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| Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 | | * Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station October 12, 1994 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
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| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 94-010-00 October 12, 1994 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a) | | |
| (2) (i) (A). Issuance of this report is required within thirty (30} days of event discovery. | | SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 94-010-00 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a) (2) (i) (A). |
| MJPJ:pc Distribution | | Issuance of this report is required within thirty (30} days of event discovery. |
| ':: ;_'-J ['" ,,... :... :1:1_; "* '-' 9410250120 941012 PDR ADOCK 05000311 S PDR The power is in your hanis. Sincerely yours, -1£11';, y 95-2189 REV I I NRC FORM 366 .:::.. NUCLEAR REGULATORY COMMISSION | | Sincerely yours, MJPJ:pc Distribution |
| *' APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT {LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF (See reverse for required number of digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) DOCKET NUMBER (2) II PAGE (3) Salem Generating Station Unit 2 05000311 1 Of()4 TITLE (4) Controlled Reactor Shutdown uue To :n Centri:tugal Charging Pump Inoperable Greater Than 72 Hours EVENT DATE (5) LER NUMBER (6 REPORT NUMBER (7) OTHER FACILITIES INVOLVED 18\ REVISION FACILITY NAME DOCKET NUMBER SEQUENTIAL MONTH DAY YEAR MONTH DAY YEAR YEAR NUMBER NUMBER 05000 FACILITY NAME DOCKET NUMBER 09 22 94 94 --010 --00 10 12 94 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more (11\ MODE (9) 1 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) POWER 20.405(a)(1 | | ':: ;_'- J ~ ['" ,,... '~ |
| )(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71 (c) LEVEL (10) 100% 20.405(a) | | :... :1:1_; ~ "* '-' |
| (1) (ii) 50.36(c)(2) 50.73(a) (2) (vii) OTHER -20.405(a) | | 9410250120 941012 PDR ADOCK 05000311 S PDR The power is in your hanis. -1£11' y |
| (1) (iii) x 50. 73 (a)(2)(i) | | 95-2189 REV -92 |
| * 50.73(a) (2) (viii) (A) (Specify in Abstract below and in Text, NRC 20.405(a) | | |
| (1) (iv) 50.73(a)(2)(ii) 50.73(a) (2) (viii) (B) Form 366A) 20.405(a)(1 | | I NRC FORM 366 .:::.. NUCLEAR REGULATORY COMMISSION *' APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT {LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF (See reverse for required number of digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. |
| )(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) | | FACILITY NAME (1) DOCKET NUMBER (2) |
| LICENSEE CONTACT FOR THIS LEA {12) NAME TELEPHONE NUMBER (Include Area Code) M. J. Pastva, Jr*' Licensee Event Reuort Coordinator 609-339-5165 CAUSE SYSTEM COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) | | II PAGE (3) |
| """'"°'""' | | Salem Generating Station Unit 2 05000311 1 Of()4 TITLE (4) Controlled Reactor Shutdown uue To :n Centri:tugal Charging Pump Inoperable Greater Than 72 Hours EVENT DATE (5) LER NUMBER (6 REPORT NUMBER (7) OTHER FACILITIES INVOLVED 18\ |
| ';;;",';':,"° | | FACILITY NAME DOCKET NUMBER SEQUENTIAL REVISION MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000 FACILITY NAME DOCKET NUMBER 09 22 94 94 -- 010 -- 00 10 12 05000 94 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more (11\ |
| * | | MODE (9) 1 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) |
| "'""" | | POWER 20.405(a)(1 )(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71 (c) |
| REPORTABLE TO NPRDS x BO SC N402 N llJliilll SUPPLEMENTAL REPORT EXPECTED 114) EXPECTED MONTH DAY YEAR I YES SUBMISSION X (If yes, complete EXPECTED SUBMISSION DATE) NO DATE (15) 01 31 95 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced tfPewritten lines) (16) At 0108 hours, on 9/19/94, 21 Cen rifugal Charging Pump (CCP} was removed from service for scheduled preventive maintenance. | | LEVEL (10) 100% 20.405(a) (1) (ii) 50.36(c)(2) 50.73(a) (2) (vii) OTHER 20.405(a) (1) (iii) x 50. 73 (a)(2)(i) *50.73(a) (2) (viii) (A) (Specify in Abstract below and in Text, NRC 20.405(a) (1) (iv) 50.73(a)(2)(ii) 50.73(a) (2) (viii) (B) Form 366A) 20.405(a)(1 )(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) |
