|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045F6631993-06-25025 June 1993 LER 93-014-00 on 930529,logic Sys Functional Testing Was Incomplete Due to Test Procedure Deficiencies.Temporary Procedure Changes made.W/930625 Ltr ML20045D9081993-06-23023 June 1993 LER 93-013-00:on 930525,automatic Reactor Scram Occurred When APRM E Spiked While Indicated Water Level Approx 6%. Possibly Caused by Spiking of LPRM Input of APRM E. Radiation Sources Replaced W/Stronger sources.W/930623 Ltr ML20045D2971993-06-18018 June 1993 LER 93-012-00:on 930519,isolation Occurred When Rhr/Lpci Pump B Started in Shutdown Cooling Mode & Inboard & Outboard Isolation Valves Closed.Caused by Pressure Transient.Test Program Developed to Obtain Necessary data.W/930618 Ltr ML20045D1201993-06-16016 June 1993 LER 92-015-01:on 920317,deficiencies W/Potential to Effect Safe Shutdown During Postulated Fires Identified Due to Lack of Commitment to Fire Protection Implementation by Mgt.Plant Mods scheduled.W/930616 Ltr ML20045A3931993-06-0303 June 1993 LER 91-029-01:on 911130 & 1213,false Primary Containment High Radiation Isolation Sys Occurred.Caused by Filters Attached to Input of Monitors.Correct Operation of Isolation of Primary Containment Vent & Valves confirmed.W/930603 Ltr ML20044F6211993-05-19019 May 1993 LER 93-010-00:on 930420,HPCI Declared Inoperable Due to Grounded Electric Circuit on Turbine Steam Supply Valve. Caused by Personnel Inattention to Detail.Personnel Counseled Re Need for Attention to detail.W/930519 Ltr ML20044F6111993-05-19019 May 1993 LER 93-009-00:on 930420,noted That Abrupt Reduction in Feedwater Flow Resulted in Rapidly Decreasing Rwl.Caused by Loose Electrical Connection on Reactor Feed Pump A.Post Trip Evaluation Conducted to Prevent recurrence.W/930519 Ltr ML20044D2051993-05-11011 May 1993 LER 93-008-00:on 930412,identified That SJAE Radiation Monitor Had Increased.Caused by Failure to Identify Need to Obtain an Offgas Sample.Daily Instrument Surveillance Test changed.W/930511 Ltr ML20044B6181993-02-11011 February 1993 LER 93-035-01:on 920825,circuit Breaker Supplying Power to Load Ctr step-down Transformer Tripped Due to High Phase Current & Grounding.Caused by Deteriorated Transformer Coil Insulation.Transformer Rebuilt & reinstalled.W/920211 Ltr ML20024H0831991-05-13013 May 1991 LER 91-005-00:on 910412,torus Water Temp Instrumentation Declared Inoperable.Caused by Uncertainty of 3.52 F. Conservative 4 Degree Bias Installed in Torus Water Instrumentation Software program.W/910513 Ltr ML20024G6831991-04-17017 April 1991 LER 91-004-00:on 910318,unmonitored Release of Radioactivity Detected Outside Auxiliary Boiler Bldg.Caused by Personnel Error & Deficiencies in Procedures.Contaminated Surfaces Covered W/Reinforced Plastic covers.W/910417 Ltr ML20028H8611991-01-25025 January 1991 LER 90-025-01:on 901115 & 1226,in Total,Five Svc Water to Emergency Svc Water Swing Check Valves Failed to Close During Testing.Caused by Corrosion Problems.Valve Internals Replaced W/Stainless Steel components.W/910125 Ltr ML20028G9451990-09-25025 September 1990 LER 90-003-01:on 900129,core Overpower Events Occurred Due to Feed Flow Transmitter Calibr.Caused by Previously Unidentified Vendor Design Error,Error Introduced as Result of Plant Mod & Improper prioritization.W/900925 Ltr ML20043J0861990-06-21021 June 1990 LER 90-017-00:on 900526,instrument Setpoint Drift Exceeds Tech Spec Limit for HPCI Turbine Trip on High Reactor Water Level.Cause Unknown.Transmitter Included in Program for Weekly Monitoring of Rosemount transmitters.W/900621 Ltr ML20043B9831990-05-23023 May 1990 LER 90-016-00:on 900424,automatic Isolation Signal Closed Suction Valves from Reactor Water Recirculation Sys.On 900425,suction Valves Closed & RHR Pump Tripped.Caused by Chattering Pressure Switch.Switches replaced.W/900523 Ltr ML20043A9601990-05-21021 May 1990 LER 90-015-00:on 900420,discovered That Prerequisite Surveillance Test of source-range Monitors Not Performed Prior to Beginning Replacement of LPRMs on 900419.Caused by Procedure Deficiency.Lprm Procedure revised.W/900521 Ltr ML20042G8311990-05-10010 May 1990 LER 90-014-00:on 900410,primary Containment Isolation Check Valve Declared Inoperable Due to Missing Spring.Caused by Personnel Error.Performance of HPCI Turbine Exhaust Drain Sys Will Be Monitored During HPCI testing.W/900510 Ltr ML20042G8301990-05-0909 May 1990 LER 90-013-00:on 900409,shutdown Cooling Automatically Isolated During Transfer of Bus.Probably Caused by Contract Personnel Accidentally Knocking Jumper Loose.Procedures Re Controls on Jumpers Will Be revised.W/900505 Ltr ML20042F7531990-05-0303 May 1990 LER 90-012-00:on 900404,normal & Emergency Svc Water Valves Found to Be Inoperable.Caused by Excessive Build Up of Corrosion on Valve Surfaces & Accumulation of Silt.Valves Cleaned & Restored to svc.W/900503 Ltr ML20012E0071990-03-21021 March 1990 LER 90-005-00:on 900220,HPCI Sys Inoperable Resulting in 7 Day Limiting Condition for Operation.Caused by Sticking or Binding in Remote Servo.Remote Servo replaced.W/900321 Ltr ML20012C5161990-03-0909 March 1990 LER 90-004-00:on 900207,isolation of RCIC Sys Occurred, Resulting in Initiation of 7-day Limiting Condition of Operation.Caused by Failure of Master Trip Unit.Subj Unit replaced.W/900309 Ltr ML20012B4351990-03-0202 March 1990 LER 90-003-00:on 900129,when More Accurate Transmitters Placed in Svc,After Calibr Span Values Adjusted,Indicated Power Exceeded Core Thermal Power Limit.Caused by Incomplete Review of Manual.Transmitters recalibr.W/900302 Ltr ML20006E8621990-02-16016 February 1990 LER 90-001-00:on 900119,reactor Scram Occurred During Calibr of Reactor Water Level Instrumentation,Resulting in Valve Packing Leak & Causing False Low Water Level.Caused by Rapid Valve Movement.Event reviewed.W/900216 Ltr ML20006E9221990-02-15015 February 1990 LER 90-002-00:on 900215,reactor High Pressure Isolation Logic Tripped & Isolated RHR Shutdown Cooling Sys B as Sys Being Started.Hydraulic Pressure Transient Suspected as Cause.Operating Procedure revised.W/900215 Ltr ML20006E2101990-02-12012 February 1990 LER 89-019-01:on 891031,HPCI Turbine Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Conductive Corrosion Products Between Amphenol Type Connector & Mounting Plate.Connector cleaned.W/900212 Ltr ML20006E2291990-02-0808 February 1990 LER 89-018-01:on 891008,HPCI High Steam Flow Signal Closed HPCI Outboard Steam Supply Isolation Valves,Causing Isolation of Logic Circuit.Caused by Overly Conservative Value for Flow Isolation Signal.Sensor vented.W/900208 Ltr ML20011E1431990-01-29029 January 1990 LER 89-020-01:on 891105,reactor Scram Initiated by High APRM Neutron Flux from Pressure Transient from Turbine Control Valve Closure.Caused by Void Collapse in Core Moderator. Computer Programming Changed Re Transient data.W/900129 Ltr ML20006C1571990-01-26026 January 1990 LER 89-026-00:on 891105,reactor Scram from Full Power Occurred Due to Problems W/Turbine electro-hydraulic Control Sys.On 891220,contractor Notified Util That Valves Tested Did Not Actuate within Setpoint as required.W/900126 Ltr ML20005E8541990-01-0202 January 1990 LER 89-025-00:on 891130,isolation Signal Closed Outboard Isolation Valves on Steam Supply Line to HPCI Sys,Rendering HPCI Sys Inoperable & Initiating 7-day Limiting Condition for Operation.Caused by Excess steam.W/900102 Ltr ML20042D3961989-12-27027 December 1989 LER 89-024-00:on 891129,RCIC Sys Inoperable for 14 Minutes During Monthly Surveillance Test.Caused by Personnel Error. Outboard Isolation Valve Opened & Critique & Discussion W/ Technicians Held to Increase Event awareness.W/891227 Ltr ML20011D1351989-12-12012 December 1989 LER 89-023-00:on 891112,reactor Scram Occurred During Scheduled Surveillance Test of Safety Relief Valves.Caused by High Neutron Flux Signal Due to Steam Pressure Transient. Change Made to Surveillance Test ST-22B.W/891212 Ltr ML19332F4751989-12-0707 December 1989 LER 89-022-00:on 891107,determined That Elastomeric Seals in 33 Snubbers Had Not Been Replaced within Plant 7-yr Svc Life Guideline.Caused by Failures in Mgt of Maint Records. Snubbers Replaced as necessary.W/891207 Ltr ML19332F4511989-12-0505 December 1989 LER 89-020-00:on 891105,reactor Scram Occurred Due to Failure in Electronic Control Card of electro-hydraulic Control Sys.Caused by Void Collapse in Core Moderator. Circuit Boards Sent to Vendor for analysis.W/891205 Ltr ML19332E6241989-11-30030 November 1989 LER 89-019-00:on 891031 & 891103,HPCI Sys Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Buildup of Conductive Corrosion Products. Connector Cleaned & Sys Returned to svc.W/891130 Ltr ML19332F0471989-11-30030 November 1989 LER 89-021-00:on 891031,circuit Breaker for RCIC Inboard Injection Valve to Feedwater Sys Tripped During Required Valve Testing.Caused by Fault in Motor Winding Insulation. New Motor installed.W/891130 Ltr ML19325F2791989-11-13013 November 1989 LER 89-007-01:on 890509,surveillance of Fire Barrier Penetrations,Per Tech Spec 4.12.F Not Conducted within Allowed Time Period.Caused by Misinterpretation of Fire Protection Ref Manual.Fire Watch established.W/891113 Ltr ML19327C1351989-11-0707 November 1989 LER 89-015-01:on 890918,two Remote Manually Operated Diaphragm Air Operated Isolation Valves Failed Closing Time Acceptance Criteria.Caused by Buildup of Iron Oxide Sludge. Valves Disassembled & Cleaned ML19327B9821989-11-0606 November 1989 LER 89-018-00:on 891008,HPCI High Steam Flow Signal Closed Isolation Valves for Outboard Steam Supply & Steam Line Warning.Caused by Air in Sensing Sys Leading to Unstable Oscillation.Pressure Sensor Vented & calibr.W/891106 Ltr ML19324B1151989-10-23023 October 1989 LER 88-008-01:during 1988 Refuel Outage,One Primary Containment Penetration Exceeded Tech Spec 4.7.A.2.b Limit When Subjected to Local Leak Rate Testing.Leakage Attributed to Wear.Valves replaced.W/891023 Ltr ML19327B1521989-10-20020 October 1989 LER 89-017-00:on 890920,ESFAS Initiated Group II Primary Containment Isolation Signal Triggering RHR & LPCI Sys Isolations.Caused by Cognitive Human Error in Not Finding Isolation Signal.Fuse Replaced & Sys restarted.W/891020 Ltr ML19327B1501989-10-18018 October 1989 LER 89-016-00:on 890918,scram Signal Automatically Initiated During Transfer of Power Supply for Reactor Protection Sys. Caused by Lack of Caution Statement in Procedure.Procedure Revised to Add Time Caution for Bus transfers.W/891018 Ltr ML19327B1331989-10-18018 October 1989 LER 89-015-00:on 890918,two of Nine Remote Manually Operated Diaphragm Air Operated Containment Isolation Valves Failed Acceptance Criteria for Closing Time.Caused by Buildup & Hardening of Iron Oxide Sludge.Valves cleaned.W/891018 Ltr ML20024A8271983-06-20020 June 1983 LER 83-023/01T-0:on 830607,water Seepage Discovered from Weld in Stainless Steel Pipe Section of Control Rod Hydraulic Return Line.Caused by Intergranular Stress Corrosion Cracking.Piping Will Be removed.W/830620 Ltr ML20024A8571983-06-18018 June 1983 LER 83-021/03L-0:on 830605,rod Block Calibr Not Performed within 7 Days of 830603 Planned Reactor Shutdown.Caused by Inadequate Mgt Controls to Implement Tech Specs.Procedures to Be revised.W/830618 ML20024A8631983-06-16016 June 1983 LER 83-022/03L-0:on 830607,during Performance of Local Leak Rate Testing of Containment Spray,Penetration X-39A Found W/ Leakage That May Exceed Tech Spec Limits.Cause Undetermined. Details Will Be Provided within 30 