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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045F6631993-06-25025 June 1993 LER 93-014-00 on 930529,logic Sys Functional Testing Was Incomplete Due to Test Procedure Deficiencies.Temporary Procedure Changes made.W/930625 Ltr ML20045D9081993-06-23023 June 1993 LER 93-013-00:on 930525,automatic Reactor Scram Occurred When APRM E Spiked While Indicated Water Level Approx 6%. Possibly Caused by Spiking of LPRM Input of APRM E. Radiation Sources Replaced W/Stronger sources.W/930623 Ltr ML20045D2971993-06-18018 June 1993 LER 93-012-00:on 930519,isolation Occurred When Rhr/Lpci Pump B Started in Shutdown Cooling Mode & Inboard & Outboard Isolation Valves Closed.Caused by Pressure Transient.Test Program Developed to Obtain Necessary data.W/930618 Ltr ML20045D1201993-06-16016 June 1993 LER 92-015-01:on 920317,deficiencies W/Potential to Effect Safe Shutdown During Postulated Fires Identified Due to Lack of Commitment to Fire Protection Implementation by Mgt.Plant Mods scheduled.W/930616 Ltr ML20045A3931993-06-0303 June 1993 LER 91-029-01:on 911130 & 1213,false Primary Containment High Radiation Isolation Sys Occurred.Caused by Filters Attached to Input of Monitors.Correct Operation of Isolation of Primary Containment Vent & Valves confirmed.W/930603 Ltr ML20044F6211993-05-19019 May 1993 LER 93-010-00:on 930420,HPCI Declared Inoperable Due to Grounded Electric Circuit on Turbine Steam Supply Valve. Caused by Personnel Inattention to Detail.Personnel Counseled Re Need for Attention to detail.W/930519 Ltr ML20044F6111993-05-19019 May 1993 LER 93-009-00:on 930420,noted That Abrupt Reduction in Feedwater Flow Resulted in Rapidly Decreasing Rwl.Caused by Loose Electrical Connection on Reactor Feed Pump A.Post Trip Evaluation Conducted to Prevent recurrence.W/930519 Ltr ML20044D2051993-05-11011 May 1993 LER 93-008-00:on 930412,identified That SJAE Radiation Monitor Had Increased.Caused by Failure to Identify Need to Obtain an Offgas Sample.Daily Instrument Surveillance Test changed.W/930511 Ltr ML20044B6181993-02-11011 February 1993 LER 93-035-01:on 920825,circuit Breaker Supplying Power to Load Ctr step-down Transformer Tripped Due to High Phase Current & Grounding.Caused by Deteriorated Transformer Coil Insulation.Transformer Rebuilt & reinstalled.W/920211 Ltr ML20024H0831991-05-13013 May 1991 LER 91-005-00:on 910412,torus Water Temp Instrumentation Declared Inoperable.Caused by Uncertainty of 3.52 F. Conservative 4 Degree Bias Installed in Torus Water Instrumentation Software program.W/910513 Ltr ML20024G6831991-04-17017 April 1991 LER 91-004-00:on 910318,unmonitored Release of Radioactivity Detected Outside Auxiliary Boiler Bldg.Caused by Personnel Error & Deficiencies in Procedures.Contaminated Surfaces Covered W/Reinforced Plastic covers.W/910417 Ltr ML20028H8611991-01-25025 January 1991 LER 90-025-01:on 901115 & 1226,in Total,Five Svc Water to Emergency Svc Water Swing Check Valves Failed to Close During Testing.Caused by Corrosion Problems.Valve Internals Replaced W/Stainless Steel components.W/910125 Ltr ML20028G9451990-09-25025 September 1990 LER 90-003-01:on 900129,core Overpower Events Occurred Due to Feed Flow Transmitter Calibr.Caused by Previously Unidentified Vendor Design Error,Error Introduced as Result of Plant Mod & Improper prioritization.W/900925 Ltr ML20043J0861990-06-21021 June 1990 LER 90-017-00:on 900526,instrument Setpoint Drift Exceeds Tech Spec Limit for HPCI Turbine Trip on High Reactor Water Level.Cause Unknown.Transmitter Included in Program for Weekly Monitoring of Rosemount transmitters.W/900621 Ltr ML20043B9831990-05-23023 May 1990 LER 90-016-00:on 900424,automatic Isolation Signal Closed Suction Valves from Reactor Water Recirculation Sys.On 900425,suction Valves Closed & RHR Pump Tripped.Caused by Chattering Pressure Switch.Switches replaced.W/900523 Ltr ML20043A9601990-05-21021 May 1990 LER 90-015-00:on 900420,discovered That Prerequisite Surveillance Test of source-range Monitors Not Performed Prior to Beginning Replacement of LPRMs on 900419.Caused by Procedure Deficiency.Lprm Procedure revised.W/900521 Ltr ML20042G8311990-05-10010 May 1990 LER 90-014-00:on 900410,primary Containment Isolation Check Valve Declared Inoperable Due to Missing Spring.Caused by Personnel Error.Performance of HPCI Turbine Exhaust Drain Sys Will Be Monitored During HPCI testing.W/900510 Ltr ML20042G8301990-05-0909 May 1990 LER 90-013-00:on 900409,shutdown Cooling Automatically Isolated During Transfer of Bus.Probably Caused by Contract Personnel Accidentally Knocking Jumper Loose.Procedures Re Controls on Jumpers Will Be revised.W/900505 Ltr ML20042F7531990-05-0303 May 1990 LER 90-012-00:on 900404,normal & Emergency Svc Water Valves Found to Be Inoperable.Caused by Excessive Build Up of Corrosion on Valve Surfaces & Accumulation of Silt.Valves Cleaned & Restored to svc.W/900503 Ltr ML20012E0071990-03-21021 March 1990 LER 90-005-00:on 900220,HPCI Sys Inoperable Resulting in 7 Day Limiting Condition for Operation.Caused by Sticking or Binding in Remote Servo.Remote Servo replaced.W/900321 Ltr ML20012C5161990-03-0909 March 1990 LER 90-004-00:on 900207,isolation of RCIC Sys Occurred, Resulting in Initiation of 7-day Limiting Condition of Operation.Caused by Failure of Master Trip Unit.Subj Unit replaced.W/900309 Ltr ML20012B4351990-03-0202 March 