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February 2, 2007
Stewart B. Minahan, Vice President-Nuclear and CNO Nebraska Public Power District 72676 648A Avenue Brownville, NE 68321
SUBJECT: COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTIONREPORT 05000298/2006005
Dear Mr. Edington:
On December 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your Cooper Nuclear Station. The enclosed integrated inspection report documents the inspection findings which were discussed on January 9, 2006, with you and other members of your staff.This inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, nine findings were evaluated under the risk significancedetermination process as having very low safety significance (Green). Eight of these findings were determined to be violations of NRC requirements. However, because these violations were of very low safety significance and the issues were entered into your corrective action program, the NRC is treating these findings as noncited violations, consistent with Section VI.A.1 of the NRC's Enforcement Policy. These noncited violations are described in the subject inspection report. If you contest the violations or significance of the violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-
4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Cooper Nuclear Station facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Nebraska Public Power District- 2 -Should you have any questions concerning this inspection, we will be pleased to discuss themwith you.
Sincerely,/RA/Michael C. Hay, ChiefProject Branch C Division of Reactor ProjectsDocket: 50-298License: DPR-46
Enclosure:
NRC Inspection Report 05000298/2006005
w/attachment:
Supplemental Information cc w/enclosure:Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499P. V. Fleming, Licensing ManagerNebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305 Nebraska Public Power District- 3 -Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Daniel K. McGhee, State Liaison OfficerBureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319Don Flater, Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319 Nebraska Public Power District- 4 -Ronald D. Asche, President and Chief Executive Officer Nebraska Public Power District 1414 15th Street Columbus, NE 68601Kevin V. Chambliss, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc.
440 Hamilton Avenue White Plains, NY 10601-1813Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Chief, Radiological Emergency Preparedness Section Kansas City Field Office Chemical and Nuclear Preparedness and Protection Division Dept. of Homeland Security 9221 Ward Parkway Suite 300 Kansas City, MO 64114-3372 Nebraska Public Power District- 5 -Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (SCS)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (MAS3)RITS Coordinator (MSH3)DRS STA (DAP)D. Cullison, OEDO RIV Coordinator (DGC)ROPreports CNS Site Secretary (SEF1)W. A. Maier, RSLO (WAM)R. E. Kahler, NSIR (REK)SUNSI Review Completed: __wcw_ADAMS: YesG No Initials: __wcw____ Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\_REACTORS\_CNS\2006\CN2006-05RP-SCS.wpdRIV:RI:DRP/CSRI:DRP/CC:DRS/OBC:DRS/PSBNHTaylorSCSchwindATGodyMPShannon E - WCWalker MCHay for /RA/ /RA/1/26/071/31/071/29/071/31/07C:DRS/EB1C:DRS/EB2C:DRP/CWBJonesLJSmithMCHay /RA/ /RA/ /RA/1/29/071/29/072/2/07OFFICIAL RECORD COPYT=Telephone E=E-mail F=Fax Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IV Docket:50-298License:DPR-46 Report:05000298/2006005 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:P.O. Box 98 Brownville, Nebraska Dates:September 24 through December 31, 2006 Inspectors:S. Schwind, Senior Resident InspectorN. Taylor, Resident Inspector J. Drake, Operations Engineer G. Guerra, Health Physicist, Plant Support Branch R. Kopriva, Senior Reactor Inspector, Engineering Branch 1 G. Pick, Senior Reactor Inspector, Engineering Branch 2 B. Tharakan, Health Physicist, Plant Support Branch W. Walker, Senior Project EngineerAccompanyingPersonnel:D. Bollock, Project EngineerC. Huffman, Nuclear Safety Professional Development ProgramApproved By:Michael C. Hay, Chief, Project Branch C, Division of Reactor Projects Enclosure-2-
SUMMARY OF FINDINGS
..................................................-3-
REPORT DETAILS
........................................................-8-
REACTOR SAFETY
.......................................................-8-1R01Adverse Weather..............................................-8-1R04 Equipment Alignment...........................................-9-1R05 Fire Protection................................................-9-1R07Biennial Heat Sink Performance.................................-10-1R08Inservice Inspection Activities...................................-11-1R11 Licensed Operator Requalification................................-12-1R12 Maintenance Effectiveness.....................................-16-1R13Maintenance Risk Assessments and Emergent Work Evaluation........-17-1R15 Operability Evaluations........................................-17-1R19 Postmaintenance Testing......................................-18-1R20 Refueling Outages............................................-20-1R22 Surveillance Testing...........................................-22-1EP6 Drill Evaluation...............................................-26-RADIATION SAFETY2OS1Access Control to Radiologically Significant Areas...................-26-2OS2ALARA Planning and Controls...................................-29-OTHER ACTIVITIES......................................................-30-4OA1Performance Indicator Verification................................-30-4OA2 Identification and Resolution of Problems..........................-31-4OA3Event Follow-up..............................................-38-4OA5Other Activities...............................................-40-4OA6 Meetings, Including Exit........................................-43-4OA7Licensee-identified Violations....................................-44-ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
................................................A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
...........................A-2
LIST OF DOCUMENTS REVIEWED
..........................................A-2
LIST OF ACRONYMS
.....................................................A-13
Enclosure-3-SUMMARY
- OF [[]]
FINDINGSIR 05000298/2006005; 09/24/2006 - 12/31/06; Cooper Nuclear Station. Licensed OperatorRequalification, Postmaintenance Testing, Refueling Outages, Surveillance Testing, Access
Controls to Radiologically Significant Areas, Identification and Resolution of Problems, Event
Followup, Other Activities.The report covered a 3-month period of inspection by resident inspectors and Region-basedinspectors. Eight Green, noncited violations and one Green Finding were identified. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the
significance determination process does not apply may be Green or be assigned a severity
level after
NRC's program for overseeing the safe operation of
commercial nuclear power reactors is described in
- NUR [[]]
EG-1649, "Reactor Oversight Process,"
Revision 3, dated July
- 2000.A.NRC -Identified and Self-Revealing FindingsCornerstone: Mitigating Systems*Green. The inspector identified a noncited violation of 10
CFR 55.21, "MedicalExamination," and 10 CFR 55.23, "Certification." The inspector identified that the
licensee failed to conduct all the medical testing required by American Nuclear
Standards Institute/American Nuclear Society 3.4 -1983, "Medical Certification and
Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," as
committed to by the facility licensee. Specifically, the licensee was not testing its
operators for nose sensitivity (i.e., ability to detect odor of products of combustion and of
tracer or market gases), Section 5.4.2, "Nose." Once identified, the licensee
implemented immediate corrective actions to medically test all operators prior to
returning to on-shift duties.This finding was more than minor because the inadequate medical examinations couldresult in potential consequences due to licensed operators who may not be medically
qualified to perform licensed duties and could, therefore, potentially affect the health and
safety of the public. The finding was also of very low safety significance because no
actual consequences were noted due to adverse medical conditions. In addition, no
adverse operational events were observed to have occurred due to inadequate medical
conditions or missed medical tests. This finding has a crosscutting aspect in the area ofhuman performance associated with work practices because the licensee did not
effectively supervise the work performed by the doctor, a contract worker, to ensure the
requirements in the applicable procedure, American National Standards
Institute 3.4-1983, were met. (Section 1R11.1)*Green. A self-revealing, noncited violation of Technical Specification 5.4.1.a wasidentified regarding the licensee's failure to follow procedures for maintenance affecting
the performance of safety-related equipment. Work Order 4514076 provided
instructions to instrumentation and control technicians to connect a digital recorder to
the Emergency Diesel Generator 2 voltage regulator. Contrary to the instructions in the
Enclosure-4-work order, the technicians connected additional test equipment, resulting in damage toEmergency Diesel Generator 2. The licensee entered this into their corrective action
program as Condition Report
CNS-2006-08999. The finding is more than minor because it is associated with the human performanceattribute of the Mitigating Systems cornerstone and affects the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences. Using the NRC Manual Chapter 0609,
Appendix GProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix G" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., "Shutdown Operations Significance Determination Process," Phase 1
Checklist, the finding is determined to have very low safety significance because one
operable diesel generator was still capable of supplying power to the Class 1E electrical
power distribution subsystems. This finding has a crosscutting aspect in the area ofhuman performance given that the licensee's work practices did not ensure that
personnel do not proceed in the face of uncertainty or unexpected circumstances.
(Section 1R19)*Green. A self-revealing, noncited violation of Technical Specification 5.4.1.a wasidentified for the licensee's failure to establish adequate maintenance procedures for
safety-related, motor-operated valves. Between 1993 and 2006, maintenance
procedures for Limitorque motor actuators did not contain sufficient detail to ensure that
actuator motor pinion gears were installed correctly. This deficiency resulted in the
failure of a low pressure safety injection valve on October 17, 2006, due to its pinion
gear migrating off the motor shaft. This issue was entered into the licensee's corrective
action program as Condition Report
CNS-2006-07490. The finding is more than minor because it is associated with the Mitigating Systemscornerstone attribute of equipment performance and affects the associated cornerstone
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events. The Phase 1 worksheets in NRC Manual Chapter 0609, "Significance
Determination Process," were used to conclude that a Phase 2 analysis was required
because it resulted in the loss of a train of low pressure coolant injection for greater than
the Technical Specification allowed outage time. The inspectors performed a Phase 2
analysis using Appendix A, "Technical Basis For At Power Significance Determination
Process," of Manual Chapter 0609, "Significance Determination Process," and the
Phase 2 worksheet for Cooper Nuclear Station. Based on the results of the Phase 2
analysis, the finding is determined to have very low safety significance. (Section 1R22)*Green. A self-revealing, noncited violation of
XVI, was identified regarding the licensee's failure to correct a nonconforming
condition in safety-related, motor-operated valves. In 1994, Limitorque and the NRC
notified the industry that the torque switch roll pin in certain Limitorque valve actuators
was susceptible to failure. The licensee took no corrective actions based on this
notification. On November 8, 2006, the acceptable torque range was exceeded during
stroking of the high pressure coolant injection inboard steam isolation valve due to the
failure of the torque switch roll pin. This issue was entered into the licensee's corrective
action program as Condition Report
Enclosure-5-The finding affected the Mitigating Systems cornerstone and is more than minorbecause, if left uncorrected, it would become a more safety significant concern. Using
the Manual Chapter 0609, "Significance Determination Process," Phase 1 Worksheet,
the finding is determined to have very low safety significance because there was no loss
of safety function for the high pressure coolant injection system. (Section
CFR Part 50, Appendix B,Criterion XVI, was identified regarding the licensee's failure to identify and correct age-
related degradation in the motor coupling for Service Water Discharge Strainer A.
Corrective maintenance designed to identify and replace degraded components was
performed in February 2006; however, the licensee failed to identify and replace a
degraded rubber sleeve in the coupling which subsequently failed on October 29, 2006.
