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| | issue date = 01/04/1994 | | | issue date = 01/04/1994 |
| | title = LER 93-019-00:on 931203,TS Action Statement Entered Due to Waste Gas Holdup Sys Oxygen Concentration Being Greater than 2% for More than 48 H.Oxygen Concentration within Waste Gas Sys Reduced to Less than 2% on 931212.W/940104 Ltr | | | title = LER 93-019-00:on 931203,TS Action Statement Entered Due to Waste Gas Holdup Sys Oxygen Concentration Being Greater than 2% for More than 48 H.Oxygen Concentration within Waste Gas Sys Reduced to Less than 2% on 931212.W/940104 Ltr |
| | author name = PASTVA M J, VONDRA C A | | | author name = Pastva M, Vondra C |
| | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY |
| | addressee name = | | | addressee name = |
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| =Text= | | =Text= |
| {{#Wiki_filter:.. . e PStiG *Public Service Electric arid Gas Company *P.O. Box 236 | | {{#Wiki_filter:.. . e PStiG |
| * Hancocks Bridge: New Jersey 08038 * . Salem Generating Station u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555. | | *Public Service Electric arid Gas Company *P.O. Box 236 |
| | * Hancocks Bridge: New Jersey 08038 * |
| | . Salem Generating Station January 4, 199'} t./ |
| | : u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555. |
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| ==Dear Sir:== | | ==Dear Sir:== |
| | |
| SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT*93-019-0b. | | SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT*93-019-0b. |
| January 4, 199'} t./ This Licensee Event Report is being submitted pursuant to the . requirements of Code of Federal Regulation lOCFR50.73(a)
| | This Licensee Event Report is being submitted pursuant to the . |
| (2) (i)(B). This report is required to be issued within thirty (30) days of event discovery. | | requirements of Code of Federal Regulation 10CFR50.73(a) (2) (i)(B). |
| MJPJ:pc Distribution 9401310028 940104 PDR ADOCK 05000272 S PDR TherxJ'i\'cr is 11; your hands. l Sincerely yours, i ' I . 95*2189 REV 7-92 l NRC FORM-366 (6-891 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 | | This report is required to be issued within thirty (30) days of event discovery. |
| .. LICENSEE EVENT REPORT (LERI EXPIRES: 4/30/92 .ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT-BRANCH (P-530). U.S. NUCLEAR REGULATORY COMMISSION. | | Sincerely yours, MJPJ:pc Distribution 9401310028 940104 ~* |
| WASHINGTON. | | PDR ADOCK 05000272 S PDR l i I |
| DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT 13150-01041, OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC :20503. FACILITY NAME (11 I DOCKET NUMBER 121 I PAGE 131 Salem Generating Station--Unit 1 o 15IoIoIo12 I 712 1 loF 0 14 TITLE (41 Waste Gas Holdup System Oxygen Concentration Greater Than :z% For More Than 48 Hours. EVENT DATE (51 MONTH DAY ii 2 ol 5 OPERATING MODE (91 YEAR 9 3 5 0 0 LER NUMBER 161 REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl YEAR \?? SEQUENTIAL it\ REVlSION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER o1s1010101 I 913 -ol 1 19 -o lo 0I1 ol4 9[ 4 0 1 5 IO J.O I O I I THIS REPORT IS SUBMITTED PURSUANT TO THE OF 10 CFR §: (Ch*_ck ono or moro of th* fo/low;ngJ 1111 20.402(bl 20.405lcl 60.73l*ll2Hivl 73.71lbl -,_ ,___ 20.405(o)(1llil | | TherxJ'i\'cr is 11; your hands. |