days.W/830616 Ltr ML20028D6951983-01-11011 January 1983 LER 82-057/03L-0:on 821216,during Normal Operation,Reactor Scrammed on High Neutron Flux on Power Range Monitors. Caused by Reactor Pressure Spike Created by Sudden Closure of One MSIV Due to Improper Maint.Procedure Changed ML20027B5291982-09-10010 September 1982 LER 82-041/03X-1:on 820830,during Surveillance Test,Both Standby Liquid Control Sys Squib Valves Actuated.Caused by Operator Pulling Wrong Fuses.Operator Counseled ML20052F9721982-05-0303 May 1982 LER 82-003/01X-1:on 820302,during Normal Shutdown Operations,Only Two Intermediate Range Monitors in Trip Sys a Were Operable.Caused by Personnel Error & Inadequate Procedures.Procedures Revised ML20052E2811982-04-30030 April 1982 LER 82-017/03L-0:on 820402,MSIV 10% Closure Position Switches on Two Valves Did Not Trip When Tested.Caused by Mechanical Drift of Valve Position Switch Operating Cams. Adjustment Made ML20052C2511982-04-20020 April 1982 LER 82-005/01X-1:on 820315,during Normal Operation, Containment Oxygen Concentration Exceeded 4% Limit for Approx 6-h.Caused by Personnel Error.Startup Checkoff List Revised 1993-06-03
[Table view] Category:RO)
MONTHYEARML20045F6631993-06-25025 June 1993 LER 93-014-00 on 930529,logic Sys Functional Testing Was Incomplete Due to Test Procedure Deficiencies.Temporary Procedure Changes made.W/930625 Ltr ML20045D9081993-06-23023 June 1993 LER 93-013-00:on 930525,automatic Reactor Scram Occurred When APRM E Spiked While Indicated Water Level Approx 6%. Possibly Caused by Spiking of LPRM Input of APRM E. Radiation Sources Replaced W/Stronger sources.W/930623 Ltr ML20045D2971993-06-18018 June 1993 LER 93-012-00:on 930519,isolation Occurred When Rhr/Lpci Pump B Started in Shutdown Cooling Mode & Inboard & Outboard Isolation Valves Closed.Caused by Pressure Transient.Test Program Developed to Obtain Necessary data.W/930618 Ltr ML20045D1201993-06-16016 June 1993 LER 92-015-01:on 920317,deficiencies W/Potential to Effect Safe Shutdown During Postulated Fires Identified Due to Lack of Commitment to Fire Protection Implementation by Mgt.Plant Mods scheduled.W/930616 Ltr ML20045A3931993-06-0303 June 1993 LER 91-029-01:on 911130 & 1213,false Primary Containment High Radiation Isolation Sys Occurred.Caused by Filters Attached to Input of Monitors.Correct Operation of Isolation of Primary Containment Vent & Valves confirmed.W/930603 Ltr ML20044F6211993-05-19019 May 1993 LER 93-010-00:on 930420,HPCI Declared Inoperable Due to Grounded Electric Circuit on Turbine Steam Supply Valve. Caused by Personnel Inattention to Detail.Personnel Counseled Re Need for Attention to detail.W/930519 Ltr ML20044F6111993-05-19019 May 1993 LER 93-009-00:on 930420,noted That Abrupt Reduction in Feedwater Flow Resulted in Rapidly Decreasing Rwl.Caused by Loose Electrical Connection on Reactor Feed Pump A.Post Trip Evaluation Conducted to Prevent recurrence.W/930519 Ltr ML20044D2051993-05-11011 May 1993 LER 93-008-00:on 930412,identified That SJAE Radiation Monitor Had Increased.Caused by Failure to Identify Need to Obtain an Offgas Sample.Daily Instrument Surveillance Test changed.W/930511 Ltr ML20044B6181993-02-11011 February 1993 LER 93-035-01:on 920825,circuit Breaker Supplying Power to Load Ctr step-down Transformer Tripped Due to High Phase Current & Grounding.Caused by Deteriorated Transformer Coil Insulation.Transformer Rebuilt & reinstalled.W/920211 Ltr ML20024H0831991-05-13013 May 1991 LER 91-005-00:on 910412,torus Water Temp Instrumentation Declared Inoperable.Caused by Uncertainty of 3.52 F. Conservative 4 Degree Bias Installed in Torus Water Instrumentation Software program.W/910513 Ltr ML20024G6831991-04-17017 April 1991 LER 91-004-00:on 910318,unmonitored Release of Radioactivity Detected Outside Auxiliary Boiler Bldg.Caused by Personnel Error & Deficiencies in Procedures.Contaminated Surfaces Covered W/Reinforced Plastic covers.W/910417 Ltr ML20028H8611991-01-25025 January 1991 LER 90-025-01:on 901115 & 1226,in Total,Five Svc Water to Emergency Svc Water Swing Check Valves Failed to Close During Testing.Caused by Corrosion Problems.Valve Internals Replaced W/Stainless Steel components.W/910125 Ltr ML20028G9451990-09-25025 September 1990 LER 90-003-01:on 900129,core Overpower Events Occurred Due to Feed Flow Transmitter Calibr.Caused by Previously Unidentified Vendor Design Error,Error Introduced as Result of Plant Mod & Improper prioritization.W/900925 Ltr ML20043J0861990-06-21021 June 1990 LER 90-017-00:on 900526,instrument Setpoint Drift Exceeds Tech Spec Limit for HPCI Turbine Trip on High Reactor Water Level.Cause Unknown.Transmitter Included in Program for Weekly Monitoring of Rosemount transmitters.W/900621 Ltr ML20043B9831990-05-23023 May 1990 LER 90-016-00:on 900424,automatic Isolation Signal Closed Suction Valves from Reactor Water Recirculation Sys.On 900425,suction Valves Closed & RHR Pump Tripped.Caused by Chattering Pressure Switch.Switches replaced.W/900523 Ltr ML20043A9601990-05-21021 May 1990 LER 90-015-00:on 900420,discovered That Prerequisite Surveillance Test of source-range Monitors Not Performed Prior to Beginning Replacement of LPRMs on 900419.Caused by Procedure Deficiency.Lprm Procedure revised.W/900521 Ltr ML20042G8311990-05-10010 May 1990 LER 90-014-00:on 900410,primary Containment Isolation Check Valve Declared Inoperable Due to Missing Spring.Caused by Personnel Error.Performance of HPCI Turbine Exhaust Drain Sys Will Be Monitored During HPCI testing.W/900510 Ltr ML20042G8301990-05-0909 May 1990 LER 90-013-00:on 900409,shutdown Cooling Automatically Isolated During Transfer of Bus.Probably Caused by Contract Personnel Accidentally Knocking Jumper Loose.Procedures Re Controls on Jumpers Will Be