i i.t1 iU'.'. . . Sincerely, A. C. Bakken, III General Manager -Salem Operations I llllll lllll lllll lllll llllll llll llll llll * !ii & 7 , c , . 95-2168 REV 6. | | * !ii & 7 , |
| NRCFORM 366 (4-95) U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 04/30/98 LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. | | Tl] *'"*)\'.'":. |
| FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) (See reverse for required number of digits/characters for each block) DOCKET NUMBER (2) PAGE (3) SALEM GENERATING STATION UNIT 2 05000311 1 OF 5 TITLE (4) LOSS OF FIRE PROTECTION WATER TO THE SALEM UNIT 1 AND 2 AUXILIARY BUILDINGS AND CONTAINMENTS.
| | 1.. ~I |
| EVENT DATE (5) MONTH DAY YEAR 09 09 97 ! OPERATING MODE(9) POWER LEVEL (10) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) YEAR I FACILITY NAME DOCKET NUMBER SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER STATION UNIT 1 05000272 97 003 00 10 15 97 FACILITY NAME DOCKET NUMBER ----05000 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) 20.2201 (b) 20.2203(a)(2)(v) | | . \C! |
| : 50. 73(a)(2)(i)
| | ''1\'1ll'' ii *1** 1 t~ ll |
| : 50. 73(a)(2)(viii) 20.2203(a)(1) 20.2203(a)(3)(i)
| | . ~ i i.t1 iU'.'. |
| : 50. 73(a)(2)(ii)
| | 95-2168 REV 6. 9~ |
| : 50. 73(a)(2)(x) 20.2203(a)(2)(i) 20.2203(a)(3)(ii)
| | |
| : 50. 73(a)(2)(iii)
| | NRCFORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. |
| : 73. 71 20.2203(a)(2)(ii) 20.2203(a)(4)
| | REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INDUSTRY. |
| : 50. 73(a)(2)(iv)
| | COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION FORWARD AND RECORDS MANAGEMENT BRANCH (T-6 F33), U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. |
| X OTHER 20.2203(a)(2)(iii) 50.36(c)(1) | | FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3) |
| : 50. 73(a)(2)(v) 20.2203(a)(2)(iv) 50.36(c)(2)
| | SALEM GENERATING STATION UNIT 2 05000311 1 OF 5 TITLE (4) |
| : 50. 73(a)(2)(vii)
| | LOSS OF FIRE PROTECTION WATER TO THE SALEM UNIT 1 AND 2 AUXILIARY BUILDINGS AND CONTAINMENTS. |
| LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER (Include Area Code) E. H. Villar (Station Licensing Enginner) 609 339 5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) I YES (If yes, complete EXPECTED SUBMISSION DATE). ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) EXPECTED SUBMISSION DATE (15) MONTH DAY YEAR At 2210 hrs on September 16, 1997, a Unit 1 Nuclear Control Operator (NCO) identified that the fire protection water for Salem Units 1 and 2 Auxiliary Buildings and Containment was isolated. | | EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| Fire protection water for these areas is supplied via valves 1FP186 and 1FP187, which were found closed. While the exact cause of the valves being mispositoned could not be determined, the valves were most probably misaligned during relamping activities on September 9, 1997. The cause of the condition going unidentified is attributed to human error due to inattention to detail by the NCO and the Loss Prevention Operators during subsequent panel reviews. Fire protection personnel were promptly notified, and the valves were opened at 2237 hrs. | | MONTH DAY YEAR YEAR I SEQUENTIAL NUMBER IREVISION NUMBER MONTH DAY YEAR FACILITY NAME STATION UNIT 1 DOCKET NUMBER 05000272 FACILITY NAME DOCKET NUMBER 09 09 97 97 -- 003 -- 00 10 15 97 05000 |
| | ! OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) |
| | MODE(9) 20.2201 (b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) 50. 73(a)(2)(viii) |
| | POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50. 73(a)(2)(ii) 50. 73(a)(2)(x) |
| | LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73. 71 20.2203(a)(2)(ii) 20.2203(a)(4) 50. 73(a)(2)(iv) X OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) ~rrnc~~ ~.~~~~~elow 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER (Include Area Code) |
| | E. H. Villar (Station Licensing Enginner) 609 339 5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR YES SUBMISSION I(If yes, complete EXPECTED SUBMISSION DATE). DATE (15) |
| | ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) |
| | At 2210 hrs on September 16, 1997, a Unit 1 Nuclear Control Operator (NCO) identified that the fire protection water for Salem Units 1 and 2 Auxiliary Buildings and Containment was isolated. Fire protection water for these areas is supplied via valves 1FP186 and 1FP187, which were found closed. |
| | While the exact cause of the valves being mispositoned could not be determined, the valves were most probably misaligned during relamping activities on September 9, 1997. The cause of the condition going unidentified is attributed to human error due to inattention to detail by the NCO and the Loss Prevention Operators during subsequent panel reviews. |
| | Fire protection personnel were promptly notified, and the valves were opened at 2237 hrs. |
| * Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively. | | * Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively. |
| This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30 Special Report. NRC FORM 366 (4-95) | | This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30 Special Report. |
| NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) 05000311 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 2 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) PLANT IDENTIFICATION: | | NRC FORM 366 (4-95) |
| Salem Generating Station -Unit 2 Public Service Electric and Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE: | | |
| 97 --003 00 PAGE (3) 2 OF 5 Loss of Fire Protection Water to Salem Units 1 and 2 Auxiliary Buildings and Containments.
| | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95) |
| Date of Occurrence: | | LICENSEE EVENT REPORT (LER) |
| Date of Identification Report Date: September 9, 1997 September 16, 1997 October 15, 1997 CONDITIONS PRIOR TO OCCURRENCE:
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 2 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| Salem Unit 1 -Defueled Salem Unit 2 -Mode 1 approximately 58% Power DESCRIPTION OF OCCURRENCE: | | PLANT IDENTIFICATION: |
| The following is a timeline of the events, as recreated from operators logs, interviews, and a brief summary of the event recreation, as well as .a level one root cause investigation Timeline July 15, 1997 -Valves 1FP186 and 1FP187 were stroked open and closed using surveillance procedure SC.FP-ST.FS-0:07. | | Salem Generating Station - Unit 2 Public Service Electric and Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE: |
| September 1, 1997-Valves 1FP186 and 1FP187 were locally position verified open by Loss Prevention personnel. | | Loss of Fire Protection Water to Salem Units 1 and 2 Auxiliary Buildings and Containments. |
| September 2, 1997 -1FP147 was stroked open and closed during performance of procedure Sl.RA-IS.ZZ-0001, "Types B And C Leak Rate Test." The controls for 1FP147 are located on panel 1RP5, immediately to the right of the control for 1FP186 and 1FP187. NRG FORM 366A (4-95) | | Date of Occurrence: September 9, 1997 Date of Identification September 16, 1997 Report Date: October 15, 1997 CONDITIONS PRIOR TO OCCURRENCE: |
| NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) 05000311 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 2 97 --003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) DESCRIPTION OF OCCURRENCE (cont'd); | | Salem Unit 1 - Defueled Salem Unit 2 - Mode 1 approximately 58% Power DESCRIPTION OF OCCURRENCE: |
| PAGE (3) 3 OF 5 September 6, 1997 -I&C Craft personnel started relamping activities at panel 1RP5 per Work Order. September 9, 1997 -I&C Craft personnel completed relamping 1RP5. Work Order notations and personnel interviews indicate that valves 1FP186 and 1FP187 were relamped on the second night the panel was worked on. This work was performed from 2100 hrs on September 8 to 0700 hrs on September 9, 1997. September 16, 1997 -At 2210 hrs a Unit 1 NCO noted that the indicator for valves 1FP186 and 1FP187 was illuminated, and at 2225, the valves were field verified closed by Loss Prevention personnel.