This issue was entered into the licensee's corrective action program as Condition Report
CNS-2006-08226. The finding is more than minor because it is associated with the Mitigating Systemscornerstone attribute of equipment performance and affects the associated cornerstone
objective to ensure the availability and reliability of systems that respond to initiating
events. The Phase 1 worksheet in Manual Chapter 0609, "Significance Determination
Process," were used to conclude that a Phase 2 analysis was required because the
finding also increased the likelihood of a loss of service water initiating event. Based on
the results of a Phase 3 analysis, the finding is determined to have very low safety
significance. The cause of the finding is related to the corrective action component of
the crosscutting area of problem identification and resolution in that the licensee failed toidentify this issue in a timely manner. (Section 4OA2.1)*Green. A self-revealing finding was identified regarding the failure to install heat traceon the standby liquid control system in accordance with the vendor manual. The heat
trace was installed in 1994 without the required ground-fault circuit protection. This
resulted in a small fire in the heat trace on November 11, 2006. This issue was entered
into the licensee's corrective action program as Condition Report
CNS-2006-09006.The finding is more than minor because it is associated with the Mitigating SystemsCornerstone attribute of design control and affects the associated cornerstone objective
to ensure the availability, reliability, and capability of the standby liquid control system
that is required to respond to initiating events, such as anticipated transients without
scrams. Using the Manual Chapter 0609, "Significance Determination Process,"
Phase 1 Worksheet, the finding is determined to have very low safety significance
because it did not result in a loss of safety function. (Section 4OA3.1)Cornerstone: Barrier Integrity
Green. The
CFR Part 50, Appendix B,Criterion XVI, involving the licensee's failure to promptly identify and correct a condition
adverse to quality regarding an unanalyzed condition in the torus. Specifically, the
inspectors identified a trolley/hoist and chain in the torus that had been in the torus for
Enclosure-6-the past five operating cycles without being evaluated for its potential impact on safety-related equipment. The licensee documented the condition in Condition Report
CNS-2006-09338.The finding is more than minor because it is associated with the Barrier Integritycornerstone attribute of design control and it affects the associated cornerstone
objective to provide reasonable assurance that physical design barriers protect the
public from radionuclide releases caused by accidents or events. Using the NRC
Manual Chapter 0609, "Significance Determination Process," Phase 1 worksheet, the
finding is determined to have very low safety significance because it did not represent
an actual breach of containment. This finding has a crosscutting aspect in the area ofproblem identification and resolution in that the licensee did not implement a corrective
action program with a low threshold for identifying issues. Specifically, the unanalyzed
condition existed in a location frequently accessed during refueling outages but never
questioned by the licensee. (Section 1R20)*Green. The NRC identified a noncited violation of Technical Specification 5.4.1.aregarding the licensee's failure to follow procedures for power operation and process
monitoring. Specifically, the licensee operated the reactor above the total core flow
limit, contrary to requirements of General Operating Procedure 2.1.10, "Station Power
Changes." The licensee documented this violation in Condition Report
CNS-2006-
255.The finding is more than minor because it is associated with the Barrier Integritycornerstone attribute of human performance (procedural adherence) and it affects the
associated cornerstone objective to provide reasonable assurance that physical design
barriers, such as fuel cladding, protect the public from radionuclide releases caused by
accidents or events. Using the NRC Manual Chapter 0609, "Significance Determination
Process," Phase 1 worksheet, the finding is determined to have very low safety
significance because it only had the potential to affect the fuel cladding barrier. This
finding has a crosscutting aspect in the area of human performance in that the licenseedid not effectively communicate expectations regarding work practices to operators for
the control of key parameters such as total core flow. (Section 4OA2.1)Cornerstone: Occupational Radiation Safety
- Green. The inspectors reviewed a self-revealing, noncited violation of TechnicalSpecification 5.4.1.a involving the licensee's procedure for reactor pressure vessel
refueling preparation was not adequate. The licensee's refueling procedure allowed the
control room supervisor or shift manager to alter the sequence to suit existing plant
conditions and time requirements. However, the procedure did not contain any
precautions or limitations to consider the impact that altering the sequence would have
on ancillary systems, such as the high efficiency particulate air filter hose connection to
the reactor pressure vessel vent. In addition, the change in sequence was not
communicated or coordinated with radiation protection to evaluate potential radiological
impacts. Consequently, when the licensee raised the reactor pressure vessel water
level at an earlier stage in the reactor head disassembly process, the increased
temperature and pressure applied to the high efficiency particulate air hose caused it to
Enclosure-7-disconnect from the reactor pressure vessel vent. The loss of this connection releasedactivation products onto the refuel floor and created an airborne radioactivity area, which
alarmed the continuous air monitor and contaminated five workers. The licensee's
immediate corrective actions were to evacuate personnel from the refuel floor and begin
decontamination of the workers and the areas involved.The finding is more than minor because it is associated with the occupational RadiationSafety cornerstone attribute of Program and Process, and it affects the cornerstone
objective to ensure the adequate protection of a worker's health and safety from
exposure to radiation from radioactive materials because it resulted in unintended
internal doses. Using the Occupational Radiation Safety Significance Determination
Process, the finding is determined to have very low safety significance (Green) because
it was not an as low as is reasonably achievable finding, there was no overexposure or
substantial potential for an overexposure, and the ability to assess the dose was not
compromised. Additionally, this finding had a crosscutting aspect in the area of humanperformance associated with the component of work control because the licensee failed
to coordinate work activities by incorporating actions to address the impact of the work
on different job activities and communicate, coordinate, and cooperate with each other
during activities in which interdepartmental coordination is necessary to assure
appropriate plant and human performance. (Section 2OS1)B.Licensee Identified ViolationsViolations of very low safety significance that were identified by the licensee have beenreviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensee's corrective action program. These violations and
correction action tracking numbers are listed in Section 4OA7 of this report.
Enclosure-8-REPORT
- DETAIL [[]]
SSummary of Plant StatusThe plant began the inspection period at essentially full reactor power in coastdown toRefueling Outage 23. The reactor was manually scrammed on October 21, 2006, for the
refueling outage. A plant startup was conducted on November 21, 2006, and the and the main
generator was synchronized to the grid on November 22, 2006. Reactor power was reduced to
percent on November 24, 2006, and the main turbine was removed from service to repair a
steam leak on Moisture Separator C. Full power operation was achieved on November 27,
2006. The plant remained at full power for the remainder of the period.1.REACTOR
- SAFET [[]]
YCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather (71111.01A) a.Inspection ScopeThe inspectors completed a review of the licensee's readiness for seasonalsusceptibilities involving extreme low temperatures. The inspectors: (1) reviewed plant
procedures, the Updated Final Safety Analysis Report (UFSAR), and Technical
Specifications (TS) to ensure that operator actions defined in adverse weather
procedures maintained the readiness of essential systems; (2) walked down portions of
the three systems listed below to ensure that adverse weather protection features (heat
tracing, space heaters, weatherized enclosures, etc.) were sufficient to support
operability, including the ability to perform safe shutdown functions; (3) evaluated
operator staffing levels to ensure the licensee could maintain the readiness of essential
systems required by plant procedures; and (4) reviewed the corrective action
program (CAP) to determine if the licensee identified and corrected problems related to
adverse weather conditions. *Fire protection*Condensate storage
- Emergency diesel generators (EDGs)Documents reviewed by the inspectors included:
- Maintenance Procedure 7.2.80, "Intake Structure Guide Wall Winterization andRestoration," Revision 5*General Operating Procedure 2.1.14, "Seasonal Weather Preparations,"Revision 8The inspectors completed one sample.
Enclosure-9- b. FindingsNo findings of significance were identified.1R04 Equipment Alignment (71111.04)Partial System Walkdowns a.Inspection ScopeThe inspectors: (1) walked down portions of the two risk important systems listed belowand reviewed plant procedures and documents to verify that critical portions of the
selected systems were correctly aligned; and (2) compared deficiencies identified during
the walkdown to the licensee's
CAP to ensure problems were being
identified and corrected. *September 29, 2006: Offsite power sources during planned maintenance on thestation startup service transformer*December 11, 2006: Service Water (SW) Loop A while Loop B was inoperablefor planned maintenanceDocuments reviewed by the inspectors included:
- Surveillance Procedure 6.EE.610, "Offsite Power Alignment," Revision 16*System Operating Procedure 2.2.71, "Service Water System," Revision 90The inspectors completed two samples. b.FindingsNo findings of significance were identified.1R05 Fire Protection (71111.05Q) a.Inspection ScopeThe inspectors walked down the six plant areas listed below to assess the materialcondition of active and passive fire protection features and their operational alignment.
The inspectors: (1) verified that transient combustibles and hot work activities were
controlled in accordance with plant procedures; (2) observed the condition of fire
detection devices to verify they remained functional; (3) observed fire suppression
systems to verify they remained functional and that access to manual actuators was
unobstructed; (4) verified that fire extinguishers and hose stations were provided at their
designated locations and that they were in a satisfactory condition; (5) verified that
passive fire protection features (electrical raceway barriers, fire doors, fire dampers,
steel fire proofing, penetration seals, and oil collection systems) were in a satisfactory
material condition; (6) verified that adequate compensatory measures were established
Enclosure-10-for degraded or inoperable fire protection features and that the compensatory measureswere commensurate with the significance of the deficiency; and (7) reviewed the CAP to
determine if the licensee identified and corrected fire protection problems. September 29, 2006: Fire Zone 3A, 4160V Bus 1F RoomSeptember 29, 2006: Fire Zone 3b, 4160V Bus 1G RoomNovember 1, 2006: Fire Zone 20A, Service Water Pump RoomNovember 11, 2006: Fire Zone 5A, Reactor Building 976 EastDecember 8, 2006: Fire Zone 14A,
EDG 2 RoomDocuments reviewed by the inspectors included:
CNS Fire Hazards Analysis Report, June 20, 2002The inspectors completed six samples. b. FindingsNo findings of significance were identified.1R07Biennial Heat Sink Performance (71111.07B) a.Inspection ScopeThe inspectors reviewed design documents (e.g., calculations and performancespecifications), program documents, implementing documents (e.g., test and
maintenance procedures), and corrective action documents. The inspectors interviewed
chemistry personnel, maintenance personnel, engineers, and program managers. For heat exchangers directly connected to the safety-related service water system, theinspectors verified whether testing, inspection, maintenance, and the biotic fouling
monitoring program provided sufficient controls to ensure proper heat transfer.
Specifically, the inspectors reviewed: (1) heat exchanger test methods and test results
from performance testing, and (2) if necessary, heat exchanger inspection and cleaning
methods and results. For heat exchangers directly or indirectly connected to the safety-related service watersystem, the inspectors verified that: (1) the condition and operation was consistent with
design assumptions in the heat transfer calculations, (2) the potential for water hammer
was assessed, as applicable, and (3) chemistry controls for heat exchangers indirectly
connected to the safety-related service water system were appropriate. For the ultimate heat sink and its subcomponents, the inspectors reviewed the followingrequirements: (1) macrofouling controls, (2) biotic fouling controls, and (3) performance
tests for pumps and valves.
Enclosure-11-If available, the inspectors reviewed additional nondestructive examination (NDE) resultsfor the selected heat exchangers that demonstrated structural integrity. The inspectors selected heat exchangers that ranked high in the plant-specific riskassessment and were directly or indirectly connected to the safety-related service water
system. The inspectors selected the following specific heat exchangers: Division
REC) heat exchanger
Turbine equipment cooling heat exchangersThe inspector completed three of the required two to three samples. b.FindingsNo findings of significance were identified.1R08Inservice Inspection Activities.1Performance of
NDE activities of at least two or threedifferent types. The inspector witnessed the performance of two unltrasonic, two
penetrant, and two visual examinations. In addition, the inspector reviewed other visual,
penetrant, magnetic particle, and ultrasonic inspections. The complete list of NDE
activities reviewed is listed in the "List of Documents Reviewed" attachment to this
report. For each of the selected
- NDE activities, the inspector verified that the examinationswere performed in accordance with American Society of Mechanical Engineers (
ASME)
Code requirements.During the review of each examination, the inspector verified that appropriate NDEprocedures were used, that examinations and conditions were as specified in the
procedure, and that test instrumentation or equipment was properly calibrated and within
the allowable calibration period. During the underwater visual inspections of the steam
dryer, two cracked tack welds were identified. The tack welds are located on one of the
four steam dryer lifting lugs. An evaluation of the cracked tack welds was performed
and were found to be acceptable as is. The inspector also reviewed the evaluation
documentation to verify that these indications revealed by the examinations were
dispositioned in accordance with the
- III [[]]
NDE personnelobserved performing examinations or identified during review of completed examination
packages.
Enclosure-12-The inspection procedure requires review of one or two examinations from the previousoutage with recordable indications that were accepted for continued service to ensure
that the disposition was done in accordance with the
- AS [[]]
ME Code. There were no
recordable indications that required evaluation during the last outage. The licensee completed welding on one pressure boundary Class 2 structure at the endof Refueling Outage RF23. The licensee modified the support for the vent/purge line in
containment for Valve AOV-237. The inspector verified that acceptance and preservice
examinations were completed in accordance with the
ASME Code Section XI repairsor replacements meet Code requirements. There were no Code repairs or
replacements available at the time of this inspection. The inspector reviewed three licensee Request for Relief submittals for the fourth10-year interval inservice inspection. These relief requests pertained to peripheral
control rod drives, buried service water piping, and reactor vessel head flange leak
detection lines. The inspector reviewed the licensee's compliance to the relief request
response.The inspector completed the minimum one sample for this inspection. b.FindingsNo findings of significance were identified..2Identification and Resolution of Problems a. Inspection ScopeThe inspector reviewed selected inservice inspection related condition reports issuedduring the current and past refueling outages. The review served to verify that the
licensee's corrective action process was being correctly utilized to identify conditions
adverse to quality and that those conditions were being adequately evaluated,
corrected, and trended. b.FindingsNo findings of significance were identified.1R11Licensed Operator Requalification (71111.11Q).1Quarterly Requalification Activities a.Inspection ScopeThe inspectors observed testing and training of senior reactor operators and reactoroperators in the simulator on October 2, 2006, to verify adequacy of the training, to
Enclosure-13-assess operator performance, and to assess the evaluator's critique. The inspectorsobserved a simulator scenario involving a failure of the main turbine hydraulic control
system. Documents reviewed by the inspectors included:Lesson Plan
- SKL [[051-51-49, Loss of Main Generator Cooling and Failure of theDigital-Electrohydraulic Control SystemThe inspectors completed one sample. b.FindingsNo findings of significance were identified..2Licensed Operator Requalification (71111.11B)Biennial Inspection a.Inspection ScopeThe inspectors: (1) evaluated examination security measures and procedures forcompliance with 10]]
CFR 55.49; (2) evaluated the licensee's sample plan for the written
examinations for compliance with
NUREG-1021, as referenced in the
facility requalification program procedures; and (3) evaluated maintenance of license
conditions for compliance with 10 CFR 55.53 by review of facility records (medical and
administrative), procedures, and tracking systems for licensed operator training,
qualification, and watchstanding. In addition, the inspectors reviewed remedial training
and examinations for examination failures for compliance with facility procedures and
responsiveness to address areas failed.Furthermore, the inspectors: (1) interviewed six personnel (three operators, twoinstructors/evaluators, and one training supervisor) regarding the policies and practices
for administering examinations; (2) observed the administration of two dynamic
simulator scenarios to a requalification crew by facility evaluators, including an
operations department manager, who participated in the crew and individual
evaluations; and (3) observed two facility evaluators administer five job performance
measures, including two in the control room simulator in a dynamic mode and three in
the plant under simulated conditions. Each job performance measure was observed
being performed by an average of four requalification candidates. The inspectors also reviewed the remediation process for three individuals, one of whichinvolved a written examination failure, one a simulator examination failure, and one
periodic weekly quiz failure. The inspectors also reviewed the results of the annual
licensed operator requalification operating examinations for 2004 and 2006. The results
of the examinations were also reviewed to assess the licensee's appraisal of operator
performance and the feedback of that performance analysis to the requalification
training program. Inspectors also observed the exam security maintenance during the
exam week. Examination results were also assessed to determine if they were
consistent with the guidance contained in
- NUR [[]]
EG 1021, "Operator Licensing
Enclosure-14-Examination Standards for Power Reactors," Revision 9, and NRC ManualChapter 0609, Appendix I, "Operator Requalification Human Performance Significance
Determination Process [SDP]." Additionally, the inspector reviewed 12 licensed
operators' medical records maintained by the facility licensee and assessed compliance
with the medical standards delineated in
ANS 3.4-1983, "American National
Standard Medical Certification and Monitoring of Personnel Requiring Operator Licenses
for Nuclear Power Plants," and with
CFR 55.25. During the in-office review, the inspectors evaluated the written examination results,whether the written examination was developed and administered in accordance with
the standards described in
- NUR [[]]
EG 1021, and any issues identified in accordance with
NRC Manual Chapter 0609, Appendix I. The written examination review was focused on
quality aspects of the examination, such as discrimination validity, examination question
psychometric quality, and examination integrity. b.FindingsIntroduction: The inspector identified a Green, noncited violation (NCV) of
CFR 55.23, "Certification," involving the failure to
conduct all the medical testing required by
ANS 3.4-1983, "Medical Certification
and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants." Description: The inspector determined that an apparent long-standing programmaticdeficiency had existed at the Cooper Nuclear Station, whereby the licensee's medical
physician was not adequately testing all licensed operators (both initial and renewal
licensees) in accordance with
ANSI/ANS 3.4-
1983Property "ANSI code" (as page type) with input value "ANSI/ANS 3.4-</br></br>1983" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.. Specifically, certain medical conditions identified by the inspector in the licensedoperators' medical records led to the identification that a medical test required to be
conducted in accordance with
ANS 3.4 (nose sensitivity, Section 5.4.2) was not
tested on any of the 57 licensed operators. At a minimum, this issue involved the last
two biennial medical examinations conducted in years 2004 and 2006. The lack of
testing also included the most recently licensed operators following the June 2005 initial
license examination. The failure to conduct all the required medical examination tests
was a potential violation of 10 CFR 55.21 and 55.23. The inspector verified the adequacy of immediate corrective actions implemented by thelicensee. The licensee took the following corrective actions, which were considered to
be prompt, from the time the licensee was informed by the NRC that a problem existed,
involving complete and accurate performance and reporting requirements of medical
examinations. The medical physicians who performed these medical evaluations were givenadditional training on the requirements of
- ANS 3.4-1983.The contracts between the medical facility and the utility were altered tospecifically require a review against the
- AN [[]]
SI standard.