revised.W/900505 Ltr ML20042F7531990-05-0303 May 1990 LER 90-012-00:on 900404,normal & Emergency Svc Water Valves Found to Be Inoperable.Caused by Excessive Build Up of Corrosion on Valve Surfaces & Accumulation of Silt.Valves Cleaned & Restored to svc.W/900503 Ltr ML20012E0071990-03-21021 March 1990 LER 90-005-00:on 900220,HPCI Sys Inoperable Resulting in 7 Day Limiting Condition for Operation.Caused by Sticking or Binding in Remote Servo.Remote Servo replaced.W/900321 Ltr ML20012C5161990-03-0909 March 1990 LER 90-004-00:on 900207,isolation of RCIC Sys Occurred, Resulting in Initiation of 7-day Limiting Condition of Operation.Caused by Failure of Master Trip Unit.Subj Unit replaced.W/900309 Ltr ML20012B4351990-03-0202 March 1990 LER 90-003-00:on 900129,when More Accurate Transmitters Placed in Svc,After Calibr Span Values Adjusted,Indicated Power Exceeded Core Thermal Power Limit.Caused by Incomplete Review of Manual.Transmitters recalibr.W/900302 Ltr ML20006E8621990-02-16016 February 1990 LER 90-001-00:on 900119,reactor Scram Occurred During Calibr of Reactor Water Level Instrumentation,Resulting in Valve Packing Leak & Causing False Low Water Level.Caused by Rapid Valve Movement.Event reviewed.W/900216 Ltr ML20006E9221990-02-15015 February 1990 LER 90-002-00:on 900215,reactor High Pressure Isolation Logic Tripped & Isolated RHR Shutdown Cooling Sys B as Sys Being Started.Hydraulic Pressure Transient Suspected as Cause.Operating Procedure revised.W/900215 Ltr ML20006E2101990-02-12012 February 1990 LER 89-019-01:on 891031,HPCI Turbine Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Conductive Corrosion Products Between Amphenol Type Connector & Mounting Plate.Connector cleaned.W/900212 Ltr ML20006E2291990-02-0808 February 1990 LER 89-018-01:on 891008,HPCI High Steam Flow Signal Closed HPCI Outboard Steam Supply Isolation Valves,Causing Isolation of Logic Circuit.Caused by Overly Conservative Value for Flow Isolation Signal.Sensor vented.W/900208 Ltr ML20011E1431990-01-29029 January 1990 LER 89-020-01:on 891105,reactor Scram Initiated by High APRM Neutron Flux from Pressure Transient from Turbine Control Valve Closure.Caused by Void Collapse in Core Moderator. Computer Programming Changed Re Transient data.W/900129 Ltr ML20006C1571990-01-26026 January 1990 LER 89-026-00:on 891105,reactor Scram from Full Power Occurred Due to Problems W/Turbine electro-hydraulic Control Sys.On 891220,contractor Notified Util That Valves Tested Did Not Actuate within Setpoint as required.W/900126 Ltr ML20005E8541990-01-0202 January 1990 LER 89-025-00:on 891130,isolation Signal Closed Outboard Isolation Valves on Steam Supply Line to HPCI Sys,Rendering HPCI Sys Inoperable & Initiating 7-day Limiting Condition for Operation.Caused by Excess steam.W/900102 Ltr ML20042D3961989-12-27027 December 1989 LER 89-024-00:on 891129,RCIC Sys Inoperable for 14 Minutes During Monthly Surveillance Test.Caused by Personnel Error. Outboard Isolation Valve Opened & Critique & Discussion W/ Technicians Held to Increase Event awareness.W/891227 Ltr ML20011D1351989-12-12012 December 1989 LER 89-023-00:on 891112,reactor Scram Occurred During Scheduled Surveillance Test of Safety Relief Valves.Caused by High Neutron Flux Signal Due to Steam Pressure Transient. Change Made to Surveillance Test ST-22B.W/891212 Ltr ML19332F4751989-12-0707 December 1989 LER 89-022-00:on 891107,determined That Elastomeric Seals in 33 Snubbers Had Not Been Replaced within Plant 7-yr Svc Life Guideline.Caused by Failures in Mgt of Maint Records. Snubbers Replaced as necessary.W/891207 Ltr ML19332F4511989-12-0505 December 1989 LER 89-020-00:on 891105,reactor Scram Occurred Due to Failure in Electronic Control Card of electro-hydraulic Control Sys.Caused by Void Collapse in Core Moderator. Circuit Boards Sent to Vendor for analysis.W/891205 Ltr ML19332E6241989-11-30030 November 1989 LER 89-019-00:on 891031 & 891103,HPCI Sys Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Buildup of Conductive Corrosion Products. Connector Cleaned & Sys Returned to svc.W/891130 Ltr ML19332F0471989-11-30030 November 1989 LER 89-021-00:on 891031,circuit Breaker for RCIC Inboard Injection Valve to Feedwater Sys Tripped During Required Valve Testing.Caused by Fault in Motor Winding Insulation. New Motor installed.W/891130 Ltr ML19325F2791989-11-13013 November 1989 LER 89-007-01:on 890509,surveillance of Fire Barrier Penetrations,Per Tech Spec 4.12.F Not Conducted within Allowed Time Period.Caused by Misinterpretation of Fire Protection Ref Manual.Fire Watch established.W/891113 Ltr ML19327C1351989-11-0707 November 1989 LER 89-015-01:on 890918,two Remote Manually Operated Diaphragm Air Operated Isolation Valves Failed Closing Time Acceptance Criteria.Caused by Buildup of Iron Oxide Sludge. Valves Disassembled & Cleaned ML19327B9821989-11-0606 November 1989 LER 89-018-00:on 891008,HPCI High Steam Flow Signal Closed Isolation Valves for Outboard Steam Supply & Steam Line Warning.Caused by Air in Sensing Sys Leading to Unstable Oscillation.Pressure Sensor Vented & calibr.W/891106 Ltr ML19324B1151989-10-23023 October 1989 LER 88-008-01:during 1988 Refuel Outage,One Primary Containment Penetration Exceeded Tech Spec 4.7.A.2.b Limit When Subjected to Local Leak Rate Testing.Leakage Attributed to Wear.Valves replaced.W/891023 Ltr ML19327B1521989-10-20020 October 1989 LER 89-017-00:on 890920,ESFAS Initiated Group II Primary Containment Isolation Signal Triggering RHR & LPCI Sys Isolations.Caused by Cognitive Human Error in Not Finding Isolation Signal.Fuse Replaced & Sys restarted.W/891020 Ltr ML19327B1501989-10-18018 October 1989 LER 89-016-00:on 890918,scram Signal Automatically Initiated During Transfer of Power Supply for Reactor Protection