| | LICENSEE CONTACT FOR THIS LEA {12) |
| | NAME TELEPHONE NUMBER (Include Area Code) |
| | M. J. Pastva, Jr*' Licensee Event Reuort Coordinator 609-339-5165 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | CAUSE SYSTEM |
| | ~~~* """'"°'""' ';;;",';':,"° * ~"'° "'""" ffiM~"ITT """'"°'"~ REPORTABLE TO NPRDS x |
| | llJliilll BO SC N402 N I SUPPLEMENTAL REPORT EXPECTED 114) EXPECTED MONTH DAY YEAR YES SUBMISSION NO X (If yes, complete EXPECTED SUBMISSION DATE) DATE (15) 01 31 95 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced tfPewritten lines) (16) |
| | At 0108 hours, on 9/19/94, 21 Cen rifugal Charging Pump (CCP} was removed from service for scheduled preventive maintenance. |
| Post-maintenance testing results satisfied ASME operability criteria. | | Post-maintenance testing results satisfied ASME operability criteria. |
| Increased axial vibration readings in 21CCP speed increaser were measured however, the vibration was not felt to impact pump operability and it was returned to service, at 2100 hours on 9/21/94. Additional vibration readings showed unstable and increasing speed increaser vibration and at approximately 0100 hours, on 9/22/94, 21CCP was declared inoperable (effective from prior removal from service on 9/19/94). | | Increased axial vibration readings in 21CCP speed increaser were measured however, the vibration was not felt to impact pump operability and it was returned to service, at 2100 hours on 9/21/94. |
| At 0108 hours (same day) the Technical Specification (TS) action time expired and at 1222 hours (same day) the Unit was placed in MODE 4 (HOT SHUTDOWN). | | Additional vibration readings showed unstable and increasing speed increaser vibration and at approximately 0100 hours, on 9/22/94, 21CCP was declared inoperable (effective from prior removal from service on 9/19/94). At 0108 hours (same day) the Technical Specification (TS) action time expired and at 1222 hours (same day) the Unit was placed in MODE 4 (HOT SHUTDOWN). Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No. |
| Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No. SU-1023-SX, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence. | | SU-1023-SX, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence. The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours on 9/25/94, the TS action was exited. It is anticipated that by 1/31/95 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration. |
| The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours on 9/25/94, the TS action was exited. It is anticipated that by 1/31/95 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration. | |
| NRC FORM 366 (5-92) | | NRC FORM 366 (5-92) |
| BLOCK NUMBER 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15
| | |
| * REQUIRED NUMBER OF DIGITS/CHARACTERS FOR EACH BLOCK NUMBER OF DIGITS/CHARACTERS TITLE UP TO 46 FACILITY NAME 8 TOTAL 3 IN ADDITION TO 05000 DOCKET NUMBER VARIES PAGE NUMBER UP TO 76 TITLE 6 TOTAL 2 PER BLOCK EVENT DATE 7 TOTAL 2 FOR YEAR 3 FOR SEQUENTIAL NUMBER LER NUMBER 2 FOR REVISION NUMBER 6 TOTAL 2 PER BLOCK REPORT DATE UP TO 18 FACILITY NAME 8 TOTAL--DOCKET NUMBER OTHER FACILITIES INVOLVED 3 IN ADDITION TO 05000 1 OPERATING MODE 3 POWER LEVEL 1 CHECK BOX THAT APPLIES REQUIREMENTS OF 10 CFR UP TO 50 FOR NAME 14 FOR TELEPHONE LICENSEE CONTACT CAUSE VARIES 2 FOR SYSTEM 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES 1 CHECK BOX THAT APPLIES SUPPLEMENTAL REPORT EXPECTED 6 TOTAL 2 PER BLOCK EXPECTED SUBMISSION DATE *l | | *l REQUIRED NUMBER OF DIGITS/CHARACTERS FOR EACH BLOCK BLOCK NUMBER OF TITLE NUMBER DIGITS/CHARACTERS 1 UP TO 46 FACILITY NAME 8 TOTAL 2 DOCKET NUMBER 3 IN ADDITION TO 05000 3 VARIES PAGE NUMBER 4 UP TO 76 TITLE 6 TOTAL 5 EVENT DATE 2 PER BLOCK 7 TOTAL 2 FOR YEAR 6 LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 6 TOTAL 7 REPORT DATE 2 PER BLOCK UP TO 18 FACILITY NAME 8 OTHER FACILITIES INVOLVED 8 TOTAL-- DOCKET NUMBER 3 IN ADDITION TO 05000 9 1 OPERATING MODE 10 3 POWER LEVEL 1 |
| * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
| | 11 REQUIREMENTS OF 10 CFR CHECK BOX THAT APPLIES UP TO 50 FOR NAME 12 LICENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES 1 |
| Westinghouse | | 14 SUPPLEMENTAL REPORT EXPECTED CHECK BOX THAT APPLIES 6 TOTAL 15 EXPECTED SUBMISSION DATE 2 PER BLOCK |