1990 LER 90-003-00:on 900129,when More Accurate Transmitters Placed in Svc,After Calibr Span Values Adjusted,Indicated Power Exceeded Core Thermal Power Limit.Caused by Incomplete Review of Manual.Transmitters recalibr.W/900302 Ltr ML20006E8621990-02-16016 February 1990 LER 90-001-00:on 900119,reactor Scram Occurred During Calibr of Reactor Water Level Instrumentation,Resulting in Valve Packing Leak & Causing False Low Water Level.Caused by Rapid Valve Movement.Event reviewed.W/900216 Ltr ML20006E9221990-02-15015 February 1990 LER 90-002-00:on 900215,reactor High Pressure Isolation Logic Tripped & Isolated RHR Shutdown Cooling Sys B as Sys Being Started.Hydraulic Pressure Transient Suspected as Cause.Operating Procedure revised.W/900215 Ltr ML20006E2101990-02-12012 February 1990 LER 89-019-01:on 891031,HPCI Turbine Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Conductive Corrosion Products Between Amphenol Type Connector & Mounting Plate.Connector cleaned.W/900212 Ltr ML20006E2291990-02-0808 February 1990 LER 89-018-01:on 891008,HPCI High Steam Flow Signal Closed HPCI Outboard Steam Supply Isolation Valves,Causing Isolation of Logic Circuit.Caused by Overly Conservative Value for Flow Isolation Signal.Sensor vented.W/900208 Ltr ML20011E1431990-01-29029 January 1990 LER 89-020-01:on 891105,reactor Scram Initiated by High APRM Neutron Flux from Pressure Transient from Turbine Control Valve Closure.Caused by Void Collapse in Core Moderator. Computer Programming Changed Re Transient data.W/900129 Ltr ML20006C1571990-01-26026 January 1990 LER 89-026-00:on 891105,reactor Scram from Full Power Occurred Due to Problems W/Turbine electro-hydraulic Control Sys.On 891220,contractor Notified Util That Valves Tested Did Not Actuate within Setpoint as required.W/900126 Ltr ML20005E8541990-01-0202 January 1990 LER 89-025-00:on 891130,isolation Signal Closed Outboard Isolation Valves on Steam Supply Line to HPCI Sys,Rendering HPCI Sys Inoperable & Initiating 7-day Limiting Condition for Operation.Caused by Excess steam.W/900102 Ltr ML20042D3961989-12-27027 December 1989 LER 89-024-00:on 891129,RCIC Sys Inoperable for 14 Minutes During Monthly Surveillance Test.Caused by Personnel Error. Outboard Isolation Valve Opened & Critique & Discussion W/ Technicians Held to Increase Event awareness.W/891227 Ltr ML20011D1351989-12-12012 December 1989 LER 89-023-00:on 891112,reactor Scram Occurred During Scheduled Surveillance Test of Safety Relief Valves.Caused by High Neutron Flux Signal Due to Steam Pressure Transient. Change Made to Surveillance Test ST-22B.W/891212 Ltr ML19332F4751989-12-0707 December 1989 LER 89-022-00:on 891107,determined That Elastomeric Seals in 33 Snubbers Had Not Been Replaced within Plant 7-yr Svc Life Guideline.Caused by Failures in Mgt of Maint Records. Snubbers Replaced as necessary.W/891207 Ltr ML19332F4511989-12-0505 December 1989 LER 89-020-00:on 891105,reactor Scram Occurred Due to Failure in Electronic Control Card of electro-hydraulic Control Sys.Caused by Void Collapse in Core Moderator. Circuit Boards Sent to Vendor for analysis.W/891205 Ltr ML19332E6241989-11-30030 November 1989 LER 89-019-00:on 891031 & 891103,HPCI Sys Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Buildup of Conductive Corrosion Products. Connector Cleaned & Sys Returned to svc.W/891130 Ltr ML19332F0471989-11-30030 November 1989 LER 89-021-00:on 891031,circuit Breaker for RCIC Inboard Injection Valve to Feedwater Sys Tripped During Required Valve Testing.Caused by Fault in Motor Winding Insulation. New Motor installed.W/891130 Ltr ML19325F2791989-11-13013 November 1989 LER 89-007-01:on 890509,surveillance of Fire Barrier Penetrations,Per Tech Spec 4.12.F Not Conducted within Allowed Time Period.Caused by Misinterpretation of Fire Protection Ref Manual.Fire Watch established.W/891113 Ltr ML19327C1351989-11-0707 November 1989 LER 89-015-01:on 890918,two Remote Manually Operated Diaphragm Air Operated Isolation Valves Failed Closing Time Acceptance Criteria.Caused by Buildup of Iron Oxide Sludge. Valves Disassembled & Cleaned ML19327B9821989-11-0606 November 1989 LER 89-018-00:on 891008,HPCI High Steam Flow Signal Closed Isolation Valves for Outboard Steam Supply & Steam Line Warning.Caused by Air in Sensing Sys Leading to Unstable Oscillation.Pressure Sensor Vented & calibr.W/891106 Ltr ML19324B1151989-10-23023 October 1989 LER 88-008-01:during 1988 Refuel Outage,One Primary Containment Penetration Exceeded Tech Spec 4.7.A.2.b Limit When Subjected to Local Leak Rate Testing.Leakage Attributed to Wear.Valves replaced.W/891023 Ltr ML19327B1521989-10-20020 October 1989 LER 89-017-00:on 890920,ESFAS Initiated Group II Primary Containment Isolation Signal Triggering RHR & LPCI Sys Isolations.Caused by Cognitive Human Error in Not Finding Isolation Signal.Fuse Replaced & Sys restarted.W/891020 Ltr ML19327B1501989-10-18018 October 1989 LER 89-016-00:on 890918,scram Signal Automatically Initiated During Transfer of Power Supply for Reactor Protection Sys. Caused by Lack of Caution Statement in Procedure.Procedure Revised to Add Time Caution for Bus transfers.W/891018 Ltr ML19327B1331989-10-18018 October 1989 LER 89-015-00:on 890918,two of Nine Remote Manually Operated Diaphragm Air Operated Containment Isolation Valves Failed Acceptance Criteria for Closing Time.Caused by Buildup & Hardening of Iron Oxide Sludge.Valves