Sys. Caused by Lack of Caution Statement in Procedure.Procedure Revised to Add Time Caution for Bus transfers.W/891018 Ltr ML19327B1331989-10-18018 October 1989 LER 89-015-00:on 890918,two of Nine Remote Manually Operated Diaphragm Air Operated Containment Isolation Valves Failed Acceptance Criteria for Closing Time.Caused by Buildup & Hardening of Iron Oxide Sludge.Valves cleaned.W/891018 Ltr ML20024A8271983-06-20020 June 1983 LER 83-023/01T-0:on 830607,water Seepage Discovered from Weld in Stainless Steel Pipe Section of Control Rod Hydraulic Return Line.Caused by Intergranular Stress Corrosion Cracking.Piping Will Be removed.W/830620 Ltr ML20024A8571983-06-18018 June 1983 LER 83-021/03L-0:on 830605,rod Block Calibr Not Performed within 7 Days of 830603 Planned Reactor Shutdown.Caused by Inadequate Mgt Controls to Implement Tech Specs.Procedures to Be revised.W/830618 ML20024A8631983-06-16016 June 1983 LER 83-022/03L-0:on 830607,during Performance of Local Leak Rate Testing of Containment Spray,Penetration X-39A Found W/ Leakage That May Exceed Tech Spec Limits.Cause Undetermined. Details Will Be Provided within 30 days.W/830616 Ltr ML20028D6951983-01-11011 January 1983 LER 82-057/03L-0:on 821216,during Normal Operation,Reactor Scrammed on High Neutron Flux on Power Range Monitors. Caused by Reactor Pressure Spike Created by Sudden Closure of One MSIV Due to Improper Maint.Procedure Changed ML20027B5291982-09-10010 September 1982 LER 82-041/03X-1:on 820830,during Surveillance Test,Both Standby Liquid Control Sys Squib Valves Actuated.Caused by Operator Pulling Wrong Fuses.Operator Counseled ML20052F9721982-05-0303 May 1982 LER 82-003/01X-1:on 820302,during Normal Shutdown Operations,Only Two Intermediate Range Monitors in Trip Sys a Were Operable.Caused by Personnel Error & Inadequate Procedures.Procedures Revised ML20052E2811982-04-30030 April 1982 LER 82-017/03L-0:on 820402,MSIV 10% Closure Position Switches on Two Valves Did Not Trip When Tested.Caused by Mechanical Drift of Valve Position Switch Operating Cams. Adjustment Made ML20052C2511982-04-20020 April 1982 LER 82-005/01X-1:on 820315,during Normal Operation, Containment Oxygen Concentration Exceeded 4% Limit for Approx 6-h.Caused by Personnel Error.Startup Checkoff List Revised 1993-06-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARJAFP-99-0277, Monthly Operating Rept for Sept 1999 Fpr Ja FitzPatrick Nuclear Power Plant.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 Fpr Ja FitzPatrick Nuclear Power Plant.With ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data JAFP-99-0261, Monthly Operating Rept for Aug 1999 for Jafnpp.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Jafnpp.With JAFP-99-0236, Monthly Operating Rept for July 1999 for Ja FitzPatrick Npp. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Ja FitzPatrick Npp. with ML20216D9541999-07-28028 July 1999 Safety Evaluation Authorizing Proposed Alternatives for Second 10-year Interval Pursuant to 10CFR50.55a(a)(3)(ii) ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept JAFP-99-0211, Monthly Operating Rept for June 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Ja FitzPatrick Nuclear Power Plant.With JAFP-99-0175, Annual Summary of Changes,Tests & Experiments for 1997/1998. with1999-06-0202 June 1999 Annual Summary of Changes,Tests & Experiments for 1997/1998. with JAFP-99-0181, Monthly Operating Rept for May 1999 for Jafnpp.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Jafnpp.With JAFP-99-0166, Monthly Operating Rept for Apr 1999 for Ja FitzPatrick Nuclear Plant.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Ja FitzPatrick Nuclear Plant.With JAFP-99-0142, Monthly Operating Rept for Mar 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ja FitzPatrick Nuclear Power Plant.With JAFP-99-0092, Monthly Operating Rept for Feb 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ja FitzPatrick Nuclear Power Plant.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20202J0891999-02-0303 February 1999 Safety Evaluation Accepting Rev 2 of Third Interval Inservice Testing Program for Pumps & Valves for James a FitzPatrick Nuclear Power Plant ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc JAFP-99-0011, Monthly Operating Rept for Dec 1998 for Ja FitzPatrick Nuclear Power Plant.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Ja FitzPatrick Nuclear Power Plant.With ML20198F9991998-12-0404 December 1998 Assessment of Licensing Basis for Use of Containment Overpressure Credit for Net Positive Suction Head Analyses Power Authority of State of New York,James a Fitzpatrick Nuclear Power Plant ML20196J3501998-12-0404 December 1998 SER Accepting License Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves JAFP-98-0396, Monthly Operating Rept for Nov 1998 for Ja FitzPatrick Npp. with1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Ja FitzPatrick Npp. with ML20196F9251998-11-25025 November 1998 Safety Evaluation Re Thrid 10-year Interval Inservice Insp Program Relief Requests for Plant ML20195J7521998-11-18018 November 1998 Rev 7 to Jaf Colr ML20195K4211998-11-17017 November 1998 Safety Evaluation Authorizing Proposed Alternative in Relief Request VRR-05 Per 10CFR50.55a(a)(3)(i) & PRR-01,PRR-02R1, PRR-03,PRR-04,VRR-02,VRR-03 & VRR-04 Per 10CFR50.55a(a)(3)(ii) ML20195E1051998-11-13013 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves, Issued 950817 ML20197G6221998-11-0606 November 1998 Non-proprietary Rev 7 to HI-971661, Licensing Rept for Reracking of Ja FitzPatrick Sfp ML20155H5321998-11-0303 November 1998 Safety Evaluation Authorizing Alternative to ASME Code Requirements for CRD Bolting ML20155H5801998-11-0303 November 1998 Safety Evaluation Authorizing Postponement of Beginning of Augmented Exam Requirements of 10CFR50.55a(g)(6)(ii)(A)(2) Re ASME Code,Section XI JAFP-98-0360, Monthly Operating Rept for Oct 1998 for Ja FitzPatrick Nuclear Power Plant.