| ..__;_ 50.36(cll1l 60.73_(*11211*1 73.71 lcl -,___ ,___
| | . 95*2189 REV 7-92 |
| 50.36lcll21 60.7311l121(vii) | | |
| OTHER !Specify in Absrrocl I I .-.--,___ -btJ/ow tJnd in T1Jxt, NRC Form ' ,,,. 20.4051o)(1 lliiil x 50.731*ll2llil 50.7311H2llviiil!AI | | l NRC FORM-366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 (6-891 |
| -366AJ -;-.-. """* ....... -,___ 50.7311)(2)(iil 60.7311l12)(viiillBl
| | . EXPIRES: 4/30/92 |
| ,___ ,___ 50.7311)(2)(iiil 60.7311l12llxl
| | .ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT- BRANCH (P-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT 13150-01041, OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC :20503. |
| [''"\"'"?''\'")""\{"-")"(){)"")""{)J--J 20.40511)(1 | | FACILITY NAME (11 DOCKET NUMBER 121 I PAGE 131 Salem Generating Station-- Unit 1 TITLE (41 Io 15IoIoIo12 I 712 1 loF 0 14 Waste Gas Holdup System Oxygen Concentration Greater Than :z% For More Than 48 Hours. |
| )(iv)* ['}:(\: ::::::.:-: | | EVENT DATE (51 LER NUMBER 161 REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR |
| .; .. ,., "" 20.40511ll111vl | | \?? SEQUENTIAL NUMBER it\ REVlSION NUMBER MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI o1s1010101 I I ii 2 ol 5 9 3 913 - ol 1 19 - o lo 0I1 ol4 9[ 4 0 1 5 IO J.O I O I I I THIS REPORT IS SUBMITTED PURSUANT TO THE R~OUIREMENTS OF 10 CFR §: (Ch*_ck ono or moro of th* fo/low;ngJ 1111 OPERATING MODE (91 5 20.402(bl 20.405lcl ,_ 60.73l*ll2Hivl ,___ 73.71lbl 20.405(o)(1llil 50.36(cll1l 60.73_(*11211*1 73.71 lcl 0 0 2~.40511)(1)(iil 50.36lcll21 |
| ,* .... *' '...... ,* :* ,* .* ,* ,*: .. ' ;* ;* LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. J. Pastva, Jr. -LER.Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN *THIS REPORT 1131 :*:* :*:-:**:*::*:*:.; | | ,___ 60.7311l121(vii) OTHER !Specify in Absrrocl |
| .. ;.;.;.::*:-:*:*:*
| | .-.- - x btJ/ow tJnd in T1Jxt, NRC Form |
| CAUSE SYSTEM COMPONENT i:::: "\: :::::,:Y::?:F CAUSE SYSTEM COMPONENT
| | [''"\"'"?''\'")""\{"-")"(){)"")""{)J--J |
| :-:* *:*:*:*: :-:* :-:* :-:-*:*: :-:-::: :-:* -:-: I I I I I I I :-:* :-:* -:-: I I I I *:*: }: :} :::::::r ;::: -:-:-:::::;:;::;::-:*
| | ,,,. 20.4051o)(1 lliiil 20.40511)(1 )(iv)* |
| -:-:-:*:* | | -,___ 50.731*ll2llil 50.7311)(2)(iil 50.7311H2llviiil!AI 60.7311l12)(viiillBl |
| I I I I I I I -:-:::;:;::: | | ' - 366AJ |
| :-:*::::::::::;:.,., *:*:* I I I I SUPPLEMENTAL REPORT EXPECTED 1141 (If v*s. comp/*<* EXPECTED SUBMISSION DATE! ABSTRACT (Umii to 1400 spaces, i.ll., approximately fifrsen single-space rvpewrirren lines) (16) TURER I I I I I I EXPECTED SUBMISSION DATE 1151 MONTH DAY YEAR I I I oxygen (0 2) concentration within the waste Gas Holdup System was > 2% for > 48 hours. On 12/3/93, at 0910 hours, Technical Specification (TS) Action Statement 3.11.2.5.a.