| -Pressurized Water Reactor LER NUMBER 94-010-00 PAGE 2 of 4 Energy Industry Identification System (EIIS) and Institute of Electrical and Electronics Engineers (IEEE) Component Function Identifiers codes are identified in the text as {xx/xx} IDENTIFICATION OF OCCURRENCE: | | |
| Controlled Reactor Shutdown Due To 21 Centrifugal Charging Pump Inoperable Greater Than 72 Hours Event Date: 9/22/94 Report Date: 10/12/94 This report was initiated by Incident Report No. 94-271. CONDITIONS PRIOR TO OCCURRENCE: | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION: |
| Mode 1 Reactor Power 100% Unit Load 1080 MWe At 0108 hours on September 19, 1994, 21 Centrifugal Charging Pump (CCP) {BQ/P} was removed from service for scheduled preventive maintenance (PM). One of the activities was to investigate unusual noise from the speed increaser | | Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) and Institute of Electrical and Electronics Engineers (IEEE) Component Function Identifiers codes are identified in the text as {xx/xx} |
| {BQ/P/SC} | | IDENTIFICATION OF OCCURRENCE: |
| during pump operation. | | Controlled Reactor Shutdown Due To 21 Centrifugal Charging Pump Inoperable Greater Than 72 Hours Event Date: 9/22/94 Report Date: 10/12/94 This report was initiated by Incident Report No. 94-271. |
| An adjustment was made to the motor shaft to speed increaser coupling. | | CONDITIONS PRIOR TO OCCURRENCE: |
| Following post-maintenance testing, the pump, motor, and speed increaser vibrations were satisfactory and testing results satisfied ASME criteria for pump operability. | | Mode 1 Reactor Power 100% Unit Load 1080 MWe At 0108 hours on September 19, 1994, 21 Centrifugal Charging Pump (CCP) {BQ/P} was removed from service for scheduled preventive maintenance (PM). One of the activities was to investigate unusual noise from the speed increaser {BQ/P/SC} during pump operation. An adjustment was made to the motor shaft to speed increaser coupling. |
| Increased axial vibration readings were measured in the speed increaser. | | Following post-maintenance testing, the pump, motor, and speed increaser vibrations were satisfactory and testing results satisfied ASME criteria for pump operability. Increased axial vibration readings were measured in the speed increaser. After Engineering review and consultation with the vendor, it was determined that the increased axial vibration did not impact pump operability. The pump was determined to be operable and returned to service, at 2100 hours on September 21, 1994. Additional vibration readings were recommended to verify that the axial vibration remained stable and that the consequences of the coupling adjustment were negligible. |
| After Engineering review and consultation with the vendor, it was determined that the increased axial vibration did not impact pump operability. | |
| The pump was determined to be operable and returned to service, at 2100 hours on September 21, 1994. Additional vibration readings were recommended to verify that the axial vibration remained stable and that the consequences of the coupling adjustment were negligible. | |
| DESCRIPTION OF OCCURRENCE: | | DESCRIPTION OF OCCURRENCE: |
| At 2330 hours (same day), additional vibration readings indicated unstable and increasing axial vibration in the 21CCP speed increaser. | | At 2330 hours (same day), additional vibration readings indicated unstable and increasing axial vibration in the 21CCP speed increaser. This condition challenged pump operability and at approximately 0100 hours, on September 22,1994, it was declared inoperable (effective from prior removal from service on September 19th) . |
| This condition challenged pump operability and at approximately 0100 hours, on September 22,1994, it was declared inoperable (effective from prior removal from service on September 19th) . Insufficient time remained to restore the pump to Operable status | | Insufficient time remained to restore the pump to Operable status |
| * LICENSEE EVENT REPORT (LER} TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 DESCRIPTION OF OCCURRENCE: (cont'd) LER NUMBER 94-010-00 PAGE 3 of 4 prior to expiration of the 72-hour action time of Technical Specification (TS} 3.5.2.a, which occurred at 0108 hours (same day}. At 0230 hours (same day} a controlled shutdown was initiated.
