ML19309B215: Difference between revisions

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   ,      10 I 3 l Inot be demonstrated operable per TS Table 4.2-1.                                                        No hazard existed.                                                  I 1016IISee attachment for details.                                                                                                                                                      I I
   ,      10 I 3 l Inot be demonstrated operable per TS Table 4.2-1.                                                        No hazard existed.                                                  I 1016IISee attachment for details.                                                                                                                                                      I I
1017] I I
1017] I I
10181l                                                                                                                                                                              80 7        8 3 Sv5 TEM              CAUSE          CAust                                                        COMP              VALVf CCCE                  COCE        SUSCODE                    COMPONENT CODE                  SU8CCDE            suSCCOE lol9l                            lC lD l@ lE l@ y@ l ll Nl Sl Tl Rl Ul@ l C l@ ]@                                        18          is                20 7        4                      9          to            11            12              13 SEQU EN TI AL                      OCCU R R E NCE        REPORT                          REVISION
10181l                                                                                                                                                                              80 7        8 3 Sv5 TEM              CAUSE          CAust                                                        COMP              VALVf CCCE                  COCE        SUSCODE                    COMPONENT CODE                  SU8CCDE            suSCCOE lol9l                            lC lD l@ lE l@ y@ l ll Nl Sl Tl Rl Ul@ l C l@ ]@                                        18          is                20 7        4                      9          to            11            12              13 SEQU EN TI AL                      OCCU R R E NCE        REPORT                          REVISION (gg gg      EVENTYEAR                                  REPOR T NO.                            COOE                TvPE                              NC.
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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333 ATTACHMENT TO LER 79-038/03X-1                        Page 1 of I While in a cold shutdown condition, during the calibration of Instrument 02-TIC-200, the instrument could not be demonstrated to be within calibration. Since the referenced instrument provided Indication and control of the sixteen (16) Main Steam Line Tunnel High Temperature Detectors, these instruments could not be demonstrated fully operable as required by Technical Specifications Appendix A, Table 4.2-1.
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333 ATTACHMENT TO LER 79-038/03X-1                        Page 1 of I While in a cold shutdown condition, during the calibration of Instrument 02-TIC-200, the instrument could not be demonstrated to be within calibration. Since the referenced instrument provided Indication and control of the sixteen (16) Main Steam Line Tunnel High Temperature Detectors, these instruments could not be demonstrated fully operable as required by Technical Specifications Appendix A, Table 4.2-1.
On-site calibration of the controller was not possible and attempted off-site calibratloa did not yield satisfactory results. Accordingly, the calibration of the Main Steam Tunnel High Temperature Detectors was verified by changing the Instrument Surveillance Procedure to allow the use of other equipment. Proper operation was verified on August 24, 1979 (prior to plant startup on September 3,1979) by completion of F-ISP-45 titled " Main Steam Line High Temperature" to meet the requirements of Technical Specifications Table 4.2-1.      No additional corrective action is required.
On-site calibration of the controller was not possible and attempted off-site calibratloa did not yield satisfactory results. Accordingly, the calibration of the Main Steam Tunnel High Temperature Detectors was verified by changing the Instrument Surveillance Procedure to allow the use of other equipment. Proper operation was verified on August 24, 1979 (prior to plant startup on September 3,1979) by completion of F-ISP-45 titled " Main Steam Line High Temperature" to meet the requirements of Technical Specifications Table 4.2-1.      No additional corrective action is required.
NOTE:    Revision 1 of this LER is submitted to provide additional Information with respect to corrective action.
NOTE:    Revision 1 of this LER is submitted to provide additional Information with respect to corrective action.
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Latest revision as of 11:02, 1 February 2020

Revised LER 79-038/03X-1:on 790611,during Cold Shutdown Surveillance Revealed Calibr Instrument for Main Steam Tunnel High Temp Switches Could Not Be Calibr.Caused by Instrument 02-TIC-200 Drift.Alternate Instrumentation Used
ML19309B215
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 03/27/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309B209 List:
References
LER-79-038-03X, LER-79-38-3X, NUDOCS 8004030278
Download: ML19309B215 (2)


Text

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U. S. NUCLE AR REGULATORY COMMISSION

, .s LICENSEE EVENT REPORT

/ i kj (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATioN)

CONTROL BLOCK: l 1

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7 LICENSEE COCE CON'T l0lII ," l L @l015 l0 l0 l0 l3 l3 l3 G10 69l 6 i EVENT fad 1 l 11719 DATE l@l 0131217 74 75 REPCRT DATE l 8 l o l@ 18 0 J 8 60 61 COCK ET NUVSER EVENT DESCRIPTION AND PAC 8A8LE CONSECUENCES h 10121 10urina cold shutdown surveillance revealed that the instrument used for  !

tol3} l calibration of main steam tunnel high temoerature switches could not be 1 1

1014 l l calibrated. As a result main steam tunnel temoerature instruments could

, 10 I 3 l Inot be demonstrated operable per TS Table 4.2-1. No hazard existed. I 1016IISee attachment for details. I I

1017] I I

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41 lNl@ lAl@ l P ] 4 ] 2 ] 7 lt 44 47 3J 34 31 40 42 43 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS l i 101 lDri f t of ins trument 02-TIC-200 caused oroblem. Alternate instrumentation was I lilijlused to show main steam tunnel high temOerature switches within TS limits. I l i 171 INo additional action reauired. See attachment for details. I 9

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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333 ATTACHMENT TO LER 79-038/03X-1 Page 1 of I While in a cold shutdown condition, during the calibration of Instrument 02-TIC-200, the instrument could not be demonstrated to be within calibration. Since the referenced instrument provided Indication and control of the sixteen (16) Main Steam Line Tunnel High Temperature Detectors, these instruments could not be demonstrated fully operable as required by Technical Specifications Appendix A, Table 4.2-1.

On-site calibration of the controller was not possible and attempted off-site calibratloa did not yield satisfactory results. Accordingly, the calibration of the Main Steam Tunnel High Temperature Detectors was verified by changing the Instrument Surveillance Procedure to allow the use of other equipment. Proper operation was verified on August 24, 1979 (prior to plant startup on September 3,1979) by completion of F-ISP-45 titled " Main Steam Line High Temperature" to meet the requirements of Technical Specifications Table 4.2-1. No additional corrective action is required.

NOTE: Revision 1 of this LER is submitted to provide additional Information with respect to corrective action.

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