| | ['}:(\: ::::::.:-: .; .. ,., "" 20.40511ll111vl 50.7311)(2)(iiil 60.7311l12llxl |
| was entered due to o 2 concentration of | | ,* .... ~* *' '...... ,* :* ,* .* ,* ~.; ,*:..' ;* ;* |
| * 2.17% by volume in 13 Waste Gas Decay Tank (WGDT). Efforts to reduce the concentration to < 2% were implemented | | LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. J. Pastva, Jr. - LER.Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN *THIS REPORT 1131 CAUSE SYSTEM COMPONENT M~~~~~C- R~6°~~:g;E i:::: "\: :::::,:Y::?:F CAUSE SYSTEM COMPONENT |
| .. -o 2 concentrations above were subsequently measured in other WGDTs; 3.04% in 11 WGDT on 12/8/93, .3.11% in 14 WGDT on 12/8/93, and 3.29% in 12 WGDT on 12/9/93. _The maximum o 2 concentration was 4.25% in 13 WGDT on 12/4/93. The root cause is attributed to "Design, Manufacturing, Construction/ | | 'MANUFAC-TURER I I I I I I I *:*: I I I I I I I |
| Installation", as per NUREG-1022. | | :::::::r |
| The source of the o is attributed to routine refueling/ | | }: :}:-:-:::::;:;::;::-:* -:-:-:*:* |
| maintenance outage fn addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were performed requiring these systems be opened. Prior to closure, steps were performed to purge these systems with nitrogen *. However, the design of these systems does not lend itself to effective purging. Furthermore, the calibration of the Waste Gas Analyzer introduced additional o 2 into the system. This was further due to the fact that the online o 2 analyzer was out of service for replacement. | | I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED |
| | ~NO SUBMISSION DATE 1151 |
| | ~YES (If v*s. comp/*<* EXPECTED SUBMISSION DATE! |
| | I I I ABSTRACT (Umii to 1400 spaces, i.ll., approximately fifrsen single-space rvpewrirren lines) (16) oxygen (0 2 ) concentration within the waste Gas Holdup System was > 2% |
| | for > 48 hours. On 12/3/93, at 0910 hours, Technical Specification (TS) |
| | Action Statement 3.11.2.5.a. was entered due to o 2 concentration of |
| | * 2.17% by volume in 13 Waste Gas Decay Tank (WGDT). Efforts to reduce the o~ concentration to < 2% were implemented ..- o 2 concentrations above 2~ were subsequently measured in other WGDTs; 3.04% in 11 WGDT on 12/8/93, .3.11% in 14 WGDT on 12/8/93, and 3.29% in 12 WGDT on 12/9/93. |
| | _The maximum o 2 concentration was 4.25% in 13 WGDT on 12/4/93. The root cause is attributed to "Design, Manufacturing, Construction/ |
| | Installation", as per NUREG-1022. The source of the o is attributed to routine refueling/ maintenance outage activities~ fn addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were performed requiring these systems be opened. Prior to closure, steps were performed to purge these systems with nitrogen *. However, the design of these systems does not lend itself to effective purging. |
| | Furthermore, the calibration of the Waste Gas Analyzer introduced additional o 2 into the system. This was further complicate~ due to the fact that the online o 2 analyzer was out of service for replacement. |
| o 2 concentration within the Waste Gas System was reduced to < 2% on 12/12/93, at 0408 hours, at which time the TS Action Statement was exited. Lessons learned from this event will be incorporated into future planning regarding Waste Gas System modifications. | | o 2 concentration within the Waste Gas System was reduced to < 2% on 12/12/93, at 0408 hours, at which time the TS Action Statement was exited. Lessons learned from this event will be incorporated into future planning regarding Waste Gas System modifications. |
| NRC Form 366 (6-891 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1. DOCKET NUMBER 5000272 PLANT AND SYSTEM IDENTIFICATION: | | NRC Form 366 (6-891 |
| Westinghouse | | |
| -Pressurized Water Reactor LER NUMBER 93-019..:00 PAGE 2 of 4 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE: | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1. 5000272 93-019..:00 2 of 4 PLANT AND SYSTEM IDENTIFICATION: |
| | Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx} |
| | IDENTIFICATION OF OCCURRENCE: |
| Waste Gas Holdup System Oxygen Concentration Greater Than 2% For More Than 48 Hours | | Waste Gas Holdup System Oxygen Concentration Greater Than 2% For More Than 48 Hours |