cleaned.W/891018 Ltr ML20024A8271983-06-20020 June 1983 LER 83-023/01T-0:on 830607,water Seepage Discovered from Weld in Stainless Steel Pipe Section of Control Rod Hydraulic Return Line.Caused by Intergranular Stress Corrosion Cracking.Piping Will Be removed.W/830620 Ltr ML20024A8571983-06-18018 June 1983 LER 83-021/03L-0:on 830605,rod Block Calibr Not Performed within 7 Days of 830603 Planned Reactor Shutdown.Caused by Inadequate Mgt Controls to Implement Tech Specs.Procedures to Be revised.W/830618 ML20024A8631983-06-16016 June 1983 LER 83-022/03L-0:on 830607,during Performance of Local Leak Rate Testing of Containment Spray,Penetration X-39A Found W/ Leakage That May Exceed Tech Spec Limits.Cause Undetermined. Details Will Be Provided within 30 days.W/830616 Ltr ML20028D6951983-01-11011 January 1983 LER 82-057/03L-0:on 821216,during Normal Operation,Reactor Scrammed on High Neutron Flux on Power Range Monitors. Caused by Reactor Pressure Spike Created by Sudden Closure of One MSIV Due to Improper Maint.Procedure Changed ML20027B5291982-09-10010 September 1982 LER 82-041/03X-1:on 820830,during Surveillance Test,Both Standby Liquid Control Sys Squib Valves Actuated.Caused by Operator Pulling Wrong Fuses.Operator Counseled ML20052F9721982-05-0303 May 1982 LER 82-003/01X-1:on 820302,during Normal Shutdown Operations,Only Two Intermediate Range Monitors in Trip Sys a Were Operable.Caused by Personnel Error & Inadequate Procedures.Procedures Revised ML20052E2811982-04-30030 April 1982 LER 82-017/03L-0:on 820402,MSIV 10% Closure Position Switches on Two Valves Did Not Trip When Tested.Caused by Mechanical Drift of Valve Position Switch Operating Cams. Adjustment Made ML20052C2511982-04-20020 April 1982 LER 82-005/01X-1:on 820315,during Normal Operation, Containment Oxygen Concentration Exceeded 4% Limit for Approx 6-h.Caused by Personnel Error.Startup Checkoff List Revised 1993-06-03
[Table view] Category:RO)
MONTHYEARML20045F6631993-06-25025 June 1993 LER 93-014-00 on 930529,logic Sys Functional Testing Was Incomplete Due to Test Procedure Deficiencies.Temporary Procedure Changes made.W/930625 Ltr ML20045D9081993-06-23023 June 1993 LER 93-013-00:on 930525,automatic Reactor Scram Occurred When APRM E Spiked While Indicated Water Level Approx 6%. Possibly Caused by Spiking of LPRM Input of APRM E. Radiation Sources Replaced W/Stronger sources.W/930623 Ltr ML20045D2971993-06-18018 June 1993 LER 93-012-00:on 930519,isolation Occurred When Rhr/Lpci Pump B Started in Shutdown Cooling Mode & Inboard & Outboard Isolation Valves Closed.Caused by Pressure Transient.Test Program Developed to Obtain Necessary data.W/930618 Ltr ML20045D1201993-06-16016 June 1993 LER 92-015-01:on 920317,deficiencies W/Potential to Effect Safe Shutdown During Postulated Fires Identified Due to Lack of Commitment to Fire Protection Implementation by Mgt.Plant Mods scheduled.W/930616 Ltr ML20045A3931993-06-0303 June 1993 LER 91-029-01:on 911130 & 1213,false Primary Containment High Radiation Isolation Sys Occurred.Caused by Filters Attached to Input of Monitors.Correct Operation of Isolation of Primary Containment Vent & Valves confirmed.W/930603 Ltr ML20044F6211993-05-19019 May 1993 LER 93-010-00:on 930420,HPCI Declared Inoperable Due to Grounded Electric Circuit on Turbine Steam Supply Valve. Caused by Personnel Inattention to Detail.Personnel Counseled Re Need for Attention to detail.W/930519 Ltr ML20044F6111993-05-19019 May 1993 LER 93-009-00:on 930420,noted That Abrupt Reduction in Feedwater Flow Resulted in Rapidly Decreasing Rwl.Caused by Loose Electrical Connection on Reactor Feed Pump A.Post Trip Evaluation Conducted to Prevent recurrence.W/930519 Ltr ML20044D2051993-05-11011 May 1993 LER 93-008-00:on 930412,identified That SJAE Radiation Monitor Had Increased.Caused by Failure to Identify Need to Obtain an Offgas Sample.Daily Instrument Surveillance Test changed.W/930511 Ltr ML20044B6181993-02-11011 February 1993 LER 93-035-01:on 920825,circuit Breaker Supplying Power to Load Ctr step-down Transformer Tripped Due to High Phase Current & Grounding.Caused by Deteriorated Transformer Coil Insulation.Transformer Rebuilt & reinstalled.W/920211 Ltr ML20024H0831991-05-13013 May 1991 LER 91-005-00:on 910412,torus Water Temp Instrumentation Declared Inoperable.Caused by Uncertainty of 3.52 F. Conservative 4 Degree Bias Installed in Torus Water Instrumentation Software program.W/910513 Ltr ML20024G6831991-04-17017 April 1991 LER 91-004-00:on 910318,unmonitored Release of Radioactivity Detected Outside Auxiliary Boiler Bldg.Caused by Personnel Error & Deficiencies in Procedures.Contaminated Surfaces Covered W/Reinforced Plastic covers.W/910417 Ltr ML20028H8611991-01-25025 January 1991 LER 90-025-01:on 901115 & 1226,in Total,Five Svc Water to Emergency Svc Water Swing Check Valves Failed to Close During Testing.Caused by Corrosion Problems.Valve Internals Replaced W/Stainless Steel components.W/910125 Ltr ML20028G9451990-09-25025 September 1990 LER 90-003-01:on 900129,core Overpower Events Occurred Due to Feed Flow Transmitter Calibr.Caused by Previously Unidentified Vendor Design Error,Error Introduced as Result of Plant Mod & Improper prioritization.W/900925 Ltr ML20043J0861990-06-21021 June 1990 LER 90-017-00:on 900526,instrument Setpoint Drift Exceeds Tech Spec Limit for HPCI Turbine Trip on High Reactor Water Level.Cause Unknown.Transmitter