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Ja FitzPatrick Nuclear Power Plant.With ML20155C2821998-10-30030 October 1998 Non-proprietary Rev 0 to GENE-187-30-1598 Np, CRD Bolting Flaw Evaluation for Ja FitzPatrick Nuclear Power Plant ML20154L6591998-10-14014 October 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Snubber Visual Inservice Exam Intervals & Sampling Rates Requirements Contained in ASME Code,Section Xi,Subsection Iwf,Article IWF-5000 JAFP-98-0322, Monthly Operating Rept for Sept 1998 for Ja Fitzpatrick Nuclear Power Plant.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Ja Fitzpatrick Nuclear Power Plant.With ML20153D2591998-09-21021 September 1998 SER Accepting Proposed Alternative Testing of Containment Following ECCS Suction Strainer Replacement ML20153B5611998-09-0101 September 1998 Rev 1 to JAF-SE-98-013, RHR & Core Spray Suppression Pool Suction Strainer Replacement ML20151X6891998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Ja FitzPatrick Nuclear Power Plant ML20237E8361998-08-25025 August 1998 Rev 6 to Colr ML20237E9471998-08-0808 August 1998 Rev 6 to Colr JAFP-98-0264, Monthly Operating Rept for July 1998 for Ja FitzPatrick Nuclear Plant1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Ja FitzPatrick Nuclear Plant ML20236X5881998-07-29029 July 1998 Safety Evaluation Supporting Amend 245 to License DPR-59 ML20236V8181998-07-29029 July 1998 Safety Evaluation Accepting Request for Relief from Implementation of Requirements of 10CFR50.55a Related to Containment Repair & Replacement Activities for James a FitzPatrick Nuclear Power Plant ML20153B5781998-07-28028 July 1998 Rev 0 to JAF-SE-98-025, HPCI & RCIC Suppression Pool Suction Strainer Replacement ML20236X3831998-07-14014 July 1998 Rev 2 to JAF-RPT-MULTI-02671, Summary of Detailed Evaluation for NRC Generic Ltr 96-06 ML20154L9201998-07-10010 July 1998 SER Accepting Rev to Reactor Vessel Surveillance Capsule Withdrawal Schedule for James a Fitzpatrick Nuclear Power Plant JAFP-98-0222, Monthly Operating Rept for June 1998 for Ja FitzPatrick Nuclear Power Plant1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Ja FitzPatrick Nuclear Power Plant JAFP-98-0193, Monthly Operating Rept for May 1998 for Ja FitzPatrick Nuclear Plant1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Ja FitzPatrick Nuclear Plant ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted JAFP-98-0168, Monthly Operating Rept for Apr 1998 for Ja FitzPatrick Nuclear Power Plant1998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Ja FitzPatrick Nuclear Power Plant JAFP-98-0128, Monthly Operating Rept for Mar 1998 for Ja FitzPatrick Nuclear Power Plant1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Ja FitzPatrick Nuclear Power Plant ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively JAFP-98-0091, Monthly Operating Rept for Feb 1998 for JAFNPP1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for JAFNPP ML20202G9081998-02-0606 February 1998 Safety Evaluation Re Amend to License DPR-59 to Revise TS Tables 3.2-2 & 4.2-2 JAFP-98-0058, Monthly Operating Rept for Jan 1998 for Ja FitzPatrick Nuclear Power Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Ja FitzPatrick Nuclear Power Plant 1999-09-30
[Table view] |
Text
-. _ _ - _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ - _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ . _ _ _ . _
JImis A. F6 i ' rick Nucteet Power /Isnt
, P.O Box 41
} Lycoming New York 13093 315 342-3640 4 NewYorkPower
& M$o@,' """**F*'"*"d**
Resident Manager May 13, 1991 JAFP-91-0297 l
United States Nuclear Regulatory Commission Document Control Desk Mail Station P1-137 Washington, DC 20555 SUELTECT: DOCKET NC. 50-333 LICENSEE EVENT REPORT: 91-005-00 Torus Water Average Temperature Monitor Inoperable
Dear Sir:
This~ report is submitted in accordance with 10 CFR 50.73 (a) (2) (i) (B) .
Questions concerning this report may be addressed to Hamilton Fish at (315) 349-6013.
Ver tr4 ours, gm WILL A% FERNAND.EZ lChtl WP:HCF:mac-Enclosure-cc: USNRC, Region I USNRC,-Resident Inspector INPO Records Center American Nuclear Insurers F
0304/0672
,10su oi,3 910s12 r5 a.2 gor < neockosoogg3 ,p
1
- m. . v.s muc6ua usutavo., oo .tn.,
~
UCENSEE EVENT REPORT (LER) "*"''"
..cion m ooc.it .m ._...=
l AMES AiflT2 PATRICK NUCLE AR POWER PL ANT o t s t o lo l o l 3 l 313 1 lod 0 t6
, '"
- TO R U S WATER TEMPERATURE INSTRUMENTATION INOPERABLE DUE TO 3.5 DEGREE TNRTRUMENT CHANNEL UNCrpTATMTY sve.rt cars ,a, l ss. munes. se .s.o.,o. teen orme. ..catriiss invotvsp set wo=t- o.v v s.. j .u. "tt;;,*q_. a,. = uc%v. c., vs., . . c e . * =" occaa r =v=es. s-1 I I ! # ! !
04 1:2 9:1 9:1 -
01 0i 5 -
0 io 0 i5 1 3 9il f I I I I I ! ! ! I t ! ! 1 ! i
, , , , , , , i rms .s o.T is sueuirvio .v.sv.=t to vwe asovi.sunn o. is ce. 4 on. ., e, ea, w , ou
ao ' * ' I nemo i n .., i eo n oim, n,m.
~""'
so . n ..ntun ~~1 m m .in, I~~ m rwnei..i ,s.ru.i
'".P 0,0;O'~"" n .num d .o, m ,wim ,
~~"
erwe . <s s .. ..,,,,,
2J* ~ ~ '"' '"
-~
_.,n,,
n o..n o.,
} ,u.ono a . ....o, .,
[ ,w.an n.,
i
.,n n., ; o n .u. ~ --l . ,w ,a ,.. .
ksCthett Comt.CT .o. T,est Lt. nti
%.M4 Ytta.wont wwwege Hamilton C. Fish " C***
3,1 1 5 3; 4j 9l- p p 91 l3 co-,in o~ t me .o. uc co-o n, ..itv. ene..... . em. ...o., m,
?;ust 8v8Ttw cow *oNt%?
[ ((,'e'hI C.wSt S vi? t w cow'0%B%t u.y .C. meg $.ega g s , ~.
1 1 I I ! ! l l ll ! I i ! ! !
0'~
! ! ! I I i i I I ! t ! ! ! -
_ . . . .. . t . . .o . . . . .. r . o -
_ ,_ o.. ,...
Ytl tse . e.,aave f ofF#D $veet?33eo4 CA fif %O g
}
sv a.ct m~ . , .= ..= .~., . ..,. . ~, , .. , n .