| * Event Date: 12/5/93 Report Date: 1/4/94 This report was initiated by Incident Report No. 93-494. CONDITIONS PRIOR TO OCCURRENCE: | | * Event Date: 12/5/93 Report Date: 1/4/94 This report was initiated by Incident Report No. 93-494. |
| | CONDITIONS PRIOR TO OCCURRENCE: |
| Mode 5; 11th refueling/maintenance outage in progress; Reactor core reload complete DESCRIPTION OF OCCURRENCE: | | Mode 5; 11th refueling/maintenance outage in progress; Reactor core reload complete DESCRIPTION OF OCCURRENCE: |
| Oxygen concentration within the Waste Gas Holdup System {WE} was greater than 2% for more than 48 hours, which exceeded Technical Specification (TS) Action Statement 3.11.2.5.a. | | Oxygen concentration within the Waste Gas Holdup System {WE} was greater than 2% for more than 48 hours, which exceeded Technical Specification (TS) Action Statement 3.11.2.5.a. |
| On December 3, 1993, at 0910 hours,' TS .Action Statement 3-.11.2.5.a. | | On December 3, 1993, at 0910 hours,' TS .Action Statement 3-.11.2.5.a. |
| was entered due to oxygen concentration of 2.17% by volume as measured in 13 Waste* Gas Decay Tank (WGDT). Efforts to reduce the oxygen concentrat:ion to< 2% were implementtad. | | was entered due to oxygen concentration of 2.17% by volume as measured in 13 Waste* Gas Decay Tank (WGDT). Efforts to reduce the oxygen concentrat:ion to< 2% were implementtad. oxygen concentrations above* |
| oxygen concentrations above* 2% were subsequently measured in other WGDTs; 3.04% in 11 WGDT on December 8, 3.11% in 14 WGDT on December 8, and 3.29% in 12 WGDT on December 9. The maximum measured concentration was 4.25% in 13 WGDT on December 4. Oxygen.concentration within the Waste Gas Holdup System was reduced to less than 2% on December 12, 1993 at 0408 hours, at which time the TS -Action Statement was exited. ANALYSIS OF OCCURRENCE: | | 2% were subsequently measured in other WGDTs; 3.04% in 11 WGDT on December 8, 3.11% in 14 WGDT on December 8, and 3.29% in 12 WGDT on December 9. The maximum measured concentration was 4.25% in 13 WGDT on December 4. Oxygen.concentration within the Waste Gas Holdup System was reduced to less than 2% on December 12, 1993 at 0408 hours, at which time the TS -Action Statement was exited. |
| There is an increased probability of oxygen concentration greater than 2% within the Waste Gas Holdup System after a refueling/maintenance outage. oxygen may enter the Waste Gas Holdup System via the eves Holdup Tanks, the Reactor Coolant Drain Tank, the Pressurizer Relief Tank, and the Volume Control Tank (VCT). The valves which provide direct flow to the Waste Gas Header when these tanks are opened to the LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station Unit 1 DOCKET NUMBER 5000272 ANALYSIS OF OCCURRENCE: (cont'd) LER NUMBER 93-019-00 PAGE 3 of 4 ambient atmosphere are required to be closed. In addition, extensive modifications to the Waste Gas Analyzer and the Waste Gas System were performed.* | | ANALYSIS OF OCCURRENCE: |
| | There is an increased probability of oxygen concentration greater than 2% within the Waste Gas Holdup System after a refueling/maintenance outage. oxygen may enter the Waste Gas Holdup System via the eves Holdup Tanks, the Reactor Coolant Drain Tank, the Pressurizer Relief Tank, and the Volume Control Tank (VCT). The valves which provide direct flow to the Waste Gas Header when these tanks are opened to the |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-019-00 3 of 4 ANALYSIS OF OCCURRENCE: (cont'd) ambient atmosphere are required to be closed. In addition, extensive modifications to the Waste Gas Analyzer and the Waste Gas System were performed.* |
| APPARENT CAUSE OF OCCURRENCE: | | APPARENT CAUSE OF OCCURRENCE: |
| The root cause is attributed to "Design, Manufacturing, Construction/Installation", as per NUREG-1022. | | The root cause is attributed to "Design, Manufacturing, Construction/Installation", as per NUREG-1022. The source of the oxygen is attributed to routine refueling/ maintenance outage . |
| The source of the oxygen is attributed to routine refueling/ | | activities. In addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were* performed requiring th*ese systems be opened~ Prior to closure, steps were performed to purge the_se systems with nitrogen. However, the design of these systems does not lend itself to effective purging. Furthermore, the calibrat~on of the Waste Gas Analyzer introduced additional oxygen into the system. This situation was further complicated due to the fact that the online oxygen analyzer was out of service for replacement. |
| maintenance outage . activities. | |
| In addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were* performed requiring th*ese systems be Prior to closure, steps were performed to purge the_se systems with nitrogen. | |
| However, the design of these systems does not lend itself to effective purging. Furthermore, the of the Waste Gas Analyzer introduced additional oxygen into the system. This situation was further complicated due to the fact that the online oxygen analyzer was out of service for replacement. | |
| PREVIOUS SIMILAR OCCURRENCES: | | PREVIOUS SIMILAR OCCURRENCES: |
| LER 272/87-019-00 reported a similar event in the Waste Gas System. Corrective actions to the 1987 event have been effective for normal . refueling/maintenance outage activities. | | LER 272/87-019-00 reported a similar event in the Waste Gas System. |
| SAFETY SIGNIFICANCE This event is reportable in accordance with lOCFR 50.73(a) (2) (i) (B), since TS Action statement 3.11.2.5.a was not met. This event did not affect the health or safety of the public. The concern for oxygen within the Waste Gas Holdup System is due to the presence of hydrogen gas within the system*. In sufficient quantities, hydrogen in the presence of oxygen can be explosive. | | Corrective actions to the 1987 event have been effective for normal . |
| The TS level of not greater than 2% oxygen is conservatively low, ensuring that this explosive hazard is not present. Monitoring of the oxygen concentration in accordance with TS ensures that if the concentration increases above the 2% limitation, expeditious corrective action can* be taken to lower the level to below 2%. During this event the highest-measured hydrogen concentration was 1.51%, therefore potential for an explosive mixture of hydrogen and oxygen in the Waste Gas Holdup system did not exist. CORRECTIVE ACTION: oxygen concentration within the Waste Gas system was reduced to less than 2% on December 12, 1993 at 0408 hours, at.which time the TS Action Statement was exited. | | refueling/maintenance outage activities. |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000272 LER NUMBER 93-019-00 PAGE 4 of 4 Lessons learned from this event will be incorporated into future planning regarding Waste Gas System MJPJ:pc SORC Mtg. 94-001 eneral Manager -Salem Operations}} | | SAFETY SIGNIFICANCE This event is reportable in accordance with 10CFR 50.73(a) (2) (i) (B), |
| | since TS Action statement 3.11.2.5.a was not met. |
| | This event did not affect the health or safety of the public. The concern for oxygen within the Waste Gas Holdup System is due to the presence of hydrogen gas within the system*. In sufficient quantities, hydrogen in the presence of oxygen can be explosive. The TS level of not greater than 2% oxygen is conservatively low, ensuring that this explosive hazard is not present. Monitoring of the oxygen concentration in accordance with TS ensures that if the concentration increases above the 2% limitation, expeditious corrective action can* |
| | be taken to lower the level to below 2%. During this event the highest-measured hydrogen concentration was 1.51%, therefore potential for an explosive mixture of hydrogen and oxygen in the Waste Gas Holdup system did not exist. |
| | CORRECTIVE ACTION: |
| | oxygen concentration within the Waste Gas system was reduced to less than 2% on December 12, 1993 at 0408 hours, at.which time the TS Action Statement was exited. |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-019-00 4 of 4 CORRECTIVE ACTION: (cont'd) |
| | Lessons learned from this event will be incorporated into future planning regarding Waste Gas System modi:j:~ |
| | eneral Manager - |
| | Salem Operations MJPJ:pc SORC Mtg. 94-001}} |
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Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
.. . e PStiG
- Public Service Electric arid Gas Company *P.O. Box 236
. Salem Generating Station January 4, 199'} t./
- u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555.
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT*93-019-0b.
This Licensee Event Report is being submitted pursuant to the .
requirements of Code of Federal Regulation 10CFR50.73(a) (2) (i)(B).
This report is required to be issued within thirty (30) days of event discovery.
Sincerely yours, MJPJ:pc Distribution 9401310028 940104 ~*
PDR ADOCK 05000272 S PDR l i I
TherxJ'i\'cr is 11; your hands.
. 95*2189 REV 7-92
l NRC FORM-366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 (6-891
. EXPIRES: 4/30/92
.ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT- BRANCH (P-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT 13150-01041, OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC :20503.
FACILITY NAME (11 DOCKET NUMBER 121 I PAGE 131 Salem Generating Station-- Unit 1 TITLE (41 Io 15IoIoIo12 I 712 1 loF 0 14 Waste Gas Holdup System Oxygen Concentration Greater Than :z% For More Than 48 Hours.
EVENT DATE (51 LER NUMBER 161 REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR
\?? SEQUENTIAL NUMBER it\ REVlSION NUMBER MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI o1s1010101 I I ii 2 ol 5 9 3 913 - ol 1 19 - o lo 0I1 ol4 9[ 4 0 1 5 IO J.O I O I I I THIS REPORT IS SUBMITTED PURSUANT TO THE R~OUIREMENTS OF 10 CFR §: (Ch*_ck ono or moro of th* fo/low;ngJ 1111 OPERATING MODE (91 5 20.402(bl 20.405lcl ,_ 60.73l*ll2Hivl ,___ 73.71lbl 20.405(o)(1llil 50.36(cll1l 60.73_(*11211*1 73.71 lcl 0 0 2~.40511)(1)(iil 50.36lcll21
,___ 60.7311l121(vii) OTHER !Specify in Absrrocl
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LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. J. Pastva, Jr. - LER.Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN *THIS REPORT 1131 CAUSE SYSTEM COMPONENT M~~~~~C- R~6°~~:g;E i:::: "\: :::::,:Y::?:F CAUSE SYSTEM COMPONENT
'MANUFAC-TURER I I I I I I I *:*: I I I I I I I
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I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED
~NO SUBMISSION DATE 1151
~YES (If v*s. comp/*<* EXPECTED SUBMISSION DATE!
I I I ABSTRACT (Umii to 1400 spaces, i.ll., approximately fifrsen single-space rvpewrirren lines) (16) oxygen (0 2 ) concentration within the waste Gas Holdup System was > 2%
for > 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. On 12/3/93, at 0910 hours0.0105 days <br />0.253 hours <br />0.0015 weeks <br />3.46255e-4 months <br />, Technical Specification (TS)
Action Statement 3.11.2.5.a. was entered due to o 2 concentration of
- 2.17% by volume in 13 Waste Gas Decay Tank (WGDT). Efforts to reduce the o~ concentration to < 2% were implemented ..- o 2 concentrations above 2~ were subsequently measured in other WGDTs; 3.04% in 11 WGDT on 12/8/93, .3.11% in 14 WGDT on 12/8/93, and 3.29% in 12 WGDT on 12/9/93.
_The maximum o 2 concentration was 4.25% in 13 WGDT on 12/4/93. The root cause is attributed to "Design, Manufacturing, Construction/
Installation", as per NUREG-1022. The source of the o is attributed to routine refueling/ maintenance outage activities~ fn addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were performed requiring these systems be opened. Prior to closure, steps were performed to purge these systems with nitrogen *. However, the design of these systems does not lend itself to effective purging.
Furthermore, the calibration of the Waste Gas Analyzer introduced additional o 2 into the system. This was further complicate~ due to the fact that the online o 2 analyzer was out of service for replacement.
o 2 concentration within the Waste Gas System was reduced to < 2% on 12/12/93, at 0408 hours0.00472 days <br />0.113 hours <br />6.746032e-4 weeks <br />1.55244e-4 months <br />, at which time the TS Action Statement was exited. Lessons learned from this event will be incorporated into future planning regarding Waste Gas System modifications.
NRC Form 366 (6-891
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1. 5000272 93-019..:00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
Waste Gas Holdup System Oxygen Concentration Greater Than 2% For More Than 48 Hours
- Event Date: 12/5/93 Report Date: 1/4/94 This report was initiated by Incident Report No.93-494.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 5; 11th refueling/maintenance outage in progress; Reactor core reload complete DESCRIPTION OF OCCURRENCE:
Oxygen concentration within the Waste Gas Holdup System {WE} was greater than 2% for more than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, which exceeded Technical Specification (TS) Action Statement 3.11.2.5.a.
On December 3, 1993, at 0910 hours0.0105 days <br />0.253 hours <br />0.0015 weeks <br />3.46255e-4 months <br />,' TS .Action Statement 3-.11.2.5.a.
was entered due to oxygen concentration of 2.17% by volume as measured in 13 Waste* Gas Decay Tank (WGDT). Efforts to reduce the oxygen concentrat:ion to< 2% were implementtad. oxygen concentrations above*
2% were subsequently measured in other WGDTs; 3.04% in 11 WGDT on December 8, 3.11% in 14 WGDT on December 8, and 3.29% in 12 WGDT on December 9. The maximum measured concentration was 4.25% in 13 WGDT on December 4. Oxygen.concentration within the Waste Gas Holdup System was reduced to less than 2% on December 12, 1993 at 0408 hours0.00472 days <br />0.113 hours <br />6.746032e-4 weeks <br />1.55244e-4 months <br />, at which time the TS -Action Statement was exited.
ANALYSIS OF OCCURRENCE:
There is an increased probability of oxygen concentration greater than 2% within the Waste Gas Holdup System after a refueling/maintenance outage. oxygen may enter the Waste Gas Holdup System via the eves Holdup Tanks, the Reactor Coolant Drain Tank, the Pressurizer Relief Tank, and the Volume Control Tank (VCT). The valves which provide direct flow to the Waste Gas Header when these tanks are opened to the
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-019-00 3 of 4 ANALYSIS OF OCCURRENCE: (cont'd) ambient atmosphere are required to be closed. In addition, extensive modifications to the Waste Gas Analyzer and the Waste Gas System were performed.*
APPARENT CAUSE OF OCCURRENCE:
The root cause is attributed to "Design, Manufacturing, Construction/Installation", as per NUREG-1022. The source of the oxygen is attributed to routine refueling/ maintenance outage .
activities. In addition, extensive modifications to the Waste Gas Analyzer and Waste Gas System were* performed requiring th*ese systems be opened~ Prior to closure, steps were performed to purge the_se systems with nitrogen. However, the design of these systems does not lend itself to effective purging. Furthermore, the calibrat~on of the Waste Gas Analyzer introduced additional oxygen into the system. This situation was further complicated due to the fact that the online oxygen analyzer was out of service for replacement.
PREVIOUS SIMILAR OCCURRENCES:
LER 272/87-019-00 reported a similar event in the Waste Gas System.
Corrective actions to the 1987 event have been effective for normal .
refueling/maintenance outage activities.
SAFETY SIGNIFICANCE This event is reportable in accordance with 10CFR 50.73(a) (2) (i) (B),
since TS Action statement 3.11.2.5.a was not met.
This event did not affect the health or safety of the public. The concern for oxygen within the Waste Gas Holdup System is due to the presence of hydrogen gas within the system*. In sufficient quantities, hydrogen in the presence of oxygen can be explosive. The TS level of not greater than 2% oxygen is conservatively low, ensuring that this explosive hazard is not present. Monitoring of the oxygen concentration in accordance with TS ensures that if the concentration increases above the 2% limitation, expeditious corrective action can*
be taken to lower the level to below 2%. During this event the highest-measured hydrogen concentration was 1.51%, therefore potential for an explosive mixture of hydrogen and oxygen in the Waste Gas Holdup system did not exist.
CORRECTIVE ACTION:
oxygen concentration within the Waste Gas system was reduced to less than 2% on December 12, 1993 at 0408 hours0.00472 days <br />0.113 hours <br />6.746032e-4 weeks <br />1.55244e-4 months <br />, at.which time the TS Action Statement was exited.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-019-00 4 of 4 CORRECTIVE ACTION: (cont'd)
Lessons learned from this event will be incorporated into future planning regarding Waste Gas System modi:j:~
eneral Manager -
Salem Operations MJPJ:pc SORC Mtg.94-001