| | The following is a timeline of the events, as recreated from operators logs, interviews, and a brief summary of the event recreation, as well as .a level one root cause investigation Timeline July 15, 1997 - Valves 1FP186 and 1FP187 were stroked open and closed using surveillance procedure SC.FP-ST.FS-0:07. |
| At 2237, Operations personnel opened the valves, and at 2243, the valves were field verified open by Loss Prevention personnel. | | September 1, 1997- Valves 1FP186 and 1FP187 were locally position verified open by Loss Prevention personnel. |
| | September 2, 1997 - 1FP147 was stroked open and closed during performance of procedure Sl.RA-IS.ZZ-0001, "Types B And C Leak Rate Test." The controls for 1FP147 are located on panel 1RP5, immediately to the right of the control for 1FP186 and 1FP187. |
| | NRG FORM 366A (4-95) |
| | |
| | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 3 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | DESCRIPTION OF OCCURRENCE (cont'd); |
| | September 6, 1997 - I&C Craft personnel started relamping activities at panel 1RP5 per Work Order. |
| | September 9, 1997 - I&C Craft personnel completed relamping 1RP5. Work Order notations and personnel interviews indicate that valves 1FP186 and 1FP187 were relamped on the second night the panel was worked on. This work was performed from 2100 hrs on September 8 to 0700 hrs on September 9, 1997. |
| | September 16, 1997 - At 2210 hrs a Unit 1 NCO noted that the indicator for valves 1FP186 and 1FP187 was illuminated, and at 2225, the valves were field verified closed by Loss Prevention personnel. At 2237, Operations personnel opened the valves, and at 2243, the valves were field verified open by Loss Prevention personnel. |
| Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively. | | Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively. |
| This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30, Special Report. CAUSE OF OCCURRENCE; The exact cause of how the 1FP186 and 1FP187 valves were closed, and could have potentially been closed from September 1, 1997, through September 16, 1997, could not be determined. | | This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30, Special Report. |
| These dates represent the times when the 1FP186 and 1FP187 valves were field verified open by Loss Prevention personnel. | | CAUSE OF OCCURRENCE; The exact cause of how the 1FP186 and 1FP187 valves were closed, and could have potentially been closed from September 1, 1997, through September 16, 1997, could not be determined. These dates represent the times when the 1FP186 and 1FP187 valves were field verified open by Loss Prevention personnel. |
| However from the timeline of the events, as presented above, the most probable cause for the inadvertent closure of the 1FP186 and 1FP187 valves was relamping activities on 1RP5 panel on September 9, 1997. NRG FORM 366A (4-95) | | However from the timeline of the events, as presented above, the most probable cause for the inadvertent closure of the 1FP186 and 1FP187 valves was relamping activities on 1RP5 panel on September 9, 1997. |
| ' NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) 05000311 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 2 97 --003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) CAUSE OF OCCURRENCE (cont'd): | | NRG FORM 366A (4-95) |
| PAGE (3) 4 OF 5 The cause for this condition going unidentified for the period from September 9, 1997, through September 16, 1997 is attributed to human error due to inattention to detail by the Nuclear Control Operators and the Loss Prevention Operators during subsequent panel reviews. The reviews did not focus on valve position indication, but were focused on verification of alarm status and lamp functionality.