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| At 0300 hours (same day}, the NRC was notified of the initiation of the controlled shutdown, in accordance with lOCFR50.72(b} (i} (A}. At 0509 hours (same day} the Unit was placed in MODE 3 (HOT STANDBY} and, at 1222 hours (same day} was placed in MODE 4 (HOT SHUTDOWN}, as required by TS 3.5.2.a. ANALYSIS OF OCCURRENCE: | | LICENSEE EVENT REPORT (LER} TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 3 of 4 DESCRIPTION OF OCCURRENCE: (cont'd) prior to expiration of the 72-hour action time of Technical Specification (TS} 3.5.2.a, which occurred at 0108 hours (same day}. |
| In MODES 1 through 3, operability of two (2) independent Emergency Core Cooling Systems subsystems ensures sufficient emergency core cooling capability in the event of a Loss-Of-Coolant Accident assuming the loss of one subsystem through any active single failure consideration. | | At 0230 hours (same day} a controlled shutdown was initiated. At 0300 hours (same day}, the NRC was notified of the initiation of the controlled shutdown, in accordance with 10CFR50.72(b} (i} (A}. At 0509 hours (same day} the Unit was placed in MODE 3 (HOT STANDBY} and, at 1222 hours (same day} was placed in MODE 4 (HOT SHUTDOWN}, as required by TS 3.5.2.a. |
| Whenever a single CCP is unavailable, the redundant CCP will provide high head injection flow for the mitigation of any design base accident. | | ANALYSIS OF OCCURRENCE: |
| | In MODES 1 through 3, operability of two (2) independent Emergency Core Cooling Systems subsystems ensures sufficient emergency core cooling capability in the event of a Loss-Of-Coolant Accident assuming the loss of one subsystem through any active single failure consideration. Whenever a single CCP is unavailable, the redundant CCP will provide high head injection flow for the mitigation of any design base accident. |
| APPARENT CAUSE OF OCCURRENCE: | | APPARENT CAUSE OF OCCURRENCE: |
| Upon measuring high vibration in the 21CCP speed increaser it was conservatively determined that the pump was inoperable from when it was previously removed from service on September | | Upon measuring high vibration in the 21CCP speed increaser it was conservatively determined that the pump was inoperable from when it was previously removed from service on September 19. As such, there was insufficient time to restore the pump to Operable status prior to expiration of the action time constraints of TS 3.5.2.a. |
| : 19. As such, there was insufficient time to restore the pump to Operable status prior to expiration of the action time constraints of TS 3.5.2.a. Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No. SU-1023-8X, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence.
| | Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No. SU-1023-8X, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence. |
| PREVIOUS OCCURRENCES: | | PREVIOUS OCCURRENCES: |
| Based upon review of documentation, the high vibration of 21CCP pump speed increaser, as presently understood, is an isolated occurrence. | | Based upon review of documentation, the high vibration of 21CCP pump speed increaser, as presently understood, is an isolated occurrence. |
Line 72: |
Line 77: |
| SAFETY SIGNIFICANCE: | | SAFETY SIGNIFICANCE: |
| This occurrence is reportable pursuant to the requirements of | | This occurrence is reportable pursuant to the requirements of |
| * r
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| * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 SAFETY SIGNIFICANCE: (cont'd) DOCKET NUMBER 5000311 LER NUMBER 94-010-00 PAGE 4 of 4 10CFR50.73(a) | | r |
| (2) (i) (A), due to completion of a TS-required shutdown. | | * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 4 of 4 SAFETY SIGNIFICANCE: (cont'd) 10CFR50.73(a) (2) (i) (A), due to completion of a TS-required shutdown. |
| During this occurrence 22CCP was available, if required, to provide high head injection flow for the mitigation of any design base accident. | | During this occurrence 22CCP was available, if required, to provide high head injection flow for the mitigation of any design base accident. |
| CORRECTIVE ACTION: The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours on September 25, 1994, the Action of TS 3.5.2.a was exited. It is anticipated that by January 31, 1995 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration. | | CORRECTIVE ACTION: |
| | The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours on September 25, 1994, the Action of TS 3.5.2.a was exited. |
| | It is anticipated that by January 31, 1995 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration. |
| MJPJ:pc SORC Mtg. 94-078}} | | MJPJ:pc SORC Mtg. 94-078}} |
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Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Text
OPS~G
- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station October 12, 1994 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 94-010-00 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a) (2) (i) (A).