Enclosure-15-The administrative procedure governing the medical reporting process wasrevised, including the development of a comprehensive medical checklist.The Cooper Nuclear Station medical records were audited to identify anyadditional problems with medical conditions that were not reported to the NRC.The licensee implemented immediate corrective action to conduct the missedtest on all operators before they were allowed back on-shift. The missed medical test was conducted using a scratch and sniff card to verify thatlicensed personnel could detect odors. The licensee had this test conducted and
reviewed and certified by a medical physician. Analysis: The inspector reviewed the missed medical examination issue against theguidance contained in Appendix B, "Issue Dispositioning Screening," of Inspection
Manual Chapter 0612, "Power Reactor Inspection Reports." This finding affected the
mitigating system cornerstone objective because inadequate medical examinations
on operator license applicants and licensed operators could result in potential
consequences of licensed operators who may not be medically qualified to perform
licensed duties and could cause operational errors, therefore, potentially endangering
the health and safety of the public. Consequently, the safety significance of this issue
was determined to be more than minor. Additionally, this finding has a crosscutting
aspect in the area of human performance associated with work practices because the
licensee did not effectively supervise the work performed by the doctor, a contract
worker, to ensure the requirements in the applicable procedures,
- AN [[]]
SI 3.4-1983, were
met. The inspector reviewed this issue in accordance with Manual Chapter 0609,"Significance Determination Process," Appendix I, "Operator Requalification Human
Performance Significance Determination Process." The SDP concerning medical issues
focused on general record deficiencies exceeding a specified threshold of 20 percent of
the records reviewed. Based on this SDP, the inspector determined that this finding
was of very low safety significance (Green) because the failure to conduct the required
medical examination tests for all licensed operators and initial license applicants
exceeded the 20 percent threshold for record deficiencies. Enforcement: Part 55.21 of
CFRPart 55 license and current 10 CFR Part 55 licensee have a medical examination by a
physician every 2 years. The physician shall determine that the applicant or licensee
meets the requirements of
CFR 55.23 required that
to certify the medical fitness of the applicant, an authorized representative of the facility
licensee complete and sign Form NRC-396, "Certification of Medical Examination by
Facility Licensee." The licensee committed to follow
ANS 3.4-1983 as the way
they would meet Part 55.46 (d)(1).
ANS 3.4-1983 required, in part, that the
primary responsibility for assuring that qualified personnel are on duty rests with the
facility licensee. In addition, the health requirements set forth within the standard
provide the minimum necessary to determine that the physical condition and general
health of the operators were not such as might cause operational errors endangering
Enclosure-16-the public health and safety. The specific health requirements and disqualifyingconditions are described in Section 5.3, "Disqualifying Conditions," and Section 5.4,
"Specific Minimum Capacities Required for Medical Qualifications," of the
- AN [[]]
standard. However, on August 9, 2006, prompted by the inspector's assessment
regarding the inadequacy of the facility licensee's medical examinations, the licensee
conducted reviews of all medical examinations and records and found that certain
tests in accordance with
ANS 3.4-1983 had not been performed. In fact, all initial
license applicants and previously licensed operators (32 operators) were not adequately
examined for all medical tests as required to meet the minimum standards of
ANS 3.4-1983. Specifically, the facility licensee was not testing its operators for
nose sensitivity (Section 5.4.2).This Green finding concerning the missed medical test is considered a violation of10 CFR 55.21 and 55.23. Because of the very low safety significance, this violation
is being treated as an
VI.A.1 of
the NRC Enforcement Policy. This issue was in the licensee's corrective action program
as
CNS-2006-05775. The licensee adequately implemented immediate corrective
action and satisfactorily performed the missed medical test. In addition, the licensee
implemented additional corrective actions as indicated in this report. 1R12Maintenance Rule (711111.12Q) a.Inspection ScopeThe inspectors reviewed the maintenance effectiveness performance issues listed belowto: (1) verify the appropriate handling of structure, system, and component (SSC)
performance or condition problems; (2) verify the appropriate handling of degraded SSC
functional performance; (3) evaluate the role of work practices and common cause
problems; and (4) evaluate the handling of SSC issues reviewed under the requirements
of the maintenance rule,
RHR-MOV-MO25B) Failed to OpenThe inspectors completed three samples. b.FindingsNo findings of significance were identified.
Enclosure-17-1R13Maintenance Risk Assessments and Emergent Work Evaluation (71111.13) a.Inspection Scope The inspectors reviewed the two maintenance activities listed below to verify: (1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and
licensee procedures prior to changes in plant configuration for maintenance activities
and plant operations; (2) the accuracy, adequacy, and completeness of the information
considered in the risk assessment; (3) that the licensee recognized, and/or entered as
applicable, the appropriate licensee-established risk category according to the risk
assessment results and licensee procedures; and (4) the licensee identified and
corrected problems related to maintenance risk assessments.September 29, 2006: Work Order (WO) 4451770 for planned maintenance onthe station startup service transformerOctober 23, 2006:
KV Breaker)The inspectors completed two samples. b.FindingsNo findings of significance were identified.1R15 Operability Evaluations (71111.15) a.Inspection Scope For the following equipment performance issue, the inspectors: (1) reviewed plantstatus documents such as operator shift logs, emergent work documentation, deferred
modifications, and standing orders to determine if an operability evaluation was
warranted for degraded components; (2) referred to the
- UFS [[]]
AR and design basis
documents to review the technical adequacy of licensee operability evaluations;
(3) evaluated compensatory measures associated with operability evaluations;
(4) determined degraded component impact on any
SDP to evaluate
the risk significance of degraded or inoperable equipment; and (6) verified that the
licensee has identified and implemented appropriate corrective actions associated with
degraded components.Condition Report
CNS-2006-07083, EDG Tachometers ImproperlyGroundedThe inspectors completed one sample. b.FindingsNo findings of significance were identified.
Enclosure-18-1R19 Postmaintenance Testing (71111.19) a.Inspection ScopeThe inspectors selected four postmaintenance tests associated with the maintenanceactivities listed below for risk significant systems or components. For each item, the
inspectors: (1) reviewed the applicable licensing basis and/or design basis documentsto determine the safety functions; (2) evaluated the safety functions that may have been
affected by the maintenance activity; and (3) reviewed the test procedure to ensure it
adequately tested the safety function that may have been affected. The inspectors
either witnessed or reviewed test data to verify that acceptance criteria were met, plant
impacts were evaluated, test equipment was calibrated, procedures were followed,
jumpers were properly controlled, the test data results were complete and accurate, the
test equipment was removed, the system was properly re-aligned, and deficiencies
during testing were documented. The inspectors also reviewed the
- UFS [[]]
AR to
determine if the licensee identified and corrected problems related to postmaintenance
testing. *October 25, 2006:
- WO 4528348 for a modification to allow the reactor watercleanup system to be cross-connected to the fuel pool cooling system*November 5, 2006:
TS 5.4.1.a was identified regarding thelicensee's failure to follow procedures for maintenance affecting the performance of
safety-related equipment.Description: On November 11, 2006, EDG 2 was started to support postwork testingfollowing the replacement of its voltage regulator during the refueling outage.
WO 4514076 included instructions for the instrumentation & control (I&C) technicians to
connect an oscillograph recorder to the EDG output to record the voltage seen at the
voltage regulator.The EDG was secured shortly after being started due to an unrelated condition. Thetechnicians noted that the data taken by the recorder was not as expected. In an
attempt to validate the performance of the recorder, a technician connected a variac to
the recorder, without disconnecting it from the system, and applied a 60 volt test signal
Enclosure-19-to the recorder. The technician immediately realized that he had energized the voltageregulator through the recorder, secured power to the variac, and disconnected the
recorder from the system. The technician then tested the recorder with the variac off-
line and subsequently reinstalled the recorder in the system. The technician did not
notify other personnel of this error or initiate a condition report at the time.During the subsequent start of the
EDG 2 tripped and locked out on overvoltage. During the posttrip
troubleshooting, it was determined that the cause of the overvoltage condition was a
blown fuse that deenergized one of three phases of electrical power from the voltage
regulator's potential transformer. The licensee determined that the cause of the blown
fuse was the introduction of the variac into the circuit, feeding 60-volt electrical power to
the secondary windings of the potential transformer. This introduced a stepped-up
voltage on the primary windings and resulted in a blown fuse on one of the three phases
of the potential transformer. As a result, the EDG voltage regulator saw the sum of only
two phases of output voltage (versus the three normally seen) and continued to raise
voltage until an overvoltage trip was received.The inspectors reviewed the work instructions provided in WO 4514076. The scope ofthese instructions did not include any contingencies for troubleshooting unanticipated
problems with the recorder. The inspector determined that the procedural steps in the
WO were adequate for the anticipated activities, but that the I&C technicians had
deviated from the WO instructions and introduced an unanticipated piece of test
equipment to the voltage regulator circuit.Analysis: The performance deficiency associated with this finding involved thelicensee's failure to follow work instructions for maintenance affecting the performance
of safety-related equipment. The finding is more than minor because it is associated
with the human performance attribute of the mitigating systems cornerstone and affects
the cornerstone objective to ensure the availability, reliability, and capability of systems
that respond to initiating events to prevent undesirable consequences (i.e., core
damage). Using the Manual Chapter 0609, Appendix G, "Shutdown Operations
Significance Determination Process," Phase 1 checklist, the finding is determined to
have very low safety significance because one operable diesel generator was still
capable of supplying power to the Class 1E electrical power distribution subsystems.This finding has a crosscutting aspect in the area of human performance in that thelicensee's work practices did not ensure that personnel do not proceed in the face of
uncertainty or unexpected circumstances.Enforcement:
- TS 5.4.1.a requires that written procedures be established, implemented,and maintained covering the activities specified in Regulatory Guide (
RG) 1.33,
Revision 2, Appendix A, dated February 1978. RG 1.33, Appendix A, Section 9 (a),
requires that maintenance that can affect the performance of safety-related equipment
should be performed in accordance with written procedures. WO 4514076 provided
instructions to
EDG 2 voltage
regulator. Contrary to the instructions in the WO, the technicians connected additional
test equipment, resulting in damage to the EDG. Because the finding is of very low
Enclosure-20-safety significance and has been entered into the licensee's
CR-CNS-2006-08999, this violation is being treated as an NCV consistent with
Section
NCV 05000528/2006005-02, "Failure to Follow
Work Instructions."1R20Refueling Outages (7111.20) a.Inspection ScopeThe inspectors reviewed the following risk significant refueling items or outage activitiesto verify defense in depth commensurate with the outage risk control plan and
compliance with the TSs: (1) the risk control plan; (2) reactor coolant system
instrumentation; (3) electrical power; (4) decay heat removal; (5) spent fuel pool cooling;
(6) inventory control; (7) reactivity control; (8) containment closure; (9) refueling
activities; (10) heatup and cooldown activities; (11) restart activities; and (12) licensee
identification and implementation of appropriate corrective actions associated with
refueling and outage activities. The inspectors also conducted detailed inspection of the
drywell and torus for cleanliness and reactor coolant leaks.The inspectors completed one sample. b.FindingsIntroduction: The inspectors identified a Green NCV regarding the failure to promptlyidentify and correct a condition adverse to quality regarding an unanalyzed condition in
the torus.Details: During a torus closeout walkdown on November 15, 2006, the inspectorsidentified an unrestrained trolley/hoist and chain hanging from a monorail beam inside
the torus. The monorail beam is located in the top of the torus and runs the length of
the torus directly above each of the torus-to-drywell vacuum breakers. In the as-found
configuration, the trolley/hoist was free to travel around the monorail and the chains
were hanging low enough to impact the vacuum breakers. The trolley/hoist was not
fitted with any braking mechanism to keep it from moving down the monorail during a
dynamic event in the torus (such as the lift of the safety relief valves or a design basis
seismic event).The inspectors questioned licensee personnel that were present during the closeout tourabout the acceptability of leaving the trolley/hoist hanging in the torus for the next
operating cycle, after which the chain was wrapped around a handrail inside the torus, in
an attempt to restrict its potential for movement. Immediately after exiting the torus the
inspector questioned licensee management about the acceptability of this condition in
the torus. During the next shift, the licensee completed the final closeout of the torus
without making any attempt to evaluate the acceptability of the trolley/hoist.The following day the inspectors learned that the torus had been sealed and againquestioned licensee management regarding the condition; however, the licensee was
unable to demonstrate the acceptability of the trolley/hoist. They identified that the
Enclosure-21-trolley/hoist and chain had probably been in the torus for at least five operating cycleswithout being evaluated for potential impact on safety-related equipment. The licensee
subsequently re-opened the torus and removed the trolley/hoist and chain.In a subsequent evaluation documented in Condition Report
CNS-2006-09338, thelicensee determined that, although the chain and trolley/hoist could have become a
missile during postulated events in the torus, they were not of sufficient size or mass to
interfere with the function of safety-related equipment. In addition, the licensee
demonstrated that, while the hanging chain could have damaged the air operators for
the torus-to-drywell vacuum breakers, their safety function would not have been affected
since the air operators are used only for testing and are not necessary during an
accident.Analysis: The performance deficiency associated with this finding involved the failure topromptly identify and correct a condition adverse to quality. Specifically, an unanalyzed
trolley/hoist and associated length of chain hung from a monorail beam inside the torus
for at least five operating cycles until discovered by the inspectors. After being made
aware of the condition by the inspectors, the licensee did not evaluate the condition or
take any corrective action prior to performing a final closeout of the torus. The finding is
more than minor because it is associated with the Barrier Integrity cornerstone attribute
of design control and it affects the associated cornerstone objective to provide
reasonable assurance that physical design barriers protect the public from radionuclide
releases caused by accidents or events. Using the NRC Manual Chapter 0609,
"Significance Determination Process," Phase 1 worksheet, the finding is determined to
have very low safety significance because it did not represent an actual open pathway in
the physical integrity of reactor containment.This finding has a crosscutting aspect in the area of problem identification andresolution in that the licensee did not implement their CAP with a low threshold for
identifying this issue. Specifically, the trolley/hoist existed in a location frequently
accessed during refueling outages but was not identified for at least five operating
cycles.Enforcement:
XVI, requires that measures shallbe established to assure that conditions adverse to quality, such as failures,
malfunctions, deficiencies, deviations, defective material and equipment, and
nonconformance, are promptly identified and corrected. Contrary to this, an unanalyzed
trolley/hoist and chain was installed inside the torus for at least five operating cycles
without being discovered by the licensee. Once informed of the condition by the
inspectors, the licensee did not take prompt corrective actions prior to sealing the torus.