Included in Program for Weekly Monitoring of Rosemount transmitters.W/900621 Ltr ML20043B9831990-05-23023 May 1990 LER 90-016-00:on 900424,automatic Isolation Signal Closed Suction Valves from Reactor Water Recirculation Sys.On 900425,suction Valves Closed & RHR Pump Tripped.Caused by Chattering Pressure Switch.Switches replaced.W/900523 Ltr ML20043A9601990-05-21021 May 1990 LER 90-015-00:on 900420,discovered That Prerequisite Surveillance Test of source-range Monitors Not Performed Prior to Beginning Replacement of LPRMs on 900419.Caused by Procedure Deficiency.Lprm Procedure revised.W/900521 Ltr ML20042G8311990-05-10010 May 1990 LER 90-014-00:on 900410,primary Containment Isolation Check Valve Declared Inoperable Due to Missing Spring.Caused by Personnel Error.Performance of HPCI Turbine Exhaust Drain Sys Will Be Monitored During HPCI testing.W/900510 Ltr ML20042G8301990-05-0909 May 1990 LER 90-013-00:on 900409,shutdown Cooling Automatically Isolated During Transfer of Bus.Probably Caused by Contract Personnel Accidentally Knocking Jumper Loose.Procedures Re Controls on Jumpers Will Be revised.W/900505 Ltr ML20042F7531990-05-0303 May 1990 LER 90-012-00:on 900404,normal & Emergency Svc Water Valves Found to Be Inoperable.Caused by Excessive Build Up of Corrosion on Valve Surfaces & Accumulation of Silt.Valves Cleaned & Restored to svc.W/900503 Ltr ML20012E0071990-03-21021 March 1990 LER 90-005-00:on 900220,HPCI Sys Inoperable Resulting in 7 Day Limiting Condition for Operation.Caused by Sticking or Binding in Remote Servo.Remote Servo replaced.W/900321 Ltr ML20012C5161990-03-0909 March 1990 LER 90-004-00:on 900207,isolation of RCIC Sys Occurred, Resulting in Initiation of 7-day Limiting Condition of Operation.Caused by Failure of Master Trip Unit.Subj Unit replaced.W/900309 Ltr ML20012B4351990-03-0202 March 1990 LER 90-003-00:on 900129,when More Accurate Transmitters Placed in Svc,After Calibr Span Values Adjusted,Indicated Power Exceeded Core Thermal Power Limit.Caused by Incomplete Review of Manual.Transmitters recalibr.W/900302 Ltr ML20006E8621990-02-16016 February 1990 LER 90-001-00:on 900119,reactor Scram Occurred During Calibr of Reactor Water Level Instrumentation,Resulting in Valve Packing Leak & Causing False Low Water Level.Caused by Rapid Valve Movement.Event reviewed.W/900216 Ltr ML20006E9221990-02-15015 February 1990 LER 90-002-00:on 900215,reactor High Pressure Isolation Logic Tripped & Isolated RHR Shutdown Cooling Sys B as Sys Being Started.Hydraulic Pressure Transient Suspected as Cause.Operating Procedure revised.W/900215 Ltr ML20006E2101990-02-12012 February 1990 LER 89-019-01:on 891031,HPCI Turbine Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Conductive Corrosion Products Between Amphenol Type Connector & Mounting Plate.Connector cleaned.W/900212 Ltr ML20006E2291990-02-0808 February 1990 LER 89-018-01:on 891008,HPCI High Steam Flow Signal Closed HPCI Outboard Steam Supply Isolation Valves,Causing Isolation of Logic Circuit.Caused by Overly Conservative Value for Flow Isolation Signal.Sensor vented.W/900208 Ltr ML20011E1431990-01-29029 January 1990 LER 89-020-01:on 891105,reactor Scram Initiated by High APRM Neutron Flux from Pressure Transient from Turbine Control Valve Closure.Caused by Void Collapse in Core Moderator. Computer Programming Changed Re Transient data.W/900129 Ltr ML20006C1571990-01-26026 January 1990 LER 89-026-00:on 891105,reactor Scram from Full Power Occurred Due to Problems W/Turbine electro-hydraulic Control Sys.On 891220,contractor Notified Util That Valves Tested Did Not Actuate within Setpoint as required.W/900126 Ltr ML20005E8541990-01-0202 January 1990 LER 89-025-00:on 891130,isolation Signal Closed Outboard Isolation Valves on Steam Supply Line to HPCI Sys,Rendering HPCI Sys Inoperable & Initiating 7-day Limiting Condition for Operation.Caused by Excess steam.W/900102 Ltr ML20042D3961989-12-27027 December 1989 LER 89-024-00:on 891129,RCIC Sys Inoperable for 14 Minutes During Monthly Surveillance Test.Caused by Personnel Error. Outboard Isolation Valve Opened & Critique & Discussion W/ Technicians Held to Increase Event awareness.W/891227 Ltr ML20011D1351989-12-12012 December 1989 LER 89-023-00:on 891112,reactor Scram Occurred During Scheduled Surveillance Test of Safety Relief Valves.Caused by High Neutron Flux Signal Due to Steam Pressure Transient. Change Made to Surveillance Test ST-22B.W/891212 Ltr ML19332F4751989-12-0707 December 1989 LER 89-022-00:on 891107,determined That Elastomeric Seals in 33 Snubbers Had Not Been Replaced within Plant 7-yr Svc Life Guideline.Caused by Failures in Mgt of Maint Records. Snubbers Replaced as necessary.W/891207 Ltr ML19332F4511989-12-0505 December 1989 LER 89-020-00:on 891105,reactor Scram Occurred Due to Failure in Electronic Control Card of electro-hydraulic Control Sys.Caused by Void Collapse in Core Moderator. Circuit Boards Sent to Vendor for analysis.W/891205 Ltr ML19332E6241989-11-30030 November 1989 LER 89-019-00:on 891031 & 891103,HPCI Sys Declared Inoperable Due to Electrical Ground in Speed Control Circuit.Caused by Buildup of Conductive Corrosion Products. Connector Cleaned & Sys Returned to svc.W/891130 Ltr ML19332F0471989-11-30030 November 1989 LER 89-021-00:on 891031,circuit Breaker for RCIC Inboard Injection Valve to Feedwater Sys Tripped During Required Valve Testing.Caused by Fault in Motor