Issuance of this report is required within thirty (30} days of event discovery.
Sincerely yours, MJPJ:pc Distribution
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9410250120 941012 PDR ADOCK 05000311 S PDR The power is in your hanis. -1£11' y
95-2189 REV -92
I NRC FORM 366 .:::.. NUCLEAR REGULATORY COMMISSION *' APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT {LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF (See reverse for required number of digits/characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2)
II PAGE (3)
Salem Generating Station Unit 2 05000311 1 Of()4 TITLE (4) Controlled Reactor Shutdown uue To :n Centri:tugal Charging Pump Inoperable Greater Than 72 Hours EVENT DATE (5) LER NUMBER (6 REPORT NUMBER (7) OTHER FACILITIES INVOLVED 18\
FACILITY NAME DOCKET NUMBER SEQUENTIAL REVISION MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000 FACILITY NAME DOCKET NUMBER 09 22 94 94 -- 010 -- 00 10 12 05000 94 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more (11\
MODE (9) 1 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1 )(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71 (c)
LEVEL (10) 100% 20.405(a) (1) (ii) 50.36(c)(2) 50.73(a) (2) (vii) OTHER 20.405(a) (1) (iii) x 50. 73 (a)(2)(i) *50.73(a) (2) (viii) (A) (Specify in Abstract below and in Text, NRC 20.405(a) (1) (iv) 50.73(a)(2)(ii) 50.73(a) (2) (viii) (B) Form 366A) 20.405(a)(1 )(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LEA {12)
NAME TELEPHONE NUMBER (Include Area Code)
M. J. Pastva, Jr*' Licensee Event Reuort Coordinator 609-339-5165 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM
~~~* """'"°'""' ';;;",';':,"° * ~"'° "'""" ffiM~"ITT """'"°'"~ REPORTABLE TO NPRDS x
llJliilll BO SC N402 N I SUPPLEMENTAL REPORT EXPECTED 114) EXPECTED MONTH DAY YEAR YES SUBMISSION NO X (If yes, complete EXPECTED SUBMISSION DATE) DATE (15) 01 31 95 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced tfPewritten lines) (16)
At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br />, on 9/19/94, 21 Cen rifugal Charging Pump (CCP} was removed from service for scheduled preventive maintenance.
Post-maintenance testing results satisfied ASME operability criteria.
Increased axial vibration readings in 21CCP speed increaser were measured however, the vibration was not felt to impact pump operability and it was returned to service, at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> on 9/21/94.
Additional vibration readings showed unstable and increasing speed increaser vibration and at approximately 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, on 9/22/94, 21CCP was declared inoperable (effective from prior removal from service on 9/19/94). At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> (same day) the Technical Specification (TS) action time expired and at 1222 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.64971e-4 months <br /> (same day) the Unit was placed in MODE 4 (HOT SHUTDOWN). Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No.
SU-1023-SX, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence. The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.527005e-4 months <br /> on 9/25/94, the TS action was exited. It is anticipated that by 1/31/95 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration.
NRC FORM 366 (5-92)
- l REQUIRED NUMBER OF DIGITS/CHARACTERS FOR EACH BLOCK BLOCK NUMBER OF TITLE NUMBER DIGITS/CHARACTERS 1 UP TO 46 FACILITY NAME 8 TOTAL 2 DOCKET NUMBER 3 IN ADDITION TO 05000 3 VARIES PAGE NUMBER 4 UP TO 76 TITLE 6 TOTAL 5 EVENT DATE 2 PER BLOCK 7 TOTAL 2 FOR YEAR 6 LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 6 TOTAL 7 REPORT DATE 2 PER BLOCK UP TO 18 FACILITY NAME 8 OTHER FACILITIES INVOLVED 8 TOTAL-- DOCKET NUMBER 3 IN ADDITION TO 05000 9 1 OPERATING MODE 10 3 POWER LEVEL 1
11 REQUIREMENTS OF 10 CFR CHECK BOX THAT APPLIES UP TO 50 FOR NAME 12 LICENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES 1
14 SUPPLEMENTAL REPORT EXPECTED CHECK BOX THAT APPLIES 6 TOTAL 15 EXPECTED SUBMISSION DATE 2 PER BLOCK
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) and Institute of Electrical and Electronics Engineers (IEEE) Component Function Identifiers codes are identified in the text as {xx/xx}
IDENTIFICATION OF OCCURRENCE:
Controlled Reactor Shutdown Due To 21 Centrifugal Charging Pump Inoperable Greater Than 72 Hours Event Date: 9/22/94 Report Date: 10/12/94 This report was initiated by Incident Report No.94-271.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100% Unit Load 1080 MWe At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> on September 19, 1994, 21 Centrifugal Charging Pump (CCP) {BQ/P} was removed from service for scheduled preventive maintenance (PM). One of the activities was to investigate unusual noise from the speed increaser {BQ/P/SC} during pump operation. An adjustment was made to the motor shaft to speed increaser coupling.