Because this violation was of very low safety significance and was entered in the
CNS-2006-09338, this violation is being treated as an NCV,
consistent with Section
NRC Enforcement Policy: NCV 05000298/2006005-
03, "Failure to Promptly Identify and Correct an Unanalyzed Condition in the Torus."
Enclosure-22-1R22 Surveillance Testing (71111.22) a.Inspection ScopeThe inspectors reviewed the
TSs to ensure thatthe four surveillance activities listed below demonstrated that the SSCs tested were
capable of performing their intended safety functions. The inspectors either witnessed
or reviewed test data to verify that the following significant surveillance test attributes
were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of
- AS [[]]
ME
Code requirements; (12) engineering evaluations, root causes, and bases for returning
tested SSCs not meeting the test acceptance criteria were correct; (13) reference
setting data; and (14) annunciators and alarms setpoints. The inspectors also verified
that the licensee identified and implemented any needed corrective actions associated
with the surveillance testing.*October 17, 2006: Surveillance Procedure 6.2RHR.201, "RHR Power OperatedValve Operability Test (IST)(DIV 2)," Revision 19*October 25, 2006: Surveillance Procedure
- 6.PC. 513, "Main Steam Local LeakRate Tests," Revision 13*November 9, 2006: Surveillance Procedure 6.2
- DG. 302, "Undervoltage LogicFunctional, Load Shedding, and Sequential Loading Test (DIV 2)," Revision 33*November 14, 2006: Surveillance Procedure
- ECCS LeakageWalkdown," Revision 5The inspectors completed four samples. b.FindingsIntroduction: A Green, self-revealing
- NCV was identified regarding inadequatemaintenance procedures for work on safety-related motor-operated valves (
- MOV s).Description: On October 17, 2006, the Division 2 low pressure coolant injection (LPCI)inboard injection valve,
MOV-MO25B, failed to open during a quarterly surveillance
test. This is a normally shut containment isolation valve that has an active safety
function to open in order to provide a flow path for Division 2 of the
- LP [[]]
CI system. It is
also required to establish shutdown cooling using the Division
LPCI inoperable and
performed troubleshooting, which revealed that the drive train in the Limitorque valve
actuator had failed. The helical pinion gear which transfers torque from the drive motor
to the drive train had fallen off the motor shaft, which allowed the motor shaft to spin
Enclosure-23-freely without moving the valve. The licensee implemented immediate corrective actionsto replace the pinion gear in this valve actuator and to retest the valve, both of which
were completed satisfactorily on October 18, 2006.The pinion gear is normally held in place by a shaft key and key-way arrangement thatprevents radial movement and by a set-screw through the gear which lands in a dimple
on the motor shaft to prevent axial movement. The actuator for
MOV-25B is a
Limitorque size SB-3. Limitorque Maintenance Update 89-1 was issued in 1989 to
provide guidance on motor pinion installation, which included methods for locking the
set-screw and staking the pinion key to prevent axial or radial movement of the gear.
MOV-MO25B was last overhauled in 1995 using Maintenance Procedure
7.2.50.16, "Limitorque SB-3 Valve Operator Maintenance," Revision 1, in 1995, which
reflected these recommendations.The licensee documented this condition in Condition Report
CNS-2006-07490 andperformed a root cause analysis. As part of their evaluation, the licensee conducted
extent of condition inspections on a total of 35 safety-related MOV actuators of similar
size. While only one valve (RHR-MOV-MO25B) had failed due to this condition, 10 of
the MOVs showed various levels of degradation on their as-found inspections and were
considered unsatisfactory, while an additional 10 MOVs showed discrepant conditions
that required corrective actions. The following table summarizes the as-found
conditions for these inspections:ValveFunctionInspectionAs-Found ConditionCS-MOV-MO7BCore Spray (CS)
RHR-MOV-MO27ARHR Loop AInjection Outboard
IsolationNotFunctionalPinion and key migrated9/16" off motor shaft. Set-
screw was looseRHR-MOV-31BDrywell Spray AInboard IsolationUnsatKey migrated 1/16" out ofkey-way, set-screw not
landed in dimpleHPCI-MOV-MO15High PressureCoolant Injection
Steam Supply
Inboard IsolationUnsatKey migrated 1/4" out ofkey-way, pinion migrated
1/8" off motor shaft, set-
screw not tightCS-MOV-MO12BCS Pump BInjectionUnsatKey migrated 1/2" out of key-way, set-screw high in lock-
wire groove (not landed in
dimple)RHR-MOV-MO39ARHR Torus CoolingLoop A Outboard
ThrottleUnsatKey migrated 1/2" out of key-way, set-screw not landed
in dimple.
ValveFunctionInspectionAs-Found ConditionEnclosure-24-RR-MOV-MO53AReactorRecirculation
Pump A DischargeUnsatKey migrated 3/8" out ofkey-way, pinion showed
axial movementRR-MOV-MO53BReactorRecirculation
Pump B DischargeUnsatKey migrated 3/8" out ofkey-way, pinion migrated
1/16" off motor shaftRHR-MOV-MO27BRHR Loop BInjection Outboard
IsolationUnsatPinion migrated 1/2" offmotor shaft, set-screw not
landed in dimpleRHR-MOV-MO34BRHR Torus CoolingLoop B Inboard
ThrottleUnsatPinion migrated 1/2" offmotor shaft, set-screw not
landed in dimpleAfter completing these inspections, the licensee concluded that the root cause for theseconditions was a mismatch between the criticality of the task to install MOV motor pinion
gears and the level of detail in the maintenance procedures. This led to various
discrepancies in the installation of the pinion gears, such as the failure to land the pinion
set screw in the motor shaft dimple, and resulted in unacceptable migration of the pinion
gears on the motor shafts. The lack of acceptance criteria for verification of critical
steps and the lack of specific training on pinion gear installation were listed as
contributing causes. The failure of the pinion key in Valve
MOV-MO7B was
appropriately treated as a separate condition by the licensee and was verified to be an
isolated incident. The inspectors reviewed the licensee's root cause analysis, the applicable maintenanceprocedures, and industry operating experience regarding similar MOV failures. Based
on their review, the inspectors concluded that, while the licensee's maintenance
procedures contained all the recommendation from the vendors' maintenance bulletins,
they were not always adequate to ensure the actuator drive train was correctly
assembled. For example, the maintenance procedure contained the applicable steps
for aligning the pinion gear and drilling the set-screw dimple in the motor shaft, but a
procedure note allowed this step to be skipped if a dimple had previously been drilled in
the shaft. This is an acceptable practice unless the pinion gear is replaced with a new
part that may not align sufficiently with the existing dimple to allow the set-screw to
secure the gear to the shaft. The inspectors found that on at least three of the valves
the set-screw misalignment with the dimple was likely due to the use of new parts that
did not align adequately.Corrective actions for this condition included improvements to the maintenanceprocedures, additional training to personnel performing valve actuator maintenance, and
reworking of the degraded actuators to ensure adequate alignment and securing of the
pinion gear assembly.
Enclosure-25-The inspectors also concluded that the licensee's MOV program was not effective inidentifying degraded conditions such as those described above. Generic Letter 96-05,
"Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated
Valves," issued on September 18, 1996, requested that licensees establish a program to
verify on a periodic basis that safety-related MOVs continue to be capable of performing
their safety functions. In response, the licensee ultimately committed to implement an
MOV program, formulated by a consortium of licensed utilities, which consists primarily
of periodic diagnostic valve testing, to determine the need for preventive or corrective
maintenance. The licensee did not include periodic intrusive actuator inspections as a
part of this program. Most of the valves that were determined to be unsatisfactory had
no intrusive work on the actuator in more than 10 years. A total of 21 safety-related
MOVs had some type of discrepant condition that was not detected by diagnostic
testing. The only means available to detect these conditions prior to valve failure was by
intrusive inspections.Analysis: The performance deficiency associated with this finding involved thelicensee's failure to provide adequate instructions for performing safety-related MOV
maintenance. The finding is more than minor because it is associated with the
Mitigating Systems cornerstone attribute of equipment performance and affects the
associated cornerstone objective to ensure the availability, reliability, and capability of
systems that respond to initiating events. Specifically, the performance deficiency
resulted in the failure of Valve
- LP [[]]
CI system inoperable. While other degraded conditions resulted from this
performance deficiency, Division 2 of
- LP [[]]
CI was the only system adversely affected prior
to implementing corrective actions. The Phase 1 worksheet in NRC Manual
Chapter 0609, "Significance Determination Process," was used to conclude that a
Phase 2 analysis was required because the finding represented an actual loss of safety
function of a single train of
- LP [[]]
CI for greater than its Technical Specification allowed
outage time. The inspectors performed a Phase 2 analysis using Appendix A,
"Technical Basis For At Power Significance Determination Process," of NRC Manual
Chapter 0609, "Significance Determination Process," and the Phase 2 worksheet for
Cooper Nuclear Station. The inspectors assumed that Division 2 of
- LP [[]]
CI was
unavailable for 92 days. Additionally, a credit of 1 was used for operator recovery of a
failed train since Valve
MOV-MO25B could have been manually opened to
establish an injection flow path. While not specifically described in a procedure, this
action would be readily accomplished based on a simple diagnosis. These assumptions
resulted in a finding of very low safety significance with the dominant sequence being
low pressure injection with a stuck-open relief valve. These results were validated by a
senior reactor analyst who concluded that they were conservative by a factor of 4 since
the Phase 2 worksheet calculates the annual core damage frequency for exposure
times greater than 30 days, whereas this condition only existed for a quarter of that time
(92 days).Enforcement:
- TS 5.4.1.a requires that written procedures be established, implemented,and maintained covering the activities specified in
RG 1.33, Revision 2, Appendix A,
dated February 1978. RG 1.33, Appendix A, Section 9(a), requires that maintenance
affecting the performance of safety-related equipment should be performed in
Enclosure-26-accordance with written procedures. Contrary to this, Maintenance Procedure7.2.50.16, "Limitorque SB-3 Valve Operator Maintenance," Revision 1, did not contain
adequate instructions to ensure that the motor pinion gear was correctly aligned and
secured to the motor shaft in the actuator for Valve
MOV-MO25B when it was
refurbished in 1995. As a result, the pinion gear migrated off the end of the motor shaft,
resulting in a failure of the valve to operate on October 17, 2006. Because the finding is
of very low safety significance and has been entered into the licensee's CAP as
Condition Report
CNS-2006-07490, this violation is being treated as an
"Inadequate Maintenance Procedure Results in Safety-Related Valve Failure."Cornerstone: Emergency Preparedness1EP6 Drill Evaluation (71114.06) a.Inspection ScopeThe inspectors observed an emergency preparedness drill conducted on December 20,2006. The observations were made in the control room simulator and the emergency
operations facility and concentrated on the training evolution to identify any weaknesses
and deficiencies in classification, notification, and protective action recommendation. In
addition, the inspectors compared the identified weaknesses and deficiencies against
licensee identified findings to determine whether the licensee is properly identifying
deficiencies. Documents reviewed by the inspectors included:*Emergency Plan for Cooper Nuclear Station, Revision 51*Emergency Plan Implementing Procedures for Cooper Nuclear Station
- Emergency Preparedness Drill Scenario for December 20, 2006The inspectors completed one sample. b.FindingsNo findings of significance were identified.2.
- RADIAT [[]]
- ION [[]]
OS)2OS1Access Control to Radiologically Significant Areas (71121.01) a.Inspection ScopeThis area was inspected to assess licensee performance in implementing physical andadministrative controls for airborne radioactivity areas, radiation areas, high radiation
areas, and worker adherence to these controls. The inspectors used the requirements
in
TS as criteria for
determining compliance. During the inspection, the inspectors interviewed the radiation
Enclosure-27-protection manager, radiation protection supervisors, and radiation workers. Theinspectors performed independent radiation dose rate measurements and reviewed the
following items:Performance indicator (PI) events and associated documentation packages reported bythe licensee in the Occupational Radiation Safety cornerstone Controls (surveys, posting, and barricades) of three radiation, high radiation, or airborneradioactivity areasRadiation work permits, procedures, engineering controls, and air sampler locations
Conformity of electronic personal dosimeter alarm setpoints with survey indications andplant policy; workers' knowledge of required actions when their electronic personnel
dosimeter noticeably malfunctions or alarmsBarrier integrity and performance of engineering controls in airborne radioactivity areas
Adequacy of the licensee's internal dose assessment for any actual internal exposuregreater than 50 millirem Committed Effective Dose EquivalentPhysical and programmatic controls for highly activated or contaminated materials(nonfuel) stored within spent fuel and other storage pools Self-assessments and audits related to the access control program since the lastinspection; there were no licensee event reports (LERs) and special reportsCorrective action documents related to access controls
Licensee actions in cases of repetitive deficiencies or significant individual deficiencies Radiation work permit briefings and worker instructions
Adequacy of radiological controls such as, required surveys, radiation protection jobcoverage, and contamination controls during job performance Dosimetry placement in high radiation work areas with significant dose rate gradients
Changes in licensee procedural controls of high dose rate - high radiation areas andvery high radiation areasControls for special areas that have the potential to become very high radiation areasduring certain plant operationsPosting and locking of entrances to all accessible high dose rate - high radiation areasand very high radiation areas
Enclosure-28-Radiation worker and radiation protection technician performance with respect toradiation protection work requirements The inspectors completed 21 of the required 21 samples. b.FindingsInadequate Procedure for Reactor Pressure Vessel (RPV) Refueling PreparationIntroduction: The inspectors reviewed a self-revealing
RPV refueling preparation
was not adequate, resulting in an unplanned airborne radioactivity area. The violation
had very low safety significance.Description: On October 22, 2006, the high efficiency particulate air (HEPA) filter hosebetween the
HEPA filtration unit came apart, creating an
airborne radioactivity area on the refuel floor which alarmed the continuous air monitor
and contaminated five workers. The licensee's refueling procedure allowed the control
room supervisor or shift manager to make changes to the sequence of disassembling
the reactor head in preparation for refueling, but it did not contain any precautions or
limitations to consider the impact of sequence changes on ancillary systems, such as
the
- HE [[]]
PA hose connection to the reactor head vent. Consequently, when the licensee
raised the RPV water level at an earlier stage in the reactor head disassembly process,
the increased temperature and pressure applied to the
- HE [[]]
PA hose caused it to
disconnect from the RPV vent. The licensee's immediate corrective actions were to
evacuate personnel from the refuel floor and begin decontamination of the workers and
the areas involved. The highest Committed Effective Dose Equivalent received by any
of the workers was 8.3 millirem.Analysis: The failure to have an adequate procedure for refueling was determined to bea performance deficiency. The finding was greater than minor because it was
associated with the Occupational Radiation Safety cornerstone attribute of Program and
Process and affected the cornerstone objective to ensure the adequate protection of a
worker's health and safety from exposure to radiation from radioactive materials
because it resulted in unintended internal doses. Because the finding involved
unplanned, unintended dose resulting from conditions that were contrary to NRC
regulations, the finding was evaluated using the Occupational Radiation Safety SDP.
The finding was determined to be of very low safety significance because: (1) it was not
an as low as is reasonably achievable (ALARA) finding, (2) there was no personnel
overexposure, (3) there was no substantial potential for personnel overexposure, and
(4) the finding did not compromise the licensee's ability to assess dose. Additionally,
this finding had a crosscutting aspect in the area of human performance associated withthe component of work control because the licensee failed to coordinate work activities
by incorporating actions to address the impact of the work on different job activities and
communicate, coordinate, and cooperate with each other during activities in which
interdepartmental coordination is necessary to assure appropriate plant and human
performance.
Enclosure-29-Enforcement: TS 5.4.1.a requires written procedures be established, implemented, andmaintained covering the activities in Regulatory Guide 1.33, Revision 2, Appendix A.
Section 2(K) of RG 1.33 requires procedures for preparation for refueling. General
Operating Procedure 2.1.20.3, titled "RPV Refueling Preparation," states in Section 2.5
that the sequence listed in this procedure may be altered at the discretion of the control
room supervisor or shift manager to suit existing plant conditions and time requirements.
On October 22, 2006, the licensee used this procedure to disassemble the reactor head.
However, this procedure was not adequate because it did not provide any precautions
and limitations for modifying the sequence of the procedure or consideration of impacts
to ancillary systems, thus resulting in uptakes of radioactive material by five workers.
This violation was entered into licensees' CAP as Condition Report 2006-7727.
Because this finding is of very low safety significance and was entered into the
licensee's
NRC
Enforcement Policy: NCV 05000298/2006005-05, Technical Specification 5.4.1.a,
"Inadequate Procedure For Reactor Pressure Vessel Refueling Preparation."2OS2ALARA Planning and Controls (71121.02) a.Inspection ScopeThe inspectors assessed licensee performance with respect to maintaining individualand collective radiation exposures
- ALA [[]]
TS as criteria for determining
compliance. The inspectors interviewed licensee personnel and reviewed:Current 3-year rolling average collective exposure
Five outage maintenance work activities scheduled during the inspection period andassociated work activity exposure estimates which were likely to result in the highest
personnel collective exposuresSite-specific trends in collective exposures, plant historical data, and source-termmeasurementsSite-specific
- ALA [[]]
- ALA [[]]
RA work activity evaluations, exposure estimates, and exposure mitigationrequirementsUse of engineering controls to achieve dose reductions and dose reduction benefitsafforded by shieldingRecords detailing the historical trends and current status of tracked plant source termsand contingency plans for expected changes in the source term due to changes in plant
fuel performance issues or changes in plant primary chemistry
Enclosure-30-Radiation worker and radiation protection technician performance during work activitiesin radiation areas, airborne radioactivity areas, or high radiation areas Self-assessments, audits, and special reports related to the
- ALARA [[program since thelast inspectionEffectiveness of self-assessment activities with respect to identifying and addressingrepetitive deficiencies or significant individual deficiencies The inspectors completed 10 of the required 15 samples. b.FindingsNo findings of significance were identified.4.]]
- OTHER [[]]
- ACTIVI [[]]
TIES4OA1PI Verification (71151) a.Inspection ScopeOccupational Radiation Safety CornerstoneOccupational Exposure Control EffectivenessThe inspectors reviewed licensee documents from August 1, 2005, throughSeptember 30, 2006. The review included corrective action documentation that
identified occurrences in locked high radiation areas (as defined in the licensee's TS),
very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel
exposures (as defined in Nuclear Energy Institute (NEI) 99-02). Additional records
reviewed included
- ALA [[]]
RA records and whole-body counts of selected individual
exposures. The inspectors interviewed licensee personnel that were accountable for
collecting and evaluating the PI data. In addition, the inspectors toured plant areas to
verify that high radiation, locked high radiation, and very high radiation areas wereproperly controlled.
NEI 99-02, "Regulatory
Assessment Indicator Guideline," Revision 4, were used to verify the basis in reporting
for each data element.The inspectors completed one sample.
Public Radiation Safety CornerstoneRadiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspectors reviewed licensee documents from August 1, 2005, throughSeptember 30, 2006. Licensee records reviewed included corrective action
documentation that identified occurrences for liquid or gaseous effluent releases that
Enclosure-31-exceeded
- NRC. The inspectors interviewedlicensee personnel that were accountable for collecting and evaluating the
definitions and guidance contained in NEI 99-02, "Regulatory Assessment Indicator
Guideline," Revision 4, were used to verify the basis in reporting for each data element.The inspectors completed one sample.
Mitigating Systems CornerstoneThe
RHR,and cooling water systems were reviewed using Temporary Instruction 2515/169, as
documented in Section
- 4OA 5.2. The inspectors completed five samples. b.FindingsNo findings of significance were identified. 4
OA2 Identification and Resolution of Problems (71152) .1Selected Issue Follow-up Inspection a.Inspection ScopeIn addition to the routine review, the inspectors selected the issues listed below for amore in-depth review. The inspectors considered the following during the review of the
licensee's actions: (1) complete and accurate identification of the problem in a timely
manner; (2) evaluation and disposition of operability/reportability issues;
(3) consideration of extent of condition, generic implications, common cause, and
previous occurrences; (4) classification and prioritization of the resolution of the
problem; (5) identification of root and contributing causes of the problem;
(6) identification of corrective actions; and (7) completion of corrective actions in a timely
manner. Condition Report
HPCI-MOV-MO15), the maximum allowable torque for the valve and
valve actuator were exceeded. Thrust in the closed direction was found to be
73,000 pounds versus the maximum allowable value of 56,000 pounds, and 67,000
pounds of thrust were required to re-open the valve as opposed to the allowable value of
45,000 pounds. An inspection of the motor actuator revealed that the torque switch roll
pin had failed while opening the valve in preparation for the diagnostic test.Valve
MOV-MO15 is equipped with a Limitorque SMB-1 motor actuator. This sizeof actuator is typical of most Limitorque designs in that it is equipped with a torque
switch that de-energizes the actuator motor when the drive train achieves a pre-set
torque value. In addition to preventing damage to the valve and actuator components,
the torque switch ensures reliable operation of the valve by limiting the pull-out torque
required to open the valve. The torque switch is coupled to the drive train by a rack and
pinion arrangement, with the rack being integral to the drive train and the pinion being a
gear on the end of the torque switch shaft. The pinion is secured to the shaft by a pin.
The original Limitorque design specified a hollow roll pin for this application; however, on
March 23, 1994, in a letter titled "Potential 10 CFR 21 Condition," Limitorque notified the
NRC that this hollow roll pin was susceptible to failure especially in valve applicationsrequiring high pull-out torque to unseat the valve. Limitorque made no specific
recommendations in this letter but they stated that the design had been changed to
specify a larger, solid pin of a material less susceptible to shear failure. Based on this
letter, the NRC issued Information Notice 94-49, "Failure of Torque Switch Roll Pins," on
July 6, 1994, to alert licensees to this potential failure mechanism. The licensee evaluated Information Notice 94-49 and the Limitorque letter forapplicability to Cooper Nuclear Station. Valve
MOV-MO15 is susceptible to
thermal binding, and opening the valve may require high pull-out torque; therefore, it
was susceptible to the failure mechanisms discussed in the Limitorque letter.
Nevertheless, the licensee concluded the following:This item is being closed, there are no recommendations and the MUG[Motor-operated Valve Users Group] report states that valves that are
going to be susceptible should have already exhibited failures. CNS
[Cooper Nuclear Station] has not had a failure of this type. Any action
required will be taken when an update to the Part 21 or IN 94-049 are
issued.
Enclosure-33-No updated information was ever issued and, since the licensee had not seen anyfailures in the past, they erroneously concluded that they would see no failures in the
future. No actions were taken to replace the susceptible torque switches with the
improved design.The licensee documented this failure in Condition Report
MOV-MO15 actuator failure was due to their failure to
implement the Limitorque design change in 1995. Corrective actions included
replacement of the failed torque switch with the new design as well as completing an
evaluation to verify that no internal valve damage occurred due to the high torque
applied to the valve. Long-term corrective actions were established to replace the
torque switches in the remaining valve actuators that may be susceptible to this failure
mechanism.Analysis: The performance deficiency associated with this finding involved the failure tocorrect a condition adverse to quality on safety-related MOVs. Specifically, the licensee
failed to replace the torque switch in Valve
MOV-MO15 with an improved design
when they had information from the NRC and the vendor indicating that the existing
design was susceptible to failure. As a result, the torque switch in
MOV-MO15
failed on November 8, 2006.
- HP [[]]
CI was not required to be operable at the time since the
plant was in Mode 5, but this performance deficiency existed for more than 10 years and
included periods of time when
- HP [[]]
CI was required to be operable. The finding is more
than minor because, if left uncorrected, it would become a more significant safety
concern. The finding affected the Mitigating Systems cornerstone. Using the NRC
Manual Chapter 0609, "Significance Determination Process," Phase 1 worksheet, the
finding is determined to have very low safety significance because it did not result in the
actual loss of a safety function. Enforcement:
XVI, "Corrective Action," requires,in part, that measures be established to assure that conditions adverse to quality, such
as defective material and nonconformances, are promptly identified and corrected.
Contrary to this, the licensee was aware that the torque switch in Valve
CFR Part 21 notification
from Limitorque, dated March 23, 1994, and Information Notice 94-49, yet they failed to
replace the switch with a less susceptible switch available from the vendor. Because
the finding is of very low safety significance and has been entered into the licensee's
VI.A of the Enforcement Policy: NCV 05000298/2006005-
06, "Failure to Identify and Correct Nonconforming Conditions in Safety-Related Motor-
Operated Valves." Service Water Strainer FailureIntroduction: The inspectors reviewed a self-revealing, Green NCV regarding the failureto correct a condition adverse to quality. This deficiency resulted in failure of Service
Water Discharge Strainer A.
Enclosure-34-Description: On October 29, 2006, operators discovered that the backwash mechanismon Service Water Discharge Strainer A would not rotate when the strainer was placed
into the continuous backwash mode. A subsequent inspection of the strainer drive train
revealed that a flexible rubber sleeve between the motor gear and a reduction gear had
failed. The rubber sleeve is designed with splined surfaces which mate with the motor
gear and reduction gear. The spline on one end of the rubber sleeve had been stripped,
allowing the motor to spin freely. This was documented in Condition Report
CNS-
2006-08226, which was assigned Significance Category "C" or "broke-fix." A formal
cause determination was not conducted; however, during interviews, the licensee stated
that the failure was caused by damage to the rubber coupling due to improper
reassembly during past maintenance activities. Repeated attempts to align the sleeve
with the drive gears, coupled with age-related embrittlement, most likely weakened the
splines on the sleeve to the point where they failed.The inspectors reviewed Condition Report
CNS-2006-00789, which documented asimilar failure of Service Water Discharge Strainer A on February 1, 2006. This
condition was evaluated by an apparent cause determination that concluded that the
coupling had been improperly reassembled following preventive maintenance on
January 29, 2006. Corrective actions included reassembly of the coupling, which was
accomplished on February 1, 2006, under
WO also required the
replacement of degraded components, as necessary, and indicated that the coupling
gears had been replaced but not the coupling sleeve. The sleeve was approximately
years old when it failed, so it would have been reasonable for the licensee to identify
and correct any age-related degradation during corrective maintenance performed only
months before the failure.Analysis: The performance deficiency associated with this finding involved the failure toidentify and correct a condition adverse to quality. Specifically, SW Discharge Strainer
A failed on October 29, 2006, apparently due to age-related degradation of components
in the motor coupling. This degradation was not identified during corrective
maintenance on February 1, 2006, which required the identification and replacement of
degraded components. The finding is more than minor because it is associated with the
Mitigating Systems cornerstone attribute of equipment performance and affects the
associated cornerstone objective to ensure the availability and reliability of systems that
respond to initiating events. The Phase 1 worksheet in NRC Manual Chapter 0609,
"Significance Determination Process," was used to conclude that a Phase 2 analysis
was required because the findings also increased the likelihood of a loss of service
water initiating event. The assumptions used to perform the Phase 2 and Phase 3
analyses associated with
NRC Integrated
inspection Report 05000298/2006002 bound the assumptions necessary to evaluate this
finding. NCV 05000298/2006002-02 was found to be of very low safety significance;
therefore, this finding is also of very low safety significance. The treatment of this
finding was validated by a senior reactor analyst.The cause of the finding is related to the corrective action component of the crosscuttingarea of problem identification and resolution in that the licensee failed to identify this
issue in a timely manner.
Enclosure-35-Enforcement:
XVI, "Corrective Action," requires,in part, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. Contrary to this, the licensee failed to identify a
condition adverse to quality regarding degradation of the motor coupling in Service
Water Discharge Strainer A. Specifically, corrective maintenance was performed on the
motor coupling on February 1, 2006, which required the replacement of degraded
components as necessary. This maintenance activity failed to identify hardening and
embrittlement of a rubber sleeve in the coupling, resulting in failure 8 months later on
October 29, 2006. Because the finding is of very low safety significance and has been
entered into the licensee's
CR-CNS-2006-08226, this violation
is being treated as an
VI.A of the Enforcement Policy:
NCV 05000298/2006005-07, "Failure to Identify and Correct Degraded Condition on
Service Water Strainer." Operation of Reactor Above Total Core Flow LimitIntroduction: The inspectors identified a Green
TS 5.4.1.a regarding thelicensee's failure to follow procedures for power operation and process monitoring.
Specifically, the licensee operated the reactor above the total core flow limit, contrary to
requirements of General Operating Procedure 2.1.10, "Station Power Changes." Description: On October 8, 2006, the licensee initiated Condition Report
CNS-2006-07255 to document a plant monitoring information system (PMIS) warning alarm for total
core flow above 77.175 million pounds-mass per hour (MLBH). This alarm appears on
the
UFSAR-allowed limit of
77.175 (MLBH), which represents 105 percent of rated core flow. At the time the alarm
was received, the plant was operating near 105 percent of rated core flow to maximize
core thermal power during the coastdown to Refueling Outage
- RE 23.The inspectors questioned the licensee's response to the alarm and the acceptability ofoperating so close to the
UFSAR core flow limit. As a result of the licensee's response
to the question and the inspectors' direct observation of core flow spikes exceeding
77.1
- ML [[]]
BH in the control room, the inspectors asked the licensee to provide the actual
measured core flow data for the previous month.When the licensee analyzed the measured data, they determined that over the previousmonth the plant had been operating above 105 percent rated core flow approximately
percent of the time. The licensee identified that this represented an unanalyzed
condition and that the plant had been operated outside of the established power-to-flow
map in violation of General Operating Procedure 2.1.10, "Station Power Changes,"
Revision 69. Step 2.11 of Procedure 2.1.10 directed that the "Reactor should be
operated within constraints of Power-To-Flow Map." Attachment 1 to Procedure 2.1.10
is the current power-to-flow map and shows the maximum allowable core flow to be
105 percent (77.175
- ML [[]]
BH). The licensee reduced core flow until all measured spikes
were below the limit and implemented a night order to maintain core flow below
105 percent of rated flow using all available instrumentation. Condition Report
CNS-
2006-07255 was updated to reflect the procedural violation.
Enclosure-36-In order to analyze this condition, the licensee contacted the nuclear steam systemsupply vendor. The vendor provided the licensee a set of conditions during which the
plant could be operated with spikes above the 105 percent rated core flow limit but with
time-averaged core flow below the limit. The licensee determined that, for the time
period in question, these conditions were satisfied and that no damage to core internal
components had occurred.Analysis: The performance deficiency associated with this finding involved thelicensee's failure to follow the requirements of General Operating Procedure 2.1.10,
"Station Power Changes." The finding is more than minor because it is associated with
the Barrier Integrity cornerstone attribute of human performance (procedural adherence)
and it affects the associated cornerstone objective to provide reasonable assurance that
physical design barriers, such as fuel cladding, protect the public from radionuclide
releases caused by accidents or events. Using the NRC Manual Chapter 0609,
"Significance Determination Process," Phase 1 worksheet, the finding is determined to
have very low safety significance because it only had the potential to affect the fuel
cladding barrier.This finding has a crosscutting aspect in the area of human performance in that thelicensee did not effectively communicate expectations regarding work practices to
operators for the control of key parameters such as total core flow. Enforcement:
- TS 5.4.1.a requires that written procedures be established, implemented,and maintained covering the activities specified in
RG 1.33, Revision 2, Appendix A,
dated February 1978. RG 1.33, Appendix A, Section 2 (g), requires that procedures be
established and followed for power operation and process monitoring. General
Operating Procedure 2.1.0, "Station Power Changes," Revision 69, provided specific
limits for core flow on a power-to-flow map. Contrary to this procedural requirement, the
plant was operated at greater than 105 percent of rated core flow for a significant
portion of September and October 2006. Because the finding is of very low safety
significance and has been entered into the licensee's
CNS-2006-07255, this violation is being treated as an NCV consistent with
Section
NCV 05000528/2006005-08, "Operation of
Reactor Above Total Core Flow Limit.".2Semiannual Trend Review a.Inspection ScopeThe inspectors completed a semiannual trend review of repetitive or closely relatedissues that were documented in corrective action documents, corrective maintenance
documents, and the control room logs to identify trends that might indicate the existence
of more safety significant issues. The inspectors' review covered the 12-month period
between November 2005 and November 2006. When warranted, some of the samples
expanded beyond those dates to fully assess the issue. The inspectors reviewed the
following issues:
Enclosure-37-*Personnel contamination events*Fire door degradation
- Sump pump failures
- Drawing discrepancies
- Crane and hoist failuresThe inspectors compared their results with the results contained in the licensee's routinetrend reports. Corrective actions associated with a sample of the issues identified in the
licensee's trend report were reviewed for adequacy. Documents reviewed by the
inspectors are listed in the attachment. b.FindingsNo findings of significance were identified..3Radiological Protection Problem Identification and Resolution a.Inspection ScopeThe inspectors evaluated the effectiveness of the licensee's problem identification andresolution process with respect to the following inspection areas:Access Control to Radiologically Significant Areas (Section
ALARA Planning and Controls (Section 2OS2) b.FindingsNo findings of significance were identified. .4Heat Sink Performance Problem Identification and Resolution a.Inspection ScopeThe inspectors evaluated several condition reports, including root cause and apparentcause analyses, related to the performance of the service water system and the ultimate
heat sink. The inspectors evaluated corrective actions related to the following specific
items:*Control of Asiatic clams and zebra mussels*Loss of the zurn strainers The inspectors performed this evaluation by review of the corrective action programdocuments, review of records, and interviews with licensee personnel. b.FindingsNo findings of significance were identified.
Enclosure-38-4OA3Event Follow-up (71153) .1Fire in Reactor Building a.Inspection ScopeThe inspectors responded to the plant on November 11, 2006, due to the declaration ofa Notice of Unusual Event (NOUE) in response to a small fire in the reactor building.
The inspectors verified that the licensee was taking the appropriate actions in
accordance with their emergency plan and station firefighting procedures. Following the
event, the inspectors toured the area to assess the damage and potential impacts on
other plant equipment. The followup inspection also reviewed the cause of the fire and
the licensee's corrective actions. b.FindingsIntroduction: A Green, self-revealing finding was identified regarding the inadequatedesign and installation of heat tracing on the standby liquid control (SLC) system, which
resulted in a small fire in the reactor building.Details: At 5:16 a.m. on November 11, 2006, control room operators received a reportof sparks and small flames coming from a heat trace junction box on the SLC system.
This portion of the SLC system is located on the 976 foot elevation in the reactor
building. The control room entered Emergency Procedure 5.4FIRE, "General Fire
Procedure," Revision 14, and activated the station fire brigade. The reactor building
station operator also reported to the scene and discharged a dry chemical fire
extinguisher onto the junction box, which extinguished the flames. The station operator
reported his actions to the control room and the fact that the junction box was still
arcing. As directed by the control room, the operator opened two breakers on Lighting
Panel MPR1, which de-energized the heat trace and stopped the arcing. Shortly
afterward, the fire brigade arrived on the scene, conducted a thorough search of the
area to verify that the fire had not spread to adjacent areas, and declared the fire out at
5:33 a.m. The control room appropriately declared an
- NO [[]]
UE at 5:30 a.m. due to a fire
in the protected area lasting longer than 10 minutes. The
- NO [[]]
UE was exited at 5:58 a.m.
Damage was limited to approximately 10 inches of the exposed heat trace cable that
burned.During the event followup inspection, the inspectors questioned why the breaker for theheat trace had not tripped due to the fault, which caused the arcing and sparking. The
heat trace for this portion of the system is supplied by a 20 amp breaker from a 120 volt
ac lighting panel. In response, the licensee referred the inspectors to a section of the
heat trace vendor manual which stated:If the heating cable is improperly installed or physically damaged . . .sustained arcing or fire could result. If arcing does occur, the fault current
may be too low to trip conventional circuit breakers.
Enclosure-39-Raychem, the U.S. National Electrical Code, and the Canadian ElectricalCode require both ground-fault protection of equipment and a grounded
metallic covering (usually braid) on all heating cables.This section of heat trace was installed in 1994 and had no ground-fault protection.
The licensee documented this event in Condition Report
CNS-2006-09006 andperformed a root cause analysis. The licensee concluded that the fire had been caused
by the failure to install the heat trace in accordance with the vendors' recommendations.
In addition to the use a of ground-fault protected circuit, the vendor recommended
periodic measurement of heat trace insulation resistance to detect age-related
degradation of the insulation. The licensee did not routinely perform this type of
monitoring. Corrective actions included replacement of the damaged heat trace and
installation of a ground-fault interrupter on the circuit. In addition, maintenance
procedures were revised to periodically check heat trace insulation resistance values.
The licensee found similar conditions on other heat trace circuits throughout the plant
and has established corrective actions to address those conditions as well.Analysis: The performance deficiency associated with this finding involved thelicensee's failure to install heat trace in accordance with vendor recommendations,
which resulted in a fire in the
SLC heat trace is not safety-related,
but it is required to support operability of the SLC system; therefore, this finding is more
than minor because it is associated with the Mitigating Systems cornerstone attribute of
design control and affects the associated cornerstone objective to ensure the
availability, reliability, and capability of the SLC system, which is required to respond to
initiating events, such as anticipated transients without scrams. Using the NRC Manual
Chapter 0609, "Significance Determination Process," Phase 1 worksheet, the finding is
determined to have very low safety significance because it did not result in a loss of
safety function for the
"Failure to Implement Vendor Recommendations Results in a Fire." .2(Closed)
- RHR Loop B Injection Valve Failure due to IncorrectPinion Gear Installation in Motor OperatorOn October 17, 2006, during surveillance testing, the
RHR-MOV-MO25B, failed to open remotely from the control room. After troubleshooting the
valve, the licensee concluded that it failed to operate because the motor pinion gear in
the Limitorque motor actuator had migrated off the motor shaft. The licensee also
concluded that this most likely occurred during the last successful valve stroke in July
2006, which rendered Loop B inoperable for 92 days. The TS-allowed outage time for
one emergency core cooling train is 7 days. The root cause and corrective action
associated with this condition are discussed further in Section 1R22. The enforcement
aspects of this issue are discussed in Sections 1R22 and 4OA7. This item is closed.
Enclosure-40-4OA5Other Activities (71153).1(Closed) Temporary Instruction 2515/169: Mitigating Systems PerformanceIndex (MSPI) Verification a.Inspection ScopeThe inspectors sampled licensee data to verify that the licensee correctly implementedthe
- MS [[]]
PI guidance for reporting unavailability and unreliability of the monitored safety
systems. The monitored systems included the emergency alternating current (EAC)
power system,
and cooling water systems (SW). The inspectors reviewed operating logs, limiting
condition of operation logs, maintenance records, condition reports, surveillance test
data, and the maintenance rule database to verify that the licensee properly accounted
for planned unavailability, unplanned unavailability, and equipment failures. The
inspectors identified a number of errors in the baseline unavailability figures and the
reported data for the second quarter of 2006. The licensee reperformed the affected
PI threshold changes resulted from these errors.
The results of the inspectors' efforts are documented below. Documents reviewed by the inspectors are listed in the attachment. b.Findings
- 1.F or the sample selected, did the licensee accurately document the baselineplanned unavailability hours for the
MSPI systems?Not in all cases. The inspectors validated the baseline planned unavailabilityhours for each of the five monitored systems and identified one error in the
reported baseline planned unavailability data.For the
MSPI Basis Document on June 27, 2006, to add
several hundred hours of previously unrecognized unavailability. This change
was made due to the discovery of a latent design deficiency discovered in April
2006. In a corrective action response to Condition Report
the licensee evaluated that the diesel generator voltage regulators would not
have been capable of supplying essential safeguard features electrical loads if a
loss of offsite power/loss of coolant accident occurred while the diesel generator
was in parallel with the grid for testing. As a result, the licensee considered the
diesel generators to have been unavailable during parallel operations and
documented an additional 211 hours0.00244 days <br />0.0586 hours <br />3.488757e-4 weeks <br />8.02855e-5 months <br /> of planned unavailability against each EDG
from the introduction of the condition in 1998 through April 21, 2006. During the
inspection, the inspectors discovered that the loss of offsite power/loss of coolant
accident function is not a monitored function in
- MS [[]]
PI, and as such these hours
should not have contributed to the baseline planned unavailability. The licensee
Enclosure-41-plans to correct this discrepancy during a revision to the
- MS [[]]
PI Basis Documentin the next quarter. The licensee has documented this discrepancy in Condition
Report
- 2.F or the sample selected, did the licensee accurately document the actualunavailability hours for the
- MSPI systems?Not in all cases. The inspectors identified the following examples of inaccurateaccounting of system unavailability:*In the
Panel," from unavailability monitoring based on the availability of an operator to
restore control room control of the system upon demand. The inspectors
determined that this was not in accordance with the guidance in NEI 99-02,
"Regulatory Assessment Performance Indicator Guideline." On page F-6 of
NEI 99-02, Revision 4, guidelines are provided for considering a monitored
function available during testing. One of those criteria is that restoration actions
taken by operators "must be uncomplicated (a single action or a few simple
actions)." The intent of this paragraph is to allow licensees to take credit for
restoration actions that are virtually certain to be successful (i.e., probability
nearly equal to 1) during accident conditions. Based on a review of the
procedure and observation of the test by the inspectors, the inspectors
determined that this criteria was not satisfied. The licensee reviewed the
procedure and came to the conclusion that the treatment of
- HP [[]]
CI as available
during the performance of
- 6.HP [[]]
CI.102 on April 26, 2006, was inappropriate and
that the second quarter
HPCI unavailability figures under-reported
actual
MSPI-HPCI baseline unavailability
numbers will also require reassessment to include the performance of this test
each cycle. The licensee documented this discrepancy in
CNS-2006-10488.*On May 3, 2006, the licensee performed Surveillance Procedure 6.1DG.104,"Diesel Operability Test With Isolation Switches in Isolate (Div 1)." During the
performance of this test, the station entered an unanticipated orange on-line risk
window due to the unforseen unavailability of both Diesel Generator 1 and the
Emergency Station Service Transformer. Despite the Orange risk window
recognized by operations, the inspectors identified that the system engineer did
not recognize this test as an EAC unavailability window during document review
in preparation for submitting the second quarter
- 2006 MS [[]]
PI data. The licensee
recognized this human error and documented the discrepancy in Condition
Report
unavailability index was under-reported. The licensee documented this
discrepancy in Condition Report
CNS-2006-10336. As a result of the error,
the licensee submitted a PI correction data file and determined that the
Enclosure-42-unavailability index contribution to
SW changed from 9E-9 to 4.7E-8. The licensee documented
this discrepancy in Condition Report
- 3.F or the sample selected, did the licensee accurately document the actualunreliability information for each
- MSPI monitored component?Not in all cases. The inspectors identified several examples of errors in thecalculated unreliability index.*The inspectors identified a mathematical error in the
RCIC system. Section 1.4.F on page 24 of the Basis Document
demonstrates estimated demand and run hour figures for the monitored
components in the
- RC [[]]
IC system. The table documented an estimated demand
frequency of 1.3 demands per quarter for the
- RC [[]]
IC turbine. The text at the top
of the page estimated that the
- RC [[]]
IC turbine runs for approximately 30 minutes
for each test (this number was validated by the inspector by reviewing operating
logs). The documented estimate for quarterly run hours was incorrectly
calculated as 1.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> per quarter (versus 1.3 x .5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> = 0.65 hours7.523148e-4 days <br />0.0181 hours <br />1.074735e-4 weeks <br />2.47325e-5 months <br /> per
quarter). This demand estimate is an input into the calculation of the unreliability
index component of
- MS [[]]
PI. The licensee documented this discrepancy in
Condition Report
CNS-2006-10488.*In the tabulation of baseline demands and run hours for SW systemcomponents, the licensee used estimated figures based on historical averages
(as allowed by
requires that estimated demand information be updated when it differs from
actual demand data by greater than 25 percent. Based upon a review of 6
months of operating data, the inspectors identified that the estimated test
demands for the SW pumps was 25 percent greater than the actual number of
test demands. The inspectors noted that the licensee had written a notification
to create a repetitive task to evaluate the validity of the demand estimates, but
the task had yet to be defined or performed. These demand estimates are an
input to the calculation of the unreliability index component of
- MS [[]]
PI. The
licensee has documented this discrepancy in Condition Report
CNS-2006-
10488.
- 4.D id the inspector identify significant errors in the reported data, which resulted ina change to the indicated index color? Describe the actual condition andcorrective actions taken by the licensee, including the date when the revised
PIinformation was submitted to the NRC.No discrepancies were identified in the reported data which resulted in a changeto the indicated color.
Enclosure-43-
- 5.D [[id the inspector identify significant discrepancies in the Basis Document whichresulted in: (1) a change to the system boundary; (2) an addition of a monitoredcomponent; or (3) a change in the reported index color? Describe the actualcondition and corrective actions taken by the licensee, including the date of whenthe Basis Document was revised.No such issues were identified.4]]
OA6Management MeetingsOn October 17, 2006, the inspectors conducted a telephonic exit to discuss the resultsof the heat sink inspection with Mr. J. Roberts, Director, Nuclear Safety and Assurance,
and other members of the licensee staff. The inspectors returned proprietary
information examined during the inspection to the licensee. Licensee management
acknowledged the inspection results.On November 3, 2006, the inspectors presented the occupational radiation safetyinspection results to Mr. S. Minahan, General Manager of Plant Operations, and other
members of the licensee's staff who acknowledged the findings. The inspectors
confirmed that proprietary information was not provided or examined during the
inspection.Additionally, on November 14, 2006, after NRC management reviews, the healthphysics inspectors re-exited the issues identified during the inspection with Mr. D. Oshlo,
Radiation Protection Manager, and other members of the licensee's staff who
acknowledged the findings.On December 12, 2006, the inspector conducted an exit meeting to present theinspection results regarding inservice inspection activities to Mr. S. Minahan, General
Manager of Plant Operations, and other members of his staff who acknowledged the
findings. The inspector confirmed that the proprietary information reviewed was
returned to the licensee prior to the end of the inspection.On January 3, 2007, the inspector presented the inspection results from the biennialoperator requalification inspection to Mr. S. Minahan, General Manager of Plant
Operations, and other members of licensee management. The licensee acknowledged
the findings that were presented. The inspector confirmed with the licensee that no
proprietary information was received by the inspector during the inspection.On January 9, 2007, the NRC resident inspectors presented the results of the inspectionactivities to Mr. S. Minahan and other members of his staff who acknowledged the
findings. The inspectors confirmed that proprietary information was not disclosed in this
inspection report.
Enclosure-44-4OA7Licensee-Identified ViolationsThe following violations of very low significance (Green) were identified by the licenseeand are violations of
LPRM) removal and installation, Nuclear
Performance Procedure 10.29, step 2, refers to the vendor's procedure for
bending the
- LP [[]]
RM prior to storage in the spent fuel pool. Vendor Procedure
83A5614, Section 7, step 1, states to lower the elevator with a hand winch until it
contacts the hardstop or the cable goes slack (lowest possible position). During
the night shift of October 27, 2006, the elevator of the bender was not left in the
lowest possible position. A crew change occurred, and the fact that the bender
was not in the lowest possible position was not turned over to the arriving crew.
Contrary to the procedure, the arriving crew commenced bending the
- LP [[]]
RM,
which resulted in one leg of the
- LP [[]]
RM being shorter than the other and the
irradiated detectors being closer to the surface of the water than expected.
Consequently, when the
- LP [[]]
RM was moved through the transfer canal to the
spent fuel pool and raised to clear the lip of the transfer canal, the dose rates at
the surface of the water rose from 100 millirem per hour to 1,700 millirem per
hour. Radiation Protection personnel covering the job identified the increase in
dose rates and requested that the
- LP [[]]
RM be lowered in the water. At the same
time, four electronic dosimeter alarms were received. The workers placed the
- LP [[]]
RM in a safe condition by completing the evolution and then exited the area.
Using the Occupational Radiation Safety SDP, the inspectors determined that
the finding was of very low safety significance because it was not an
- ALA [[]]
finding, there was no overexposure or substantial potential for an overexposure,
and the ability to assess dose was not compromised. The licensee documented
this event in Condition Report
- TS 3.5.1 allows one train of emergency core cooling to be inoperable for up to7 days. Contrary to this,
RHR Loop B was inoperable for 92 days due to a failure
of the motor actuator on the Loop B injection valve (RHR-MOV-MO25B). This
was identified by the licensee during quarterly inservice testing of the valve and
was entered into the corrective action program as Condition Report
CNS-
2006-07490. The licensee completed corrective maintenance on the motor
actuator on October 18, 2006, and successfully re-tested the valve. This finding
was of very low safety significance as discussed in Section 1R22.*TS 5.4.1.a requires that written procedures be established, implemented, andmaintained covering the activities specified in RG 1.33, Revision 2, Appendix A,
dated February 1978. RG 1.33, Appendix A, Section 9(a), requires that
maintenance affecting the performance of safety-related equipment should be
performed in accordance with written procedures. Maintenance Procedure
7.2.50.13, "Limitorque SB-0 Valve Operator Maintenance," Revision 0, required
the use of a 4140 stainless steel motor pinion key. Contrary to this, during an
overhaul of the motor actuator for Valve
MOV-MO7B in 1993, a key was
Enclosure-45-fabricated onsite from material other than 4140 stainless steel. An inspection ofthe actuator on November 11, 2006, showed that this key had failed. The valve
remained functional despite this failure and there was no adverse impact to the
core spray system. The licensee documented this as Condition Report
CNS-
2006-08917 and replaced the failed key with one made of 4140 stainless steel.ATTACHMENT:
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- INFORM [[]]
- POINTS [[]]
- OF [[]]
- CONTAC [[]]
TLicensee PersonnelT. Bahensky, System EngineerR. Beilke, Chemistry Manager
D. Buman, Systems Engineering Division Manager (Acting)
K. Chambliss, Operations Manager
R. Dyer, Heat Exchanger Program Engineer
J. Dykstra, Electrical Engineering Program Supervisor
R. Edington, Chief Nuclear Officer
T. Erickson, System Engineer
R. Estrada, Corrective Actions Manager
J. Flaherty, Licensing
P. Fleming, Licensing Manager
J. Florence, Simulator Supervisor
S. Freeborg, Response Team Lead
K. Gardner, Supervisor, Radiation Protection
J. Gren, System Engineer
G. Hadley, System Engineer
T. Hottovy, Director of Engineering (Acting)
T. Huff, Maintenance Rule Coordinator
G. Kline, Director, Engineering
J. Larson, Supervisor, Quality Assurance
M. McCormack, Electrical Systems/I&C Engineering Supervisor
E. McCutchen, Senior Licensing Engineer, Regulatory Affairs
M. Metzger, System Engineer
S. Minahan, General Manager of Plant Operations
A. Mitchell, Manager, Design Engineering
R. Noon, Root Cause Team Leader, Corrective Actions
D. Oshlo, Manager, Radiation Protection
J. Roberts, Director, Nuclear Safety and Assurance
A. Sarver, Balance of Plant Engineering Supervisor
T. Shudak, Fire Protection Program Engineer
T. Stevens, Supervisor, Mechanical Engineering
C. Sunderman, Supervisor, Radiation Protection
K. Thomas, Mechanical Programs Supervisor
NRCS. Schwind, Senior Resident InspectorN. Taylor, Resident Inspector
AttachmentA-2LIST
- OF [[]]
- ITEMS [[]]
- AND [[]]
- NCVM edical Certification and Monitoring of Personnel RequiringOperator Licenses for Nuclear Power Plants05000298/2006005-02
NCVFailure to Follow Work Instructions
05000298/2006005-03NCVFailure to Promptly Identify and Correct an UnanalyzedCondition in the Torus05000298/2006005-04
NCVInadequate Procedure For RPV Refueling Preparation
05000298/2006005-06NCVFailure to Identify and Correct Nonconforming Conditions inSafety-Related
NCVOperation of Reactor Above Total Core Flow Limit
- LERRHR Loop B Injection Valve Failure due to Incorrect PinionGear Installation in Motor OperatorLIST
- OF [[]]
- REVIEW [[]]
EDSection 1R07: Biennial Heat Sink Inspection (71111.07B, 71152B)Procedures2.2.3.1, "Traveling Screen, Screen Wash, and Sparger System," Revision 583.10, "Erosion/Corrosion Program," Revision 11
3.30, "Macroscopic Biological Fouling Organism Sampling," Revision 5
3.34, "Heat Exchanger Program," Revision 8
6.1SW.101, "Service Water Surveillance Operation (DIV 1) (IST)," Revisions 18, 19, and 20
AttachmentA-36.2SW.101, "Service Water Surveillance Operation (DIV 2) (IST)," Revisions 18, 20, and
IST)," Revisions 13C2, 14,and 156.1SWBP.101, "RHR Service Water Booster Pump Flow Test and Valve Operability Test(DIV 1)," Revisions 10, 11, 12, and 146.2SWBP.101, "RHR Service Water Booster Pump Flow Test and Valve Operability Test(DIV 2)," Revisions 11, 12, and 136.1REC.101, "REC Surveillance Operation (IST) (DIV 1)," Revisions 7 and 8
6.2REC.101, "REC Surveillance Operation (IST) (DIV 2)," Revisions 7 and 8
REC Motor-Operated Valve Operability Test (IST)," Revisions 13C2, 14, and 15
7.2.42.1, "REC Heat Exchanger Maintenance," Revision 6
7.2.42.2, "RHR Heat Exchanger Maintenance," Revision 6
13.15.1, "Reactor Equipment Cooling Heat Exchanger Performance Analysis," Revision 24
13.17, "Residual Heat Removal Heat Exchanger Performance Testing," Revision 19
13.17.1, "Residual Heat Removal Heat Exchanger
- DAS Based Performance Testing,"Revision 613.17.2, "Thermal Performance Test Procedure For Reactor Heat Removal Heat Exchangers,"Revision 0Drawings
MISC-65, "Turning Vanes at Intake Structure Guide Wall - Plan Layout and Details,"Revision N00Plan and Profile Drawings, "Nebraska Public Power District River Intake Structure River BottomElevation Data - Brownville, Nebraska," Sheets 1 - 4, dated July 12, 2006CalculationsNEDC 93-184, "RHR Heat Exchangers and Thermal Performance Tube Plugging Margin,"Revision 1
AttachmentA-4NEDC 94-021, "REC-HX-A and
HX-B Maximum Allowable Accident Case Fouling,"Revision 4Maintenance Instructions2471325409Work Orders44915234274402
4361453
4334505
4458080Corrective Action Documents2004-033772004-063922004-070222004-074092004-075682004-076882005-013322005-022922005-026852005-030832005-031982005-03212
2005-032132005-033822005-035492005-038592005-038742005-03883
2005-038552005-041562005-049562005-050412005-056502005-06176
2005-071522005-071882005-071892005-077422005-077722005-07810
2005-078302005-084112005-084132005-084372005-084862005-08490
2005-085762005-085932005-088522005-088542005-089362005-08945
2005-092982005-093012005-093302005-093712005-093732005-09397
2006-000202006-002002006-005102006-007672006-007912006-00926
2006-009402006-011672006-011722006-011842006-013492006-01384
2006-016462006-016952006-018722006-019152006-019162006-01939
2006-022032006-022692006-024862006-026342006-029152006-03206
2006-033012006-039992006-043422006-047752006-052992006-05327
2006-066MiscellaneousCooper Nuclear Station - Service Water Options AnalysisEPRI NP-7552, "Heat Exchanger Performance Monitoring Guidelines," December 1991
AttachmentA-5Updated Final Safety Analysis Report, Sections 6.0, "Reactor Equipment Cooling System,"and 8.0, "Service Water and
- RHR Service Water Booster System" Generic Letter 89-13, "Service Water System Problems Affecting Safety-Related Equipment,"July 18, 1989Generic Letter 89-13, Supplement 1, "Service Water System Problems Affecting Safety-RelatedEquipment," April 4, 1990Letter
- LQA 8100180, "IE Bulletin 81-03, 'Flow Blockage of Cooling Water to Safety SystemComponents by Corbicula sp. and Mytilus sp.,'" dated May 29, 1981Letter
- CN [[]]
SS907024, "Response to Generic Letter 89-13," dated January 29, 1990
Letter
NSD920007, "Completion of Generic Letter 89-13 Actions," dated January 9, 1992
Letter
NRC Inspection ReportNos. 97-07 and 97-12," dated January 28, 1998Inspection Report 05000298/1997012, dated October 3, 1997
Condition Adverse Quality 97-0742
Condition Adverse Quality 97-1153
Resolve Condition Report 2001-0529
Significant Condition Adverse Quality 97-0742
Inspection Report 05000298/2005015, dated April 25, 2006
Final Report Corbicula (Asiatic Clams) Monitoring and Mitigation Service Water SystemEvaluation Nebraska Public Power District Cooper Nuclear Station, June 2006Structural Integrity Associates Report
IE Bulletin 81-03, "Flow Blockage of Cooling Water to Safety System Components by Corbiculasp. (Asiatic Clam) and Mytilus sp. (Mussel)," dated April 10, 1981Inservice tests for REC pumps, service water booster pumps and valves, and service waterpumps and valves from the 3rd Quarter 2004 throug the 2nd Quarter 2006
AttachmentA-6Erosion/Corrosion Summary Report Sections for Service Water for
COR002-19-02, "Ops Reactor Equipment Cooling," Revision 19
Lesson Plan COR002-27-02, "Ops Service Water," Revision 27
REC Heat Exchangers A and B Eddy Current Tests
Last three
REC heat exchanger test results
Selected Service Water System, Reactor Equipment Cooling Water, and Heat ExchangerProgram monthly health reportsSelf-Assessment
- SA -03-034, "Heat Exchanger Generic Letter 89-13 Program,"dated September 11, 2003Engineering Evaluation 03-003, "Reconstitute and define the basis of the Service Water PumpDischarge Strainers
SW-STNR-A, -B with respect to impact of debris size on any affected
- SW components during Zurn Strainer bypass," Revisions 0 and 2Classification Evaluation Package 97-0001, "SW &
SW Pump Suctions During theCleaning of E-Bay" Vendor Manual 66-31-74, RHR Heat Exchangers
Vendor Manual 68-28-1, Turbine Building and Reactor Building Heat ExchangersSection 1R08: Inservice Inspection Activities (71111.08)ProceduresNumberTitleRevision54-ISI-837-08Ultrasonic Through Wall Sizing of Piping Welds854-ISI-835-10Ultrasonic Examination of Ferritic Piping Welds10
54-ISI-836-10Ultrasonic Examination of Austenitic Piping Welds10
54-ISI-270-44Wet or Dry Magnetic Particle Examination44
54-ISI-147-01Ultrasonic Examination of Thickness Measurement Using Pulse-Echo Techniques154-ISI-135-08Linearity and Beam Spread Measurements8
AttachmentA-754-ISI-136-04Procedure for the Ultrasonic Examination of Vessels Not Greaterthan 2.0 Inches in Thickness454-ISI-30-04Written Practice for the qualification and Certification of
ISI-363-03Remote Underwater In-Vessel Visual Inspection of ReactorPressure Vessel Internals, Components, and Associated
Repairs, in Boiling Water Reactors 354-ISI-366-10VT-1 and
CNS Operations Manual - Maintenance Procedure - "ASMECategory F-A Component Supports Examination and
Adjustments14Fourth 10-Year Interval Inservice Inspection Request for ReliefNumberTitleDate R1-15Examination of Peripheral Control Rod Drives02/23/06PR-04System Pressure Test of the Reactor Vessel HeadFlange Lead Detection Line 02/23/06PR-06Buried Portions of Service Water Piping02/23/06Visual ExaminationsReportComponentSummaryVT-F06-007HPCI-MP-SI,
MSH-109, Main Steam Variable SpringFI.20.C.0028Surface ExaminationsReportComponentSummaryMT-F06-001HPID-CC-5, StanchionC3.20.002
AttachmentA-8PT-F06-001CRD-02-31-1,
- CI. 20.0001UT-F06-122MSC-BJ-35X, Main Steam Elbow to PipeB9.11.0093.RIUT-F06-123MSC-BJ-35X, Main Steam Elbow to PipeB9.11.0093.RICondition ReportsCR-CNS-2005-02834CR-CNS-2005-02847
- CR -CNS-2005-6632CR-CNS-2006-0297CR-CNS-2006-1066CR-CNS-2006-1439CR-CNS-2006-3741CR-CNS-2006-4003CR-CNS-2006-4057CR-CNS-2006-4067
CNS-2006-8076CR-CNS-2006-8134CR-CNS-2006-8310
AttachmentA-9ProceduresNumberTitleRevision2.1.20.3RPV Refueling Preparation (Wet Lift of Dryer andSeparator)172.0.1.1Conduct of Infrequently Performed Tests orEvolutions410.29LPRM and
- RAD [[]]
- CR -CNS-2006-0297CR-CNS-2006-1066CR-CNS-2006-1429CR-CNS-2006-1439CR-CNS-2006-3741CR-CNS-2006-4003CR-CNS-2006-4057CR-CNS-2006-4067
- CNS -2006-6632CR-CNS-2006-7860CR-CNS-2006-7965CR-CNS-2006-8501Audits and Self-AssessmentsRadiation Protection Department On-Going Assessment Report 1Q2006Radiological Department On-Going Assessment Report 2Q2006Focused Self-Assessment
- ALARA [[]]
- PLANNI [[]]
- NG [[]]
- AND [[]]
- CONTRO LSRadiation Work PermitsRWP 2006-073RWP 2006-145RWP 2006-408RWP 2006-412RWP 2006-413RWP 2006-425RWP 2006-433RWP 2006-436
- CNS [[]]
- ALA [[]]
- ALA [[]]
ALARA Planning and Controls15
AttachmentA-10ALARA Packages2006AL-04,
AL-09, Valves
2006AL-18, Scaffold Activities in Drywell
PI Verification (71151)Procedures0-PI-01Performance Indicator Program, Revision 19Section 1R11.1: Licensed Operator Requalification (71111.11B)ProceduresNumberTitleRevisionNTP 4-1Training Material Development and Revision32
NTP 4-2Examination Development18
NTP 5-2Examination26
NTP 5.3Remediation19
- OTP 804Requalification training and Examination ScenarioDevelopment14OTP 805Licensed Operator Requalification Annual-BiennialExamination
OTP 809Operator Requalification ExaminiationAdministration13OTP 810Operations Department Examiniation Security6TQD 0265Licensed Operator Requalification Program3
TPP 0201Licensed Operator Requalification Program2
AttachmentA-11MiscellaneousVarious medical records of licensed operatorsVarious Simulator Scenarios
Various Job Performance Measures
Current listing of Simulator deficiencies (July 2006)
Current list of simulator/plant differences (July 2006)
Remediation programs for various operatorsLIST
- OF [[]]
- ACRONY MSALARAas low as reasonably achievableANSI/ANSAmerican National Standards Institute/American Nuclear Society
- ASM [[]]
EAmerican Society of Mechanical Engineers
- CF [[]]
RCode of Federal Regulations
EACemergency alternating current
EDGemergency diesel generator
- HE [[]]
- HP [[]]
CIhigh pressure coolant injection
I&Cinstrumentation and control
- LP [[]]
- LP [[]]
- ML [[]]
BHmillion pounds-mass per hour
- MS [[]]
PImitigating systems performance indicator
NCVnoncited violation
- NE [[]]
- NOU [[]]
ENotice of Unusual Event
- RC [[]]
ICreactor core isolation cooling
RECreactor equipment cooling
RGRegulatory Guide
RHRresidual heat removal
RPVreactor pressure vessel
SDPsignificance determination process
SLCstandby liquid control
SSCstructure, system, and component
SWservice water
- UFSA [[]]
RUpdated Final Safety Analysis Report