EIIS Codes are in [ ]
The primary containment [NH] suppression pool (torus) water temperature instrumentation was modified in 1981.to provide for one dual element resistance temperature detector -(RTD) in each of the 16 bays of the torus. An evaluation of the system on 4/11/91 found that a maximum of one degree of non conservative error could be introduced during conditions of nonuniform addition of heat to the torus-providing torus cooling mode of Residual Heat Removal System was in operation. This data was then included in an instrument channel uncertainty calculation performed on 4/12/91. A conservative maximum
' instrument channel uncertainty of 3.52 fahrenheit degrees was calculated. However, this is within a calculated 4 degree margin to the NUREG 0783 peak local temperature limit. Conservatively, the torus water temperature instrumentation is being reported as inoperable. The torus water temperature instrument software was
.-reprogrammed to add a 4 degree bias so that the calculated bulk (average)-temperature would be displayed at a-value of 4 degrees above the water temperature actually sensed by the RTDs. Analysis shows that even if this maximum uncertainty had occurred in the non conservative (low) direction, the resulting indicated temperature would not have had an adverse effect on operator actions if events managed.by the emergency operating procedures had occurred.
Related LER 90-029
",'l5,"' "'
est Pere 3enA u 8 NUCLt&2 Etrut& Tony COManesson
'. LICENSEE EVENT REPORT (LER) TEXT CONTINUATION amovio ove =o mo-oio.
taPings g/3 igg paceuty maase til pocast nuassen m g gg ,
l AItES As FITZPATRICK .... = gg,. 6 -
g.g NilCLE AR POWER PLAlli 9 1 0 0 ' 6 mm-.
015 f o 10101 1313 I
-l l 5 -
ol o al' or of C, .
-EIIS Codes are in [ ]
Descriotion An error-introduced into the instrument software program for calculation and display of the bulk (average) water temperature for the primary containment [NH] suppression pool (torus) was discovered on 12/7/90. The error failed to exclude the signal from an RTD which was.not installed and resulted in an indicated average temperature
.which was on the order of 3 to 4 fahrenheit degrees less than the actucl-average temperature. The event is described in LER 90-029 submitted on 2/13/91. An unrelated event (LER-91-004) resulted in a plant shutdown on 3/18/91. Prior to plant startup, a thorough
-investigation of the torus watcr temperature instrumentation was conducted.
The plant was originally designed and initially operated for 7 years with 4 resistance temperature detectors (RTDs) installed in two locations. In response to NUREG 0661, a new system using 16 RTD locations was installed in 1982. One of the 16 RTDs was not installed. An evaluation was written in March 1982 to support plant startup and operation with 15 (instead of 16) RTDs. When this evaluation was re-examined in April 1991, it was determined that it was not sufficiently rigorous to meet the standards for safety evaluations which have subsequently evolved during the intervening decade. Accordingly, a new ovaluation was performed by the NSSS vendor and completed on April 11, 1991. The new evaluation considered the modification made to the system on 12/7/90 (LER 90-029) in which the signal from one-of the 15 operable RTDs was jumpered to be averaged in twice with the other 14 RTD signals and divided by 16 to obtain the torus average temperature. The evaluation examined possible errors in the average temperature during nonuniform (i.e.,
due to a single safety relief valve discharge or high pressure-coolant injection system initiation) addition of heat to the-torus pool. The
. estimate of error was based on empirical data-from the Monticello BWR-safety relief valve (SRV) [AD) tests. The evaluation found a potential for no more than a 1 degree error below the actual bulk pool temperature during nonuniform or localized addition of heat to the torus with residual heat removal (RHR) [BO) system providing pool circulation. This finding applied to RTD configurations with 15 or 16 RTDs in operable condition. Thus operation with one RTD not installed had no measurable effect on torus water average temperature.
A second analysis considered the possible instrument average deviations from true average water temperature which could result from-an assumption of NO torus water circulation coupled with non-uniform addition of heat to the torus. Application of temperature profiles from Monticello to the FitzPatrick plant with 16 RTDs operational indicated the calculated average temperature could be expected to be as much as 12-fahrenheit degrees lower than the actual bulk temperature. With 15 RTDs operating the calculated average could be gae.. m.
1 l
nc .. m.a v i wcuan nout.,on, cou-s o. l
"" ^
LICENSEE EVENT REPORT (LER) TEXT CONT!NUATION .=ov ro owe =o vio-o*
In8imit s *3t ti
,w ur,... n, ~c u i w . . m u . w . . < ., .... a, i J AM[S 1. IliIP AiRICK "" tlllP." ' O*J:
NUCLELR POW [R PLANT TEFT I# sure as se e cusweg one enhuwer WAC #e'un NBA'allih
, , ,, 3 3 3 9 1 _ o p ;5 _
o ;0 0 l3 OF 0f expected to be as much as 13 degrees lower than actual. However, l l FitzPatrick procedures insure torus water circulation by requiring j initiation of the torus cooling mode of the RHR system during a stuck l open SRV discharge, high pressure coolant injection turbine (HPCI)
(RJ) or rise in torus water temperature above 95 degrees fahrenheit.
l The installation of the 16 RTD temperature monitoring system was accomplished in 1982 in response to NUREG 0661. Subsequent to this installation NUREG 0783 " Suppression Pool Temperature Limits for BWR Containments" was issued. Among the criteria in this document was guidance that " Operating procedures and alarm set points shall consider the relative accuracy of the measurement system."
Accordingly on 4/12/91 an instrument loop accuracy and setpoint uncertainty calculation (JAF-Calc-PC-00246), which included the results of the new NSSS vendor evaluation, was completed for the torus I water temperature instrumentation. The calculation concluded that a i maximum uncertainty of 3.52 fahrenheit degrees could exist for the indicat+ temperature displayed by the instrumentation. A modificc lon (M1-91-088) and nuclear safety evaluation (JAF-SE-91-038) were prepared to conservatively change the instrument software program to provide an indicated temperature to the operators which is 4 degrees higher than the temperature measured by the RTDs. The conservative change to the instrument software program was completed at 0330 on 4/12/91. The instrument was declared to be operable at 1723 upon completion of post work testing using an instrument surveillance procedure (ISP-28).
Cause:
One RTD was not installed in 1982 because a drill bit broke off in a thermowell during attempts to remove a burr which had prevented installation of the RTD. The broken bit could not be removed without risk of penetration through the thermowell wall into the torus which was filled with approximately 800,000 gallons of water. The torus hac not been drained from the date of installation through the current date.
If torus cooling circulation is not initiated as required by procedure, the absence of one of 16 RTDs may cause a potential primary element error of 1 fahrenheit degree in average torus temperature.
This is in addition to the 12 degree error caused by lack of circulation during the nonuniform addition of heat. Nonuniform addition of heat includes events such as the actuation of a single safety relief valve (AD) or initiation of the high pressure coolant injection system turbine (BJ). The absence of one of the 16 RTDs has l
no measurable effect on average torus temperature calculations during l localized heat addition so long as the procedurally required torus cooling circulation is initiated.
eenC sonae 3ees SMI
WAC p.rm 3sta y 8 NUCLEAR KtCUL ATOA Y COumatSB80m
. UCENSEE EVENT REPORT (LER) TEXT CONTINUATION anaoao owe no m4+
(1 All t '319%
factuTV haast et ovcalt tvuelm (2' Lf m Nuust# its pact ni 1 AM[$ A. Fll!P ATRICK .ia. %: ,p, . cy,p NUCl[ AR POWER PL ANT 9 1 o l5 lo lo jo ls l3 l3 1 0l 0l 5 _
0; o Op 0F 016 rm w - . - w s un un The new analysis by the NSSS vendor concluded that (with suppression pool circulation and localized heat addition) the existing system is expected to provide bulk torus temperatures no more than 1 fahrenheit degree below the actual value. The cause of this potential error is in the analysis extrapolations from the Monticello plant data to the FitzPatrick plant. This included consideration of differences in minimum and maximum torus radius, discharge quencher submergence, and the elevation location of the RTDs relative to both quencher discharge and total submergence. The FitzPatrick RTDs are located approximately 2 feet below the midpoint of normal torus water level. This is required because the dischargo quenchers are also located at a greater submergence level. This analytical uncertainty is designated as the primary element uncertainty. This was one input into the channel uncertainty calculation.
The total calculated instrument channel uncertainty of 3.5 degrees includes the primary element uncertainty of 1 degree in addition to the uncertainties introduced by the test and measuring equipment, and the instrument electronic components including summers, voltage to current converters, and resistance to voltage converters. These uncertainties are inherent in the design of the electronic components and represent the limits of accuracy of the instrument system.
Analysis LER 90-029 reported both torus water temperature channels as being inoperable from 10/26/89, the date on which the instrument software program was changed and a calculation error introduced, through 12/7/90 when a temporary modification was made to bypass the error.
During that period the average temperature displayed by the instrument was lower than the actual temperature by 3 to 4 fahrenheit degrees.
Accordingly in that event both channels were reported as being inoperable.
In the event now being reported, there was no actual occurrence of an erroneous temperature display. There was only the possibility for such an error. The maximum 3.5 degree low reading could only have occurred if there had been a nonuniform addition of heat to the torus accompanied by a simultaneous drift of multiple electronic components in the same low temperature direction to the maximum limit of instrument tolerance.
Although such an event is unlikely, it is being conservatively reported under the provisions of 10 CFR 50.73 (a) (2) (i) (B) as if both channels were inoperable. This would be an operation prohibited by Technical Specification Table 3.2-6 which requires a minimum of one operable channel.
An analysis (EAS-094-1288) has previously been performed which demonstrated a 4 degree margin between the calculated maximum local
. ,o..,,,,
hacpere 3sta U S Nucktaa Kloukat0AT Cohenesaton
. LICENSEE EVf.NT REPORT (LER) TEXT CONTIVMTION .p.aos to owe =o mo-e+
tapints sm es plotst y haeot m Ma t t sevesat a gi M A WG A i4> PA06 (38 J AMt$ A. FITIP ATRICK 4. "W;p W,p IluCLIAR POWER PL Alli 9 1 O16l01010l3l313 1 ol ol S -
ol n 0ls- or 0 l; nre a . == , mamm pool temperature and the limiting temperature calculated p accordance with NUREG 0738. The recently calculated potential maximum instrument l channel uncertainty of 3.5 degrees is within this 4 degree marCin. l In addition the instrumentation was checked and calibrated at six month intervals through use of an instrument surveillance procedure.
The amount of drift (which is one component of uncertainty) found during these checks was generally negligible and did not approach as much as 1 fahrenheit degree. The almost total ' 'ck of instrument drift documented during this interval confirms ,e inherent stability of the instrument and provides assurance that the max'l m uncertainty of 3.5 degrees is an unlikely extreme.
As reported in LER 90-029, during the period from 10/26/89 through 12/7/90 the instrument calculated average temperature was 3 degrees less than the actual torus temperature. This was caused by the introduction of errors into the instrument software program which resulted in averaging a false 30 degree temperature signal from the missing RTD with the current readings of the 15 remaining RTDs. This condition was corrected on 12/7/90.
An analysis of the safety significance of a the 3 to 4 degree error that existed from 10/26/89 through 12/7/90 was prepared in March 1991.
The report concluded that the actual error would not have had a safety significant effect on emergency operating procedure implementation and that the safety design bases were met. An informal review of this analysis on 5/9/91 was made to encompass the possibility of the additional non conservative uncertainty error of 3.5 degrees (for a total of 7.8 degrees). This second review reached the same conclusion.
During the periods from 12/88 (date the current torus water temperature instrumentation began to be used to meet technical specifications) through 10/26/89 (date of the introduction of a program error) , and from 12/7/90 (date of mitigating the program error) through 4/12/91 (date of introducing a conservative 4 degree bias into the program), the maximum 3.5 degree uncertainty was within the a degree margin to the calculated NUREG 0783 limit.
A review of the operating records found that the highest recorded torus water temperature during the period from 10/26/89 to date was 86 degrees. The addition of the 3.5 degree program error and the 3.5 degree uncertainty results in a maximum temperature of 93 degrees.
The is 2 degrees less than the technical specification limit of 95 degrees. This provides assurance that the actual average temperature of the torus was at all times within the Technical Specification limits.
Therefore, actual torus temperature was at all times within acceptable limits and there was never an actual or potential adverse effect on plant safety.
.g.o. m.
+ ,
se8tC f aM.. lata ,
W 8 WUC48 A2 ESEU4 Af 0av Conesequech UCENSEE EVENT REPORT (LER) TEXT CONTINUATION _ anaoveo oue w bio-o*
tapints e/3196 p&capty maast tu pocoet muesten us 40m huhettaisi pa04 tai J AM[$ A, fli!PAf tlCK .t.. at:,;;;- a'y,=,;;
NUCitAR POW [R PLAhi 0 l510 l0 l0 l 3 l 3 l3 9l 1 Og 0 gl6 or gj6 mt << - . -
- 0) 0) 5 _
sm .ac m. ,im Corrective Action
- 1. A conservative 4 degree bias was installed in the torus water instrumentation software program so that the displayed '
temperature will be four degrees higher than the actual temperature as sensed by the RTDs. This temperature bias provides an additional 4 degrees margin.to the limiting 4 degree margin evaluated in EAS-094-1288.
- 2. A temporary change was made tb operating procedure OP-15 "High Pressure Coolant Injection" on-4/12/91 to required initiation of torus cooling following initiation of the HPCI system.
Eglated-LERt 90-029 4 .O.w tasa
-___ _ _ -