Following post-maintenance testing, the pump, motor, and speed increaser vibrations were satisfactory and testing results satisfied ASME criteria for pump operability. Increased axial vibration readings were measured in the speed increaser. After Engineering review and consultation with the vendor, it was determined that the increased axial vibration did not impact pump operability. The pump was determined to be operable and returned to service, at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> on September 21, 1994. Additional vibration readings were recommended to verify that the axial vibration remained stable and that the consequences of the coupling adjustment were negligible.
DESCRIPTION OF OCCURRENCE:
At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br /> (same day), additional vibration readings indicated unstable and increasing axial vibration in the 21CCP speed increaser. This condition challenged pump operability and at approximately 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, on September 22,1994, it was declared inoperable (effective from prior removal from service on September 19th) .
Insufficient time remained to restore the pump to Operable status
LICENSEE EVENT REPORT (LER} TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 3 of 4 DESCRIPTION OF OCCURRENCE: (cont'd) prior to expiration of the 72-hour action time of Technical Specification (TS} 3.5.2.a, which occurred at 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> (same day}.
At 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> (same day} a controlled shutdown was initiated. At 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> (same day}, the NRC was notified of the initiation of the controlled shutdown, in accordance with 10CFR50.72(b} (i} (A}. At 0509 hours0.00589 days <br />0.141 hours <br />8.416005e-4 weeks <br />1.936745e-4 months <br /> (same day} the Unit was placed in MODE 3 (HOT STANDBY} and, at 1222 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.64971e-4 months <br /> (same day} was placed in MODE 4 (HOT SHUTDOWN}, as required by TS 3.5.2.a.
ANALYSIS OF OCCURRENCE:
In MODES 1 through 3, operability of two (2) independent Emergency Core Cooling Systems subsystems ensures sufficient emergency core cooling capability in the event of a Loss-Of-Coolant Accident assuming the loss of one subsystem through any active single failure consideration. Whenever a single CCP is unavailable, the redundant CCP will provide high head injection flow for the mitigation of any design base accident.
APPARENT CAUSE OF OCCURRENCE:
Upon measuring high vibration in the 21CCP speed increaser it was conservatively determined that the pump was inoperable from when it was previously removed from service on September 19. As such, there was insufficient time to restore the pump to Operable status prior to expiration of the action time constraints of TS 3.5.2.a.
Identification of the cause of the high vibration in the 21CCP speed increaser, Nuttal Gear Corp., Model No. SU-1023-8X, is pending results of root cause analysis by the vendor, with assistance from PSE&G. No problems were identified as contributory to this occurrence.
PREVIOUS OCCURRENCES:
Based upon review of documentation, the high vibration of 21CCP pump speed increaser, as presently understood, is an isolated occurrence.
LER 272/89-033-00, reported the inoperability 12CCP due to equipment failure of the pump speed increaser, attributed to inadequate Service Water System cooling flow through the speed increaser lube oil cooler. However, the cause of the inadequate flow could not be determined.
SAFETY SIGNIFICANCE:
This occurrence is reportable pursuant to the requirements of
r
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 94-010-00 4 of 4 SAFETY SIGNIFICANCE: (cont'd) 10CFR50.73(a) (2) (i) (A), due to completion of a TS-required shutdown.
During this occurrence 22CCP was available, if required, to provide high head injection flow for the mitigation of any design base accident.
CORRECTIVE ACTION:
The 21CCP speed increaser was replaced, the pump was satisfactorily tested; and, at 2241 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.527005e-4 months <br /> on September 25, 1994, the Action of TS 3.5.2.a was exited.
It is anticipated that by January 31, 1995 a supplement to this report will be submitted detailing the results of the root cause analysis of the 21CCP speed increaser high vibration.
MJPJ:pc SORC Mtg.94-078