Winding Insulation. New Motor installed.W/891130 Ltr ML19325F2791989-11-13013 November 1989 LER 89-007-01:on 890509,surveillance of Fire Barrier Penetrations,Per Tech Spec 4.12.F Not Conducted within Allowed Time Period.Caused by Misinterpretation of Fire Protection Ref Manual.Fire Watch established.W/891113 Ltr ML19327C1351989-11-0707 November 1989 LER 89-015-01:on 890918,two Remote Manually Operated Diaphragm Air Operated Isolation Valves Failed Closing Time Acceptance Criteria.Caused by Buildup of Iron Oxide Sludge. Valves Disassembled & Cleaned ML19327B9821989-11-0606 November 1989 LER 89-018-00:on 891008,HPCI High Steam Flow Signal Closed Isolation Valves for Outboard Steam Supply & Steam Line Warning.Caused by Air in Sensing Sys Leading to Unstable Oscillation.Pressure Sensor Vented & calibr.W/891106 Ltr ML19324B1151989-10-23023 October 1989 LER 88-008-01:during 1988 Refuel Outage,One Primary Containment Penetration Exceeded Tech Spec 4.7.A.2.b Limit When Subjected to Local Leak Rate Testing.Leakage Attributed to Wear.Valves replaced.W/891023 Ltr ML19327B1521989-10-20020 October 1989 LER 89-017-00:on 890920,ESFAS Initiated Group II Primary Containment Isolation Signal Triggering RHR & LPCI Sys Isolations.Caused by Cognitive Human Error in Not Finding Isolation Signal.Fuse Replaced & Sys restarted.W/891020 Ltr ML19327B1501989-10-18018 October 1989 LER 89-016-00:on 890918,scram Signal Automatically Initiated During Transfer of Power Supply for Reactor Protection Sys. Caused by Lack of Caution Statement in Procedure.Procedure Revised to Add Time Caution for Bus transfers.W/891018 Ltr ML19327B1331989-10-18018 October 1989 LER 89-015-00:on 890918,two of Nine Remote Manually Operated Diaphragm Air Operated Containment Isolation Valves Failed Acceptance Criteria for Closing Time.Caused by Buildup & Hardening of Iron Oxide Sludge.Valves cleaned.W/891018 Ltr ML20024A8271983-06-20020 June 1983 LER 83-023/01T-0:on 830607,water Seepage Discovered from Weld in Stainless Steel Pipe Section of Control Rod Hydraulic Return Line.Caused by Intergranular Stress Corrosion Cracking.Piping Will Be removed.W/830620 Ltr ML20024A8571983-06-18018 June 1983 LER 83-021/03L-0:on 830605,rod Block Calibr Not Performed within 7 Days of 830603 Planned Reactor Shutdown.Caused by Inadequate Mgt Controls to Implement Tech Specs.Procedures to Be revised.W/830618 ML20024A8631983-06-16016 June 1983 LER 83-022/03L-0:on 830607,during Performance of Local Leak Rate Testing of Containment Spray,Penetration X-39A Found W/ Leakage That May Exceed Tech Spec Limits.Cause Undetermined. Details Will Be Provided within 30 days.W/830616 Ltr ML20028D6951983-01-11011 January 1983 LER 82-057/03L-0:on 821216,during Normal Operation,Reactor Scrammed on High Neutron Flux on Power Range Monitors. Caused by Reactor Pressure Spike Created by Sudden Closure of One MSIV Due to Improper Maint.Procedure Changed ML20027B5291982-09-10010 September 1982 LER 82-041/03X-1:on 820830,during Surveillance Test,Both Standby Liquid Control Sys Squib Valves Actuated.Caused by Operator Pulling Wrong Fuses.Operator Counseled ML20052F9721982-05-0303 May 1982 LER 82-003/01X-1:on 820302,during Normal Shutdown Operations,Only Two Intermediate Range Monitors in Trip Sys a Were Operable.Caused by Personnel Error & Inadequate Procedures.Procedures Revised ML20052E2811982-04-30030 April 1982 LER 82-017/03L-0:on 820402,MSIV 10% Closure Position Switches on Two Valves Did Not Trip When Tested.Caused by Mechanical Drift of Valve Position Switch Operating Cams. Adjustment Made ML20052C2511982-04-20020 April 1982 LER 82-005/01X-1:on 820315,during Normal Operation, Containment Oxygen Concentration Exceeded 4% Limit for Approx 6-h.Caused by Personnel Error.Startup Checkoff List Revised 1993-06-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARJAFP-99-0277, Monthly Operating Rept for Sept 1999 Fpr Ja FitzPatrick Nuclear Power Plant.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 Fpr Ja FitzPatrick Nuclear Power Plant.With ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data JAFP-99-0261, Monthly Operating Rept for Aug 1999 for Jafnpp.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Jafnpp.With JAFP-99-0236, Monthly Operating Rept for July 1999 for Ja FitzPatrick Npp. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Ja FitzPatrick Npp. with ML20216D9541999-07-28028 July 1999 Safety Evaluation Authorizing Proposed Alternatives for Second 10-year Interval Pursuant to 10CFR50.55a(a)(3)(ii) ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept JAFP-99-0211, Monthly Operating Rept for June 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Ja FitzPatrick Nuclear Power Plant.With JAFP-99-0175, Annual Summary of Changes,Tests & Experiments for 1997/1998. with1999-06-0202 June 1999 Annual Summary of Changes,Tests & Experiments for 1997/1998. with JAFP-99-0181, Monthly Operating Rept for May 1999 for Jafnpp.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Jafnpp.With JAFP-99-0166, Monthly Operating Rept for Apr 1999 for Ja FitzPatrick Nuclear Plant.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Ja FitzPatrick Nuclear Plant.With JAFP-99-0142, Monthly Operating Rept for Mar 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ja FitzPatrick Nuclear Power Plant.With JAFP-99-0092, Monthly Operating Rept for Feb 1999 for Ja FitzPatrick Nuclear Power Plant.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ja FitzPatrick Nuclear Power Plant.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20202J0891999-02-0303 February 1999 Safety Evaluation Accepting Rev 2 of Third Interval Inservice Testing Program for Pumps & Valves for James a FitzPatrick Nuclear Power Plant ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc JAFP-99-0011, Monthly Operating Rept for Dec 1998 for Ja FitzPatrick Nuclear Power Plant.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Ja FitzPatrick Nuclear Power Plant.With ML20198F9991998-12-0404 December 1998 Assessment of Licensing Basis for Use of Containment Overpressure Credit for Net Positive Suction Head Analyses Power Authority of State of New York,James a Fitzpatrick Nuclear Power Plant ML20196J3501998-12-0404 December 1998 SER Accepting License Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves JAFP-98-0396, Monthly Operating Rept for Nov 1998 for Ja FitzPatrick Npp. with1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Ja FitzPatrick Npp. with ML20196F9251998-11-25025 November 1998 Safety Evaluation Re Thrid 10-year Interval Inservice Insp Program Relief Requests for Plant ML20195J7521998-11-18018 November 1998 Rev 7 to Jaf Colr ML20195K4211998-11-17017 November 1998 Safety Evaluation Authorizing Proposed Alternative in Relief Request VRR-05 Per 10CFR50.55a(a)(3)(i) & PRR-01,PRR-02R1, PRR-03,PRR-04,VRR-02,VRR-03 & VRR-04 Per 10CFR50.55a(a)(3)(ii) ML20195E1051998-11-13013 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves, Issued 950817 ML20197G6221998-11-0606 November 1998 Non-proprietary Rev 7 to HI-971661, Licensing Rept for Reracking of Ja FitzPatrick Sfp ML20155H5321998-11-0303 November 1998 Safety Evaluation Authorizing Alternative to ASME Code Requirements for CRD Bolting ML20155H5801998-11-0303 November 1998 Safety Evaluation Authorizing Postponement of Beginning of Augmented Exam Requirements of 10CFR50.55a(g)(6)(ii)(A)(2) Re ASME Code,Section XI JAFP-98-0360, Monthly Operating Rept for Oct 1998 for Ja FitzPatrick Nuclear Power Plant.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Ja FitzPatrick Nuclear Power Plant.With ML20155C2821998-10-30030 October 1998 Non-proprietary Rev 0 to GENE-187-30-1598 Np, CRD Bolting Flaw Evaluation for Ja FitzPatrick Nuclear Power Plant ML20154L6591998-10-14014 October 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Snubber Visual Inservice Exam Intervals & Sampling Rates Requirements Contained in ASME Code,Section Xi,Subsection Iwf,Article IWF-5000 JAFP-98-0322, Monthly Operating Rept for Sept 1998 for Ja Fitzpatrick Nuclear Power Plant.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Ja Fitzpatrick Nuclear Power Plant.With ML20153D2591998-09-21021 September 1998 SER Accepting Proposed Alternative Testing of Containment Following ECCS Suction Strainer Replacement ML20153B5611998-09-0101 September 1998 Rev 1 to JAF-SE-98-013, RHR & Core Spray Suppression Pool Suction Strainer Replacement ML20151X6891998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Ja FitzPatrick Nuclear Power Plant ML20237E8361998-08-25025 August 1998 Rev 6 to Colr ML20237E9471998-08-0808 August 1998 Rev 6 to Colr JAFP-98-0264, Monthly Operating Rept for July 1998 for Ja FitzPatrick Nuclear Plant1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Ja FitzPatrick Nuclear Plant ML20236X5881998-07-29029 July 1998 Safety Evaluation Supporting Amend 245 to License DPR-59 ML20236V8181998-07-29029 July 1998 Safety Evaluation Accepting Request for Relief from Implementation of Requirements of 10CFR50.55a Related to Containment Repair & Replacement Activities for James a FitzPatrick Nuclear Power Plant ML20153B5781998-07-28028 July 1998 Rev 0 to JAF-SE-98-025, HPCI & RCIC Suppression Pool Suction Strainer Replacement ML20236X3831998-07-14014 July 1998 Rev 2 to JAF-RPT-MULTI-02671, Summary of Detailed Evaluation for NRC Generic Ltr 96-06 ML20154L9201998-07-10010 July 1998 SER Accepting Rev to Reactor Vessel Surveillance Capsule Withdrawal Schedule for James a Fitzpatrick Nuclear Power Plant JAFP-98-0222, Monthly Operating Rept for June 1998 for Ja FitzPatrick Nuclear Power Plant1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Ja FitzPatrick Nuclear Power Plant JAFP-98-0193, Monthly Operating Rept for May 1998 for Ja FitzPatrick Nuclear Plant1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Ja FitzPatrick Nuclear Plant ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted JAFP-98-0168, Monthly Operating Rept for Apr 1998 for Ja FitzPatrick Nuclear Power Plant1998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Ja FitzPatrick Nuclear Power Plant JAFP-98-0128, Monthly Operating Rept for Mar 1998 for Ja FitzPatrick Nuclear Power Plant1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Ja FitzPatrick Nuclear Power Plant ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively JAFP-98-0091, Monthly Operating Rept for Feb 1998 for JAFNPP1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for JAFNPP ML20202G9081998-02-0606 February 1998 Safety Evaluation Re Amend to License DPR-59 to Revise TS Tables 3.2-2 & 4.2-2 JAFP-98-0058, Monthly Operating Rept for Jan 1998 for Ja FitzPatrick Nuclear Power Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Ja FitzPatrick Nuclear Power Plant 1999-09-30
[Table view] |
Text
-g F . . . . . ,
? James A.Pitupetrick t
94 .j p* e Nuolest Power Plant .
" P.O. Box 41 p, Lycoming, New York 13093 ..
316 342-3640 E William Femander 11 -
Resident Manager F
L' February 8,1990' JAFP-90-0117
. j United States Nuclear Regulatory Commission L' DocumentsControl Desk -t E . Mail Station PI-137 Washington, D.C. 20555 l i
SUBJECT:
DOCKET NO. 50'-333 j 89-018-01 LICENSEE EVENT REPORT:
High Pressure Coolant Injection i Turbine .
Dear Siri.
This-is a revision to the' Licensee Event Report which was t submitted in accordance with 10 CFR 50.73(a)(2)(iv) on u
November 30, 1989.
-This revision reflects changes to the cause and corrective actions resulting from the knowledge gained from-subsequent extensive testing;of the HPCI system in December 1989
.(LER-89-025). !
c Questions concerning this report may be addressed to-Mr. Hamilton Fish at (315) 349-6013.
.Very'truly yours, IL FERN IZ WF:HCF:lar I
. Enclosure ec: USNRC, Region I (l-USNRC Resident Inspector INPO Records Center 3 // ikp !
American Nuclear Insurers J pd iN Y
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Update Report - Original Report Date 11/06/89 - Change to Cause and Corrective Action A routine surveillance test of the High Pressure Coolant Injection (HPCI) [BJ) system l
was in progress on 10/08/89 at 14 percent power during start-up after a planned
! three-week maintenance outage. At 10:26 A.M., a HPCI high steam flow signal closed the HPCI outboard steam supply isolation valves. Operators verified the absence of steam leakage. The surveillance tests required to be performed when HPCI is
. inoperable were initiated.
( Inspection of the differential pressure transmitter, which provides the high steam flow signal, found the calibration was accurate. During recalibration a small quantity of air.was observed to vent from the pressure instrument sensing lines.
Initially, it was incorrectly believed that presence of non-condensible, but compressible air in the sensing lines, combined with the fast start transient, resulted in oscillations and a false high steam flow signal. Subsequently I I
l (LER-89-025), it was dircovered that the high steam flow signal was valid and caused by use of a more conservative test procedure and overly conservative Technical Specification high steam flow and FSAR activation time limits.
1 Upon satisfactory performance of the surveillance test, HPCI was returned to service at 6:30 P M the same day.
LER-89-025 and LER-89-002 are related.
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Revised. February- 8, 1990 to reflect changes to cause and corrective actions. Previous report date 11/06/89.
Description j On October 8, 1989 the plant was engaged in power ascension and had achieved a level of 14 percent of full power following start-up from a '
planned three-week maintenance outage. Performance of Surveillance '
. Test ST-4N. "HPCI Flow Rate and In-Service Test (IST)" for the High-Pressure Coolant Injection (HPCI) system [BJ) was in progress. Tais test is performed at low pressure during start-up and agzin at normal operating pressure in accordance with Technical Specifications and Section XI of the ASME code. The purpose is to demonstrate pump and turbine-flow capacity, cycle isolation valves, and collect data for the '
IST: program. '
At 10:26 A.M. during HPCI turbine start-up, the "High Steam Flow" ,
annunciator alarmed and outboard steam supply isolation valve 23MOV-16 '
- and steam line warming isolation valve 23MOV-60 automatically closed to isolate the HPCI steam line.
Operators immediately inspected the HPCI steam line and turbine' areas._ .
There was no evidence of steam leakage. HPCI was-declared inoperable, '
, Required HPCI inoperability surveillance testin; of alternate systems was initiated. Instrumentation and Control technicians checked the high flow instrument _ system calibration which was satisfactory. A small quantity of air was observed to vent from the sensing line during recalibration. The cause for the high steam flow signal was initially and incorrectly believed to have been the presence of this air in the sensingtline to the steam flow differential pressure transmitters.
The HPCILsurveillance test was then performed successfully. HPCI was restored to service at-6:30 P.M.- A subsequent high steam flow isolation of HPCI on November 30, 1989 (LER-89-025) led-to extensive testing over a period of'several weeks which established other root
-causes.
Cause The cause of the automatic isolation was the initiation of the HPCI steam line high flow isolation logic circuit. Air in the sensing system leading to potentially unstable oscillation of the differential pressure signal was initially and incorrectly believed to be the cause offthe high steam flow signal which isolated the HPCI turbine. The function of this circuit is to stop steam flow from the reactor in the event of-a steam line break outside the primary containment, g,, o.. u.,
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When steam flows to HPCI, a measurable differential pressure is created between the instrument taps on the inner and outer radii of the elbow
'in the steam supply piping system inside the primary containment.
Combined differential pressure sensors and transmitters send signals o to a master trip unit (MTU). The signal strength is proportional to the magnitude of the differential pressure. The trip point is adjusted to a differential pressure signal strength which is equivalent to a steam flow of 300 percent of normal full load flow.
The pressure sensing line to the transmitter is filled with liquid to provide a relatively incompressible transmission medium. During the inspection and recalibration of the sensor transmitter (following the isolation) a small quantity of air was observed to vent from the liquid-filled sensing line at the transmitter. The presence of compressible air pockets in the small diameter sensing line or pressure chambers may have created a condition conducive to unstable compression and oscillation in the sensing line during periods of rapid change in the steam flow which exist during fast start of the HPCI turbine. A '
similar isolation of the Reactor Core Isolation Cooling (RCIC) [BN) .i system occurred in 1986 (LER-86-015). The source of air entry for that event was the previous-replacement of a transmitter unit followed by inadequate venting. However, the transmitter for the HPCI system had not been opened for testing or corrective maintenance for approximately a year. On November 30, 1989 the HPCI system was again isolated by a
-high steam flow signal during surveillance testing (LER-89-025).
Following this isolation extensive testing and research of documentation established that the isolation signal was electrically-correct but the setpoint, limits, and assumptions upon which the setpoint was based were overly conservative. The HPCI system was able to be operated within this conservatism for 14 years until several changes were made within the HPCI system including test methodology, new hydraulic actuator,_and correction of a construction error in wiring of the turbine stop valve (see LER-89-002). These changes, combined with an unnecessarily conservative design basis for response L time,.resulted in measured transient steam flows occasionally exceeding l the existing isolation setpoint. There was also a failure to fully appreciate the integrated nature of the control system which led to a failure to sufficiently test and analyze HPCI transients following procedural changes and component replacement.
A summary of these four causes follows:
1
- 1. Overly conservative value for high steam flow isolation signal:
Although the FSAR Section 7.4.3.2.7 uses an analytical limit for determination of a break in the HPCI steam line of 300% rated flow, testo have shown that the Technical Specification setpoint isolates at a differential pressure equivalent to only 200% of rated flow.
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- 2. Change to make test procedure more conservative For fourteen years HPCI had been tested by fully opening the -
discharge test valve (23MOV-21) to the CST prior to starting the turbine. In March 1989, acting on INPO recommendations, the i discharge test valve was manually pre-positioned to simulate the discharge head against reactor pressure during the pump speed ramp rather than first opening the valve and then closing down on it to obtain the required discharge pressure. In addition, a requirement to measure the HPCI response time from initiation to full rated flow against an acceptance criteria of 25 seconds was added to the procedure. The result of these changes was a demand for higher initial steam flow to provide the energy required for higher initial discharge pressures and to meet the response time criteria.
- 3. Overly conservative FSAR design basis for HPC1 response time:
The FSAR actuation time for HPCI was defined as 25 seconds from receipt of reactor vessel low low water level or high drywell ,
pressure signals to achievement of rated flow. This requirement i was in the original vendor design specification. More recent plant specific analysis for 10CFR50.46, Appendix K, and based on vendor SAFER /GESTR LOCA application methodology, redefines HPCI response time parameters. The assumed value in the analysis is 30 seconds. The current fuel reload analysis also assumes this value. Other documentation clearly defines this as the time to achieve rated flow and does not require that the discharge valve be in the full open position for HPCI to be considered to be fully actuated. The result of the 25 second requirement was a higher initial steam flow demand and resulting potential for system isolation.
- 4. Failure to appreciate the integrated nature of the HPCI control system:
This led to the associated failure to test and analyze the test start-up transient stability in sufficient depth following changes to the test procedure, adjustment of cemponent controls, and replacement of individual components in the control system.
) Adjustment to a single et st r o l c o m p o n et.*. may require readjustment i of all other interfacing controls. An integrated system test is required to establish and readjust each enterfacing control system !
component in the start-up and speed control system following i significant maintenance.
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in sufficient volume to maintain core coverage through a broad spectrum of hypothetical accident conditions. The principal component is a turbine-driven high pressure, high volume multi-stage centrifugal pump. ;
The steam supply to the turbine comes directly from the reactor vessel !
thus ensuring availability regardless of the condition of AC electric power supplies.
Because the HPCI system was inoperable due to an isolation signal, it i qualifies as an event reportable under 10 CFR 50.73(a)(2)(v) as a ,
condition that alone could have prevented the fulfillment of the safety function of a system needed to remove residual heat or mitigate the consequences of an accident. It is also reportable under 10 CFR 50,73(a)(2)(iv) as an activation of an engineered safety feature ,
for isolation. ;
Surveillance tests of back-up emergency core cooling systems were successfully completed or in progress during the eight-hour investigation of possible causes of the isolation.
If the HPCI system had continued to be unavailable, core coverage would still have been assured by the automatic depressurization system together with low pressure emergency core cooling systems including the two core spray systems [BM) and four residual heat removal (Lew Pressure Coolant Injection) systems [B0].
Furthermore, the HPCI system remained operable ct the manual mode at '
all times. The SAFER /GESTER LOCA sensitivity analysis shows that the HPCI response time has little effect on peak clad temperature. !
Corrective Action:
Short-Term: j The aressure sensor and transmitter units were immediately vented and calibrated. The system was restored to service within eight hours of the isolation event.
Following the extensive testing of the HPCI system (LER-89-025) and determination of the true root causes of the HFCI high steam flow isolation signal, the following corrective actions were accomplished:
- 1. The HPCI turbine start-up speed control ramp speed was adjusted to a new recommended value of 15 seconds.
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- 2. Technical Specification Tabic 3.2-2, Item 13 was amended to reflect a maximum mermitted high steam flow differential pressure e setting of 160 inches of water.
- 3. The HPCI steam supply line high steam flow differential pressure instrumentation setpoint was changed to 148 inches of water which correctly corresponds to approximately 300% of rