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| | issue date = 04/20/1998 | | | issue date = 04/20/1998 |
| | title = LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected | | | title = LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected |
| | author name = VILLAR E H | | | author name = Villar E |
| | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:* | | {{#Wiki_filter:NRC FORM 366 (4-95) |
| * NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
| | U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) |
| FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION (See reverse for required number of AND RECORDS MANAGEMENT BRANCH (HI F33), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 2055!HI001, AND TO digits/characters for each block) THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) DOCKET NUllDER (2) PAGE (3) SALEM GENERATING STATION UNIT 1 05000272 1of5 TITLE (4) INADEQUATE TESTING OF THE SALEM UNIT 1 CONTAINMENT AIR LOCKS RESULTED IN ENTERING TECHNICAL SPECIFICATION | | * APPROVED BY OMB NO. 3150-0104 EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. |
| | REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (HI F33), U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON, DC 2055!HI001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. |
| | FACILITY NAME (1) DOCKET NUllDER (2) PAGE (3) |
| | SALEM GENERATING STATION UNIT 1 05000272 1of5 TITLE (4) |
| | INADEQUATE TESTING OF THE SALEM UNIT 1 CONTAINMENT AIR LOCKS RESULTED IN ENTERING TECHNICAL SPECIFICATION 3.0.3. |
| | EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| | FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem Generating Station Unit 2 I 05000311 03 23 98 98 08 -- 00 04 98 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) |
| | MODE(9) 5 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i) 50. 73(a)(2)(viii) |
| | POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50. 73(a)(2)(ii) 50. 73(a)(2)(x) |
| | LEVEL (10) 0 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50. 73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) Spec~in Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER (Include Area Code) |
| | E. H. Villar, Station Licensing Engineer (609) 339-5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS |
| | ~I~li~~~~f~ ~i~ ~i CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS |
| | ~i~ ~l ~ ~ l~ ~jlj~lij~fil rm~~i~~~i~~m~~r 1 |
| | 11111111111111111-SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR SUBMISSION |
| | . IYES (If yes, complete EXPECTED SUBMISSION DATE). x1NO DATE (15) |
| | ABSTRACT (Limitto 1400 spaces, i.e., approximately 15 single-spaced typewritten Imes) (16) |
| | During a periodic performance of Sl.RA-IS.ZZ-OOOl(Q) I "Type B Mechanical Penetration Leak Rate Testing", In-Service inspection personnel noted that the Schrader valve that controls the air supply to the exterior door was not fulfilling its intended function. This condition meant that no air was being supplied to the exterior door seal during the performance of the leak rate test under ,, procedure Sl.OP-ST.CAN-0004 (Q)"Containment Air Lock Local Leak Rate Test. This resulted in a failure to meet the surveillance requirements of Technical Specification 3.6.1.3. for both Unit 1 containment air locks, and Technical Specification 3.0.3 was entered. The most probable cause is attributed to less-than-adequate practices during the replacement of the equalizing valve in accordance with a design change package. Corrective actions taken were to correct the Schrader valve linkage for both Salem Unit 1 containment air locks. The leak rate test was performed satisfactorily, and the Salem Unit 2 airlocks were inspected and found to be working properly. |
| | This condition represents a reportable condition under the provisions of 10CFR50.73 (a) (2) ( i) (B) 9804270107 980420 PDR ADOCK 05000272 S PDR |
|
| |
|
| ====3.0.3. EVENT====
| | NRC FORM 366A (4-95) |
| DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem Generating Station Unit 2 05000311 03 23 98 98 08 00 04 98 FACILITY NAME DOCKET NUMBER --05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) MODE(9) 5 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i)
| | * LICENSEE EVENT REPORT (LER). |
| : 50. 73(a)(2)(viii)
| | TEXT CONTINUATION |
| POWER 20.2203(a)(1) 20.2203(a)(3)(i)
| | * U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 2 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| : 50. 73(a)(2)(ii)
| | PLANT AND SYSTEM IDENTIFICATION Westinghouse - Pressurized Water Reactor Containment Air Lock {NH/AL}* |
| : 50. 73(a)(2)(x)
| |
| LEVEL (10) 0 20.2203(a)(2)(i) 20.2203(a)(3)(ii)
| |
| : 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(ii) 20.2203(a)(4)
| |
| : 50. 73(a)(2)(iv)
| |
| OTHER 20.2203(a)(2)(iii) 50.36(c)(1)
| |
| : 50. 73(a)(2)(v)
| |
| Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2)
| |
| : 50. 73(a)(2)(vii)
| |
| LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER (Include Area Code) E. H. Villar, Station Licensing Engineer (609) 339-5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS li fil TONPRDS r 1 11111111111111111-SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR IYES x1NO SUBMISSION . (If yes, complete EXPECTED SUBMISSION DATE). DATE (15) ABSTRACT (Limitto 1400 spaces, i.e., approximately 15 single-spaced typewritten Imes) (16) During a periodic performance of Sl.RA-IS.ZZ-OOOl(Q) | |
| I "Type B Mechanical Penetration Leak Rate Testing", In-Service inspection personnel noted that the Schrader valve that controls the air supply to the exterior door was not fulfilling its intended function.
| |
| This condition meant that no air was being supplied to the exterior door seal during the performance of the leak rate test under procedure Sl.OP-ST.CAN-0004 (Q)"Containment Air Lock Local Leak Rate Test. ,, This resulted in a failure to meet the surveillance requirements of Technical Specification 3.6.1.3. for both Unit 1 containment air locks, and Technical Specification 3.0.3 was entered. The most probable cause is attributed to less-than-adequate practices during the replacement of the equalizing valve in accordance with a design change package. Corrective actions taken were to correct the Schrader valve linkage for both Salem Unit 1 containment air locks. The leak rate test was performed satisfactorily, and the Salem Unit 2 airlocks were inspected and found to be working properly.
| |
| This condition represents a reportable condition under the provisions of 10CFR50.73 (a) (2) ( i) (B) 9804270107 980420 PDR ADOCK 05000272 S PDR
| |
| * | |
| * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER). TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 2 OF 5 SALEM GENERATING STATION UNIT 1 98 --08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) PLANT AND SYSTEM IDENTIFICATION Westinghouse
| |
| -Pressurized Water Reactor Containment Air Lock {NH/AL}* | |
| * Energy Industry Identification System (EIIS) codes and component function identifier codes appear in the text as {SS/CCC}. | | * Energy Industry Identification System (EIIS) codes and component function identifier codes appear in the text as {SS/CCC}. |
| IDENTIFICATION OF OCCURRENCE Identification Date: March 23, 1998. Reportability Date: March 23, 1998. Report Date: April 22, 1998. CONDITIONS PRIOR TO OCCURRENCE Unit 1: Mode 5 There were no structures, components, or systems that were inoperable at the start of the event that contributed to the event. DESCRIPTION OF OCCURRENCE On March 23, 1998, during a periodic performance of Sl.RA-IS.ZZ-OOOl(Q), "Type B Mechanical Penetration Leak Rate Testing", In-Service Inspection (ISI) personnel noted that the Schrader valve that controls the air supply to the 100 foot elevation exterior containment air lock door was not functioning properly. | | IDENTIFICATION OF OCCURRENCE Identification Date: March 23, 1998. |
| The 3-way Schrader valve is a vendor-supplied shutoff valve downstream of isolation valve 1CA1722 (control air isolation valve for the Unit 1 100 foot elevation air lock) . The Schrader valve is engaged by a mechanical arm which is linked to the handwheel for the exterior containment air lock door such that the Schrader valve is open when the exterior containment air lock door is closed. The Schrader valve when engaged by the door interlock mechanism (door full closed) allows control air to be supplied to both containment air lock doors (inner and outer doors) . Specifically, air is supplied to the space between the double seal and the knife edge that presses against them. NRC FORM 366A (4-95) | | Reportability Date: March 23, 1998. |
| *
| | Report Date: April 22, 1998. |
| * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 3 OF 5 SALEM GENERATING STATION UNIT 1 98 --08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) DESCRIPTION OF OCCURRENCE (cont'd) During the testing of the Unit 1 air locks, ISI personnel identified that: (1) one of the fasteners on the mechanical linkage was loose, and (2) one of the mechanical arms was bent such that a hard contact with the Schrader valve was not being made when the door was closed. In this condition, the interlock mechanism was not engaging the Schrader valve. Therefore, the outer containment air lock door seal was not being tested during the performance of the leak rate test under procedure Sl.RA-IS.ZZ-OOOl(Q), and the performance of Sl.OP-ST.CAN-0004(Q)
| | CONDITIONS PRIOR TO OCCURRENCE Unit 1: Mode 5 There were no structures, components, or systems that were inoperable at the start of the event that contributed to the event. |
| ,"Containment Air Lock Local Leak Rate Test." As a result of this condition, the Schrader valve for the 130 foot elevation containment air lock was inspected and a similar condition was identified by ISI personnel. | | DESCRIPTION OF OCCURRENCE On March 23, 1998, during a periodic performance of Sl.RA-IS.ZZ-OOOl(Q), |
| These conditions resulted in a to meet the surveillance requirements of Technical Specification 3.6.1.3. Technical Specification 3.6.1.3 requires each containment air lock to be operable in Modes 1 | | "Type B Mechanical Penetration Leak Rate Testing", In-Service Inspection (ISI) personnel noted that the Schrader valve that controls the air supply to the 100 foot elevation exterior containment air lock door was not functioning properly. |
| : 4. With an inoperable air lock, TS requires that the air lock be restored to operable within 24 hours or be in HOT STANDBY within the next 6 hours and in COLD SHUTDOWN within the following 30 hours. Since TS 3.6.1.3 Action does not allow more than one door to be inoperable, on March 23 at approximately 1400 hours, the control room operators declared both containment air locks inoperable, and entered Technical Specification 3.0.3. At approximately 1447 hours, on the same day, repairs to the air locks were performed, the containment air locks were retested satisfactorily in accordance with the provisions of Technical Specifications 4.0.3, and Technical Specifications 3.0.3 was exited. This condition, however, represents a reportable condition under the provisions of 10CFR50. 73 (a) (2) (i) (B) APPARENT CAUSE OF OCCURRENCE The most probable root cause is attributed to less-than-adequate work practices during the replacement of the equalizing valve. The Schrader valve is located inside the airlock in the upper right corner (facing the exterior door). It is directly below the equalizing valve. The Schrader valve is relatively protected from incidental contact due to normal traffic through the airlock. Therefore, it is highly unlikely that the observed condition could have occurred as a result of incidental contact by personnel while passing through the airlock. Investigation into this event, however, identified that the equalizing valve had been recently replaced in accordance with Design Change Package (DCP) 1EE00130 and work order 950905417 for both Unit 1 airlocks.
| | The 3-way Schrader valve is a vendor-supplied shutoff valve downstream of isolation valve 1CA1722 (control air isolation valve for the Unit 1 100 foot elevation air lock) . The Schrader valve is engaged by a mechanical arm which is linked to the handwheel for the exterior containment air lock door such that the Schrader valve is open when the exterior containment air lock door is closed. The Schrader valve when engaged by the door interlock mechanism (door full closed) allows control air to be supplied to both containment air lock doors (inner and outer doors) . Specifically, air is supplied to the space between the double seal and the knife edge that presses against them. |
| NRC FORM 366A (4-95) | | NRC FORM 366A (4-95) |
| *
| | |
| * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 98 --08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) APPARENT CAUSE OF OCCURRENCE (cont'd) PAGE (3) 4 OF 5 This work was completed just prior Unit 1 entering Mode 4. To replace the equalizing valve, it was necessary to do work on the mechanical linkage. A review of the DCP required testing indicated that a post modification leak rate test was performed satisfactorily using procedure Sl. RA-IS. ZZ-0001 (Q) on both containment air lock doors. Less than adequate work practices appeared to have, over time, resulted in the loosening of the fasteners.
| | NRC FORM 366A (4-95) |
| The loosening of the fasteners could have allowed the mechanical arm to be out-of-position such that the arm was slightly bent (in a direction parallel to its motion) when the door was closed. PREVIOUS OCCURRENCES A review of the LER database for Salem Units 1 and 2 issued in the last two years identified another LER involving containment air locks. Although not a similar occurrence, it is included for completeness of reporting. | | * LICENSEE EVENT REPORT (LER) |
| LER 272/96-005-16 "Inadequate Technical Specification Testing -Containment Airlock Gasket Leakage" was issued on January 21, 1998. This LER involved the failure to properly implement Technical Specification 4.6.1.3.a. | | TEXT CONTINUATION |
| Specifically, procedure Sl.OP-ST.CAN-0004(Q} | | * U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 3 OF 5 SALEM GENERATING STATION UNIT 1 08 00 98 -- |
| contained an acceptance value that was greater than allowed by TS. The corrective actions taken relative to this LER were appropriate for the identified root cause of LER 272/96-005-16, but would not have been expected to identify or prevent this event. SAFETY CONSEQUENCES AND IMPLICATIONS There were no safety consequences associated with this event, and the safety implications of a postulated event were minimal. Although the containment air lock outer door seals were not being tested, the inner seals were always tested satisfactorily. | | TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| Therefore, the containment air locks (inner seal) were able to maintain the overall leakage below the required Technical Specification limits. Maintaining the overall leakage below the required Technical Specification limits, ensures that the assumptions used in the dose analysis remain valid. Additionally, because Unit 1 had been shutdown for over two years, the activity contained within the fuel has been demonstrated by Engineering Evaluation to be much lower than the activity expected when compared with a normal refueling outage. Based on the above, there was no impact to the health and safety of the public. NRC FORM 366A (4-95) | | DESCRIPTION OF OCCURRENCE (cont'd) |
| *
| | During the testing of the Unit 1 air locks, ISI personnel identified that: |
| * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 98 --08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) CORRECTIVE ACTIONS 1. The Schrader valve linkage was repaired for both Salem Unit 1 containment air locks, and the leak rate test was performed satisfactorily.
| | (1) one of the fasteners on the mechanical linkage was loose, and (2) one of the mechanical arms was bent such that a hard contact with the Schrader valve was not being made when the door was closed. In this condition, the interlock mechanism was not engaging the Schrader valve. Therefore, the outer containment air lock door seal was not being tested during the performance of the leak rate test under procedure Sl.RA-IS.ZZ-OOOl(Q), and the performance of Sl.OP-ST.CAN-0004(Q) ,"Containment Air Lock Local Leak Rate Test." As a result of this condition, the Schrader valve for the 130 foot elevation containment air lock was inspected and a similar condition was identified by ISI personnel. |
| : 2. The Salem Unit 2 airlocks were inspected and found to be working properly. | | These conditions resulted in a ~ailure to meet the surveillance requirements of Technical Specification 3.6.1.3. Technical Specification 3.6.1.3 requires each containment air lock to be operable in Modes 1 thro~gh 4. With an inoperable air lock, TS requires that the air lock be restored to operable within 24 hours or be in HOT STANDBY within the next 6 hours and in COLD SHUTDOWN within the following 30 hours. Since TS 3.6.1.3 Action does not allow more than one door to be inoperable, on March 23 at approximately 1400 hours, the control room operators declared both containment air locks inoperable, and entered Technical Specification 3.0.3. At approximately 1447 hours, on the same day, repairs to the air locks were performed, the containment air locks were retested satisfactorily in accordance with the provisions of Technical Specifications 4.0.3, and Technical Specifications 3.0.3 was exited. |
| : 3. Additional corrective actions may be taken, as appropriate, upon completion of the level 2 condition report. 5 4. This event will be incorporated in the 1998 Maintenance Continuing Training for lessons learned. NRC FORM 366A (4-95) OF 5}} | | This condition, however, represents a reportable condition under the provisions of 10CFR50. 73 (a) (2) (i) (B) |
| | APPARENT CAUSE OF OCCURRENCE The most probable root cause is attributed to less-than-adequate work practices during the replacement of the equalizing valve. |
| | The Schrader valve is located inside the airlock in the upper right corner (facing the exterior door). It is directly below the equalizing valve. |
| | The Schrader valve is relatively protected from incidental contact due to normal traffic through the airlock. Therefore, it is highly unlikely that the observed condition could have occurred as a result of incidental contact by personnel while passing through the airlock. |
| | Investigation into this event, however, identified that the equalizing valve had been recently replaced in accordance with Design Change Package (DCP) 1EE00130 and work order 950905417 for both Unit 1 airlocks. |
| | NRC FORM 366A (4-95) |
| | |
| | NRC FORM 366A (4-95) |
| | * LICENSEE EVENT REPORT (LER) |
| | * U.S. NUCLEAR REGULATORY COMMISSION TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 4 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | APPARENT CAUSE OF OCCURRENCE (cont'd) |
| | This work was completed just prior Unit 1 entering Mode 4. To replace the equalizing valve, it was necessary to do work on the mechanical linkage. A review of the DCP required testing indicated that a post modification leak rate test was performed satisfactorily using procedure Sl. RA- IS. ZZ-0001 (Q) on both containment air lock doors. Less than adequate work practices appeared to have, over time, resulted in the loosening of the fasteners. |
| | The loosening of the fasteners could have allowed the mechanical arm to be out-of-position such that the arm was slightly bent (in a direction parallel to its motion) when the door was closed. |
| | PREVIOUS OCCURRENCES A review of the LER database for Salem Units 1 and 2 issued in the last two years identified another LER involving containment air locks. Although not a similar occurrence, it is included for completeness of reporting. LER 272/96-005-16 "Inadequate Technical Specification Testing - Containment Airlock Gasket Leakage" was issued on January 21, 1998. This LER involved the failure to properly implement Technical Specification 4.6.1.3.a. |
| | Specifically, procedure Sl.OP-ST.CAN-0004(Q} contained an acceptance value that was greater than allowed by TS. The corrective actions taken relative to this LER were appropriate for the identified root cause of LER 272/96-005-16, but would not have been expected to identify or prevent this event. |
| | SAFETY CONSEQUENCES AND IMPLICATIONS There were no safety consequences associated with this event, and the safety implications of a postulated event were minimal. |
| | Although the containment air lock outer door seals were not being tested, the inner seals were always tested satisfactorily. Therefore, the containment air locks (inner seal) were able to maintain the overall leakage below the required Technical Specification limits. Maintaining the overall leakage below the required Technical Specification limits, ensures that the assumptions used in the dose analysis remain valid. |
| | Additionally, because Unit 1 had been shutdown for over two years, the activity contained within the fuel has been demonstrated by Engineering Evaluation to be much lower than the activity expected when compared with a normal refueling outage. |
| | Based on the above, there was no impact to the health and safety of the public. |
| | NRC FORM 366A (4-95) |
| | |
| | NRC FORM 366A (4-95) |
| | * LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION |
| | * U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 5 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | CORRECTIVE ACTIONS |
| | : 1. The Schrader valve linkage was repaired for both Salem Unit 1 containment air locks, and the leak rate test was performed satisfactorily. |
| | : 2. The Salem Unit 2 airlocks were inspected and found to be working properly. |
| | : 3. Additional corrective actions may be taken, as appropriate, upon completion of the level 2 condition report. |
| | : 4. This event will be incorporated in the 1998 Maintenance Continuing Training for lessons learned. |
| | NRC FORM 366A (4-95)}} |
LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were InspectedML18106A561 |
Person / Time |
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Site: |
Salem |
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Issue date: |
04/20/1998 |
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From: |
Enrique Villar Public Service Enterprise Group |
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To: |
|
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Shared Package |
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ML18106A560 |
List: |
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References |
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LER-98-008, LER-98-8, NUDOCS 9804270107 |
Download: ML18106A561 (5) |
|
Similar Documents at Salem |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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NRC FORM 366 (4-95)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
- APPROVED BY OMB NO. 3150-0104 EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (HI F33), U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON, DC 2055!HI001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUllDER (2) PAGE (3)
SALEM GENERATING STATION UNIT 1 05000272 1of5 TITLE (4)
INADEQUATE TESTING OF THE SALEM UNIT 1 CONTAINMENT AIR LOCKS RESULTED IN ENTERING TECHNICAL SPECIFICATION 3.0.3.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem Generating Station Unit 2 I 05000311 03 23 98 98 08 -- 00 04 98 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE(9) 5 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i) 50. 73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50. 73(a)(2)(ii) 50. 73(a)(2)(x)
LEVEL (10) 0 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50. 73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50. 73(a)(2)(v) Spec~in Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
E. H. Villar, Station Licensing Engineer (609) 339-5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS
~I~li~~~~f~ ~i~ ~i CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS
~i~ ~l ~ ~ l~ ~jlj~lij~fil rm~~i~~~i~~m~~r 1
11111111111111111-SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR SUBMISSION
. IYES (If yes, complete EXPECTED SUBMISSION DATE). x1NO DATE (15)
ABSTRACT (Limitto 1400 spaces, i.e., approximately 15 single-spaced typewritten Imes) (16)
During a periodic performance of Sl.RA-IS.ZZ-OOOl(Q) I "Type B Mechanical Penetration Leak Rate Testing", In-Service inspection personnel noted that the Schrader valve that controls the air supply to the exterior door was not fulfilling its intended function. This condition meant that no air was being supplied to the exterior door seal during the performance of the leak rate test under ,, procedure Sl.OP-ST.CAN-0004 (Q)"Containment Air Lock Local Leak Rate Test. This resulted in a failure to meet the surveillance requirements of Technical Specification 3.6.1.3. for both Unit 1 containment air locks, and Technical Specification 3.0.3 was entered. The most probable cause is attributed to less-than-adequate practices during the replacement of the equalizing valve in accordance with a design change package. Corrective actions taken were to correct the Schrader valve linkage for both Salem Unit 1 containment air locks. The leak rate test was performed satisfactorily, and the Salem Unit 2 airlocks were inspected and found to be working properly.
This condition represents a reportable condition under the provisions of 10CFR50.73 (a) (2) ( i) (B) 9804270107 980420 PDR ADOCK 05000272 S PDR
NRC FORM 366A (4-95)
- LICENSEE EVENT REPORT (LER).
TEXT CONTINUATION
- U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 2 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
PLANT AND SYSTEM IDENTIFICATION Westinghouse - Pressurized Water Reactor Containment Air Lock {NH/AL}*
- Energy Industry Identification System (EIIS) codes and component function identifier codes appear in the text as {SS/CCC}.
IDENTIFICATION OF OCCURRENCE Identification Date: March 23, 1998.
Reportability Date: March 23, 1998.
Report Date: April 22, 1998.
CONDITIONS PRIOR TO OCCURRENCE Unit 1: Mode 5 There were no structures, components, or systems that were inoperable at the start of the event that contributed to the event.
DESCRIPTION OF OCCURRENCE On March 23, 1998, during a periodic performance of Sl.RA-IS.ZZ-OOOl(Q),
"Type B Mechanical Penetration Leak Rate Testing", In-Service Inspection (ISI) personnel noted that the Schrader valve that controls the air supply to the 100 foot elevation exterior containment air lock door was not functioning properly.
The 3-way Schrader valve is a vendor-supplied shutoff valve downstream of isolation valve 1CA1722 (control air isolation valve for the Unit 1 100 foot elevation air lock) . The Schrader valve is engaged by a mechanical arm which is linked to the handwheel for the exterior containment air lock door such that the Schrader valve is open when the exterior containment air lock door is closed. The Schrader valve when engaged by the door interlock mechanism (door full closed) allows control air to be supplied to both containment air lock doors (inner and outer doors) . Specifically, air is supplied to the space between the double seal and the knife edge that presses against them.
NRC FORM 366A (4-95)
NRC FORM 366A (4-95)
- LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION
- U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 3 OF 5 SALEM GENERATING STATION UNIT 1 08 00 98 --
TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE (cont'd)
During the testing of the Unit 1 air locks, ISI personnel identified that:
(1) one of the fasteners on the mechanical linkage was loose, and (2) one of the mechanical arms was bent such that a hard contact with the Schrader valve was not being made when the door was closed. In this condition, the interlock mechanism was not engaging the Schrader valve. Therefore, the outer containment air lock door seal was not being tested during the performance of the leak rate test under procedure Sl.RA-IS.ZZ-OOOl(Q), and the performance of Sl.OP-ST.CAN-0004(Q) ,"Containment Air Lock Local Leak Rate Test." As a result of this condition, the Schrader valve for the 130 foot elevation containment air lock was inspected and a similar condition was identified by ISI personnel.
These conditions resulted in a ~ailure to meet the surveillance requirements of Technical Specification 3.6.1.3. Technical Specification 3.6.1.3 requires each containment air lock to be operable in Modes 1 thro~gh 4. With an inoperable air lock, TS requires that the air lock be restored to operable within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or be in HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Since TS 3.6.1.3 Action does not allow more than one door to be inoperable, on March 23 at approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, the control room operators declared both containment air locks inoperable, and entered Technical Specification 3.0.3. At approximately 1447 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.505835e-4 months <br />, on the same day, repairs to the air locks were performed, the containment air locks were retested satisfactorily in accordance with the provisions of Technical Specifications 4.0.3, and Technical Specifications 3.0.3 was exited.
This condition, however, represents a reportable condition under the provisions of 10CFR50. 73 (a) (2) (i) (B)
APPARENT CAUSE OF OCCURRENCE The most probable root cause is attributed to less-than-adequate work practices during the replacement of the equalizing valve.
The Schrader valve is located inside the airlock in the upper right corner (facing the exterior door). It is directly below the equalizing valve.
The Schrader valve is relatively protected from incidental contact due to normal traffic through the airlock. Therefore, it is highly unlikely that the observed condition could have occurred as a result of incidental contact by personnel while passing through the airlock.
Investigation into this event, however, identified that the equalizing valve had been recently replaced in accordance with Design Change Package (DCP) 1EE00130 and work order 950905417 for both Unit 1 airlocks.
NRC FORM 366A (4-95)
NRC FORM 366A (4-95)
- LICENSEE EVENT REPORT (LER)
- U.S. NUCLEAR REGULATORY COMMISSION TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 4 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
APPARENT CAUSE OF OCCURRENCE (cont'd)
This work was completed just prior Unit 1 entering Mode 4. To replace the equalizing valve, it was necessary to do work on the mechanical linkage. A review of the DCP required testing indicated that a post modification leak rate test was performed satisfactorily using procedure Sl. RA- IS. ZZ-0001 (Q) on both containment air lock doors. Less than adequate work practices appeared to have, over time, resulted in the loosening of the fasteners.
The loosening of the fasteners could have allowed the mechanical arm to be out-of-position such that the arm was slightly bent (in a direction parallel to its motion) when the door was closed.
PREVIOUS OCCURRENCES A review of the LER database for Salem Units 1 and 2 issued in the last two years identified another LER involving containment air locks. Although not a similar occurrence, it is included for completeness of reporting. LER 272/96-005-16 "Inadequate Technical Specification Testing - Containment Airlock Gasket Leakage" was issued on January 21, 1998. This LER involved the failure to properly implement Technical Specification 4.6.1.3.a.
Specifically, procedure Sl.OP-ST.CAN-0004(Q} contained an acceptance value that was greater than allowed by TS. The corrective actions taken relative to this LER were appropriate for the identified root cause of LER 272/96-005-16, but would not have been expected to identify or prevent this event.
SAFETY CONSEQUENCES AND IMPLICATIONS There were no safety consequences associated with this event, and the safety implications of a postulated event were minimal.
Although the containment air lock outer door seals were not being tested, the inner seals were always tested satisfactorily. Therefore, the containment air locks (inner seal) were able to maintain the overall leakage below the required Technical Specification limits. Maintaining the overall leakage below the required Technical Specification limits, ensures that the assumptions used in the dose analysis remain valid.
Additionally, because Unit 1 had been shutdown for over two years, the activity contained within the fuel has been demonstrated by Engineering Evaluation to be much lower than the activity expected when compared with a normal refueling outage.
Based on the above, there was no impact to the health and safety of the public.
NRC FORM 366A (4-95)
NRC FORM 366A (4-95)
- LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION
- U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) 05000272 YEAR I SEQUENTIAL NUMBER IREVISION NUMBER 5 OF 5 SALEM GENERATING STATION UNIT 1 98 -- 08 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
CORRECTIVE ACTIONS
- 1. The Schrader valve linkage was repaired for both Salem Unit 1 containment air locks, and the leak rate test was performed satisfactorily.
- 2. The Salem Unit 2 airlocks were inspected and found to be working properly.
- 3. Additional corrective actions may be taken, as appropriate, upon completion of the level 2 condition report.
- 4. This event will be incorporated in the 1998 Maintenance Continuing Training for lessons learned.
NRC FORM 366A (4-95)