| | |
| | ' NRC FORM 366A (4-95) |
| | FACILITY NAME (1) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION DOCKET NUMBER (2) |
| | U.S. NUCLEAR REGULATORY COMMISSION LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 4 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | CAUSE OF OCCURRENCE (cont'd): |
| | The cause for this condition going unidentified for the period from September 9, 1997, through September 16, 1997 is attributed to human error due to inattention to detail by the Nuclear Control Operators and the Loss Prevention Operators during subsequent panel reviews. The reviews did not focus on valve position indication, but were focused on verification of alarm status and lamp functionality. |
| PRIOR SIMILAR OCCURRENCES: | | PRIOR SIMILAR OCCURRENCES: |
| A search of the LER database using the phrase "fire protection" did not identify any LERs within the past five years related to mispositioned fire protection valves. Similar searches were performed using the same phrases as described above for the coirective action program database searches, and no applicable documents were identified. | | A search of the LER database using the phrase "fire protection" did not identify any LERs within the past five years related to mispositioned fire protection valves. Similar searches were performed using the same phrases as described above for the coirective action program database searches, and no applicable documents were identified. |
| SAFETY CONSEQUENCES AND IMPLICATIONS: | | SAFETY CONSEQUENCES AND IMPLICATIONS: |
| Although fire suppression was potentially unavailable during the period from September 1 (when the valves were field verified opened) to September 16 (when the valves were again field verified opened), there were hourly roving fire watch tours of the Unit 1 and 2 Auxiliary Buildings. | | Although fire suppression was potentially unavailable during the period from September 1 (when the valves were field verified opened) to September 16 (when the valves were again field verified opened), there were hourly roving fire watch tours of the Unit 1 and 2 Auxiliary Buildings. These roving fire watch tours were established for other unrelated fire protection issues, but they did provide a level of assurance that a fire would not have gone undetected. PSE&G has an onsite dedicated Fire Protection Department. Additionally, the fire protection detection system for the Auxiliary Buildings and Containments was unaffected by the closure of the 1FP186 and 1FP187 valves, which provides the primary means of detection. |
| These roving fire watch tours were established for other unrelated fire protection issues, but they did provide a level of assurance that a fire would not have gone undetected. | | CORRECTIVE ACTIONS TAKEN: |
| PSE&G has an onsite dedicated Fire Protection Department. | | The valves were opened at 2237 hrs on September 16, 1997, and locally verified open by Loss Prevention personnel at 2243 hrs. |
| Additionally, the fire protection detection system for the Auxiliary Buildings and Containments was unaffected by the closure of the 1FP186 and 1FP187 valves, which provides the primary means of detection. | | NRC FORM 366A (4-95) |
| CORRECTIVE ACTIONS TAKEN: The valves were opened at 2237 hrs on September 16, 1997, and locally verified open by Loss Prevention personnel at 2243 hrs. NRC FORM 366A (4-95) | |
|
| |
|
| NRC FORM 366A LICENSFE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) SALEM.GENERATING STATION UNIT 2 U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 5 OF 5 97 --003 OD TEXT (If more space is required, use additional copies of NRC Form 366A) (17) CORRECTIVE ACTIONS TAKEN (cont'd): | | ~---------- |
| On September 18, 1997, Loss Prevention personnel completed a lineup verification of Fire Protection valves (C02 and Water) at Salem station, and as a temporary compensatory initiated position verification of the 1FP186 and 1FP187 valves on a twice per shift (every 6 hours) basis pending completion of the cause investigation. | | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION LICENSFE EVENT REPORT (LER) |
| The monthly verification of Hope Creek valves was performed the week prior so no further action was initiated for Hope Creek. Loss Prevention tours have been revised to include a once per shift verification of valve position for 1FP186 and 1FP187. This measure will remain in place until the 1RP5 panel status report checklist is revised to include verification of 1FP186 and 1FP187 indicator lamp test once per shift. Operators will receive training on the controls associated with the 1FP186 and 1FP187 valves. This training will be completed by November 30, 1997. An event notice will be issued to Operations, Work Control, Loss Prevention and Station Planning to share the lessons learned from this event. This notice will be issued by October 31, 1997. NRC FORM 366A (4-95)}} | | TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 5 OF 5 SALEM.GENERATING STATION UNIT 2 97 -- 003 OD TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | CORRECTIVE ACTIONS TAKEN (cont'd): |
| | On September 18, 1997, Loss Prevention personnel completed a lineup verification of Fire Protection valves (C02 and Water) at Salem station, and as a temporary compensatory measure~ initiated position verification of the 1FP186 and 1FP187 valves on a twice per shift (every 6 hours) basis pending completion of the cause investigation. The monthly verification of Hope Creek valves was performed the week prior so no further action was initiated for Hope Creek. |
| | Loss Prevention tours have been revised to include a once per shift verification of valve position for 1FP186 and 1FP187. This measure will remain in place until the 1RP5 panel status report checklist is revised to include verification of 1FP186 and 1FP187 indicator lamp test once per shift. |
| | Operators will receive training on the controls associated with the 1FP186 and 1FP187 valves. This training will be completed by November 30, 1997. |
| | An event notice will be issued to Operations, Work Control, Loss Prevention and Station Planning to share the lessons learned from this event. This notice will be issued by October 31, 1997. |
| | NRC FORM 366A (4-95)}} |
Similar Documents at Salem |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
e OPS~G Publi~ Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit OCT 14 1997 LR-N970674 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 SPECIAL REPORT 311/97-003 SALEM GENERATING STATION - UNIT 2 FACILITY OPERATING LICENSE DPR NO 75 DOCKET NO. 50-311 Gentlemen:
This Special Report addresses the isolation of the Fire Protection Water to the Salem Unit 1 and 2 Auxiliary Buildings and Containments due to the closure of 1FP186 and 1FP187. This report is being submitted pursuant to the requirements of Section 6.9.3 of the Salem Unit 2 Technical Specifications.
Sincerely, A. C. Bakken, III General Manager -
Salem Operations Attachment EHV/tcp C Distribution LER File 3.7 9710210010 971015 PDR ADOCK 05000311 S PDR Illllll lllll lllll lllll llllllc llll ,llll llll.
Tl] *'"*)\'.'":.
1.. ~I
. \C!
1\'1ll ii *1** 1 t~ ll
. ~ i i.t1 iU'.'.
95-2168 REV 6. 9~
NRCFORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INDUSTRY.
COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION FORWARD AND RECORDS MANAGEMENT BRANCH (T-6 F33), U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
SALEM GENERATING STATION UNIT 2 05000311 1 OF 5 TITLE (4)
LOSS OF FIRE PROTECTION WATER TO THE SALEM UNIT 1 AND 2 AUXILIARY BUILDINGS AND CONTAINMENTS.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR I SEQUENTIAL NUMBER IREVISION NUMBER MONTH DAY YEAR FACILITY NAME STATION UNIT 1 DOCKET NUMBER 05000272 FACILITY NAME DOCKET NUMBER 09 09 97 97 -- 003 -- 00 10 15 97 05000
! OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE(9) 20.2201 (b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) 50. 73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50. 73(a)(2)(ii) 50. 73(a)(2)(x)
LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73. 71 20.2203(a)(2)(ii) 20.2203(a)(4) 50. 73(a)(2)(iv) X OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) ~rrnc~~ ~.~~~~~elow 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
E. H. Villar (Station Licensing Enginner) 609 339 5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR YES SUBMISSION I(If yes, complete EXPECTED SUBMISSION DATE). DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
At 2210 hrs on September 16, 1997, a Unit 1 Nuclear Control Operator (NCO) identified that the fire protection water for Salem Units 1 and 2 Auxiliary Buildings and Containment was isolated. Fire protection water for these areas is supplied via valves 1FP186 and 1FP187, which were found closed.
While the exact cause of the valves being mispositoned could not be determined, the valves were most probably misaligned during relamping activities on September 9, 1997. The cause of the condition going unidentified is attributed to human error due to inattention to detail by the NCO and the Loss Prevention Operators during subsequent panel reviews.
Fire protection personnel were promptly notified, and the valves were opened at 2237 hrs.
- Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively.
This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30 Special Report.
NRC FORM 366 (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 2 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
PLANT IDENTIFICATION:
Salem Generating Station - Unit 2 Public Service Electric and Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Loss of Fire Protection Water to Salem Units 1 and 2 Auxiliary Buildings and Containments.
Date of Occurrence: September 9, 1997 Date of Identification September 16, 1997 Report Date: October 15, 1997 CONDITIONS PRIOR TO OCCURRENCE:
Salem Unit 1 - Defueled Salem Unit 2 - Mode 1 approximately 58% Power DESCRIPTION OF OCCURRENCE:
The following is a timeline of the events, as recreated from operators logs, interviews, and a brief summary of the event recreation, as well as .a level one root cause investigation Timeline July 15, 1997 - Valves 1FP186 and 1FP187 were stroked open and closed using surveillance procedure SC.FP-ST.FS-0:07.
September 1, 1997- Valves 1FP186 and 1FP187 were locally position verified open by Loss Prevention personnel.
September 2, 1997 - 1FP147 was stroked open and closed during performance of procedure Sl.RA-IS.ZZ-0001, "Types B And C Leak Rate Test." The controls for 1FP147 are located on panel 1RP5, immediately to the right of the control for 1FP186 and 1FP187.
NRG FORM 366A (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 3 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE (cont'd);
September 6, 1997 - I&C Craft personnel started relamping activities at panel 1RP5 per Work Order.
September 9, 1997 - I&C Craft personnel completed relamping 1RP5. Work Order notations and personnel interviews indicate that valves 1FP186 and 1FP187 were relamped on the second night the panel was worked on. This work was performed from 2100 hrs on September 8 to 0700 hrs on September 9, 1997.
September 16, 1997 - At 2210 hrs a Unit 1 NCO noted that the indicator for valves 1FP186 and 1FP187 was illuminated, and at 2225, the valves were field verified closed by Loss Prevention personnel. At 2237, Operations personnel opened the valves, and at 2243, the valves were field verified open by Loss Prevention personnel.
Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively.
This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30, Special Report.
CAUSE OF OCCURRENCE; The exact cause of how the 1FP186 and 1FP187 valves were closed, and could have potentially been closed from September 1, 1997, through September 16, 1997, could not be determined. These dates represent the times when the 1FP186 and 1FP187 valves were field verified open by Loss Prevention personnel.
However from the timeline of the events, as presented above, the most probable cause for the inadvertent closure of the 1FP186 and 1FP187 valves was relamping activities on 1RP5 panel on September 9, 1997.
NRG FORM 366A (4-95)
' NRC FORM 366A (4-95)
FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
U.S. NUCLEAR REGULATORY COMMISSION LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 4 OF 5 SALEM GENERATING STATION UNIT 2 97 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
CAUSE OF OCCURRENCE (cont'd):
The cause for this condition going unidentified for the period from September 9, 1997, through September 16, 1997 is attributed to human error due to inattention to detail by the Nuclear Control Operators and the Loss Prevention Operators during subsequent panel reviews. The reviews did not focus on valve position indication, but were focused on verification of alarm status and lamp functionality.
PRIOR SIMILAR OCCURRENCES:
A search of the LER database using the phrase "fire protection" did not identify any LERs within the past five years related to mispositioned fire protection valves. Similar searches were performed using the same phrases as described above for the coirective action program database searches, and no applicable documents were identified.
SAFETY CONSEQUENCES AND IMPLICATIONS:
Although fire suppression was potentially unavailable during the period from September 1 (when the valves were field verified opened) to September 16 (when the valves were again field verified opened), there were hourly roving fire watch tours of the Unit 1 and 2 Auxiliary Buildings. These roving fire watch tours were established for other unrelated fire protection issues, but they did provide a level of assurance that a fire would not have gone undetected. PSE&G has an onsite dedicated Fire Protection Department. Additionally, the fire protection detection system for the Auxiliary Buildings and Containments was unaffected by the closure of the 1FP186 and 1FP187 valves, which provides the primary means of detection.
CORRECTIVE ACTIONS TAKEN:
The valves were opened at 2237 hrs on September 16, 1997, and locally verified open by Loss Prevention personnel at 2243 hrs.
NRC FORM 366A (4-95)
~----------
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION LICENSFE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000311 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 5 OF 5 SALEM.GENERATING STATION UNIT 2 97 -- 003 OD TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
CORRECTIVE ACTIONS TAKEN (cont'd):
On September 18, 1997, Loss Prevention personnel completed a lineup verification of Fire Protection valves (C02 and Water) at Salem station, and as a temporary compensatory measure~ initiated position verification of the 1FP186 and 1FP187 valves on a twice per shift (every 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />) basis pending completion of the cause investigation. The monthly verification of Hope Creek valves was performed the week prior so no further action was initiated for Hope Creek.
Loss Prevention tours have been revised to include a once per shift verification of valve position for 1FP186 and 1FP187. This measure will remain in place until the 1RP5 panel status report checklist is revised to include verification of 1FP186 and 1FP187 indicator lamp test once per shift.
Operators will receive training on the controls associated with the 1FP186 and 1FP187 valves. This training will be completed by November 30, 1997.
An event notice will be issued to Operations, Work Control, Loss Prevention and Station Planning to share the lessons learned from this event. This notice will be issued by October 31, 1997.
NRC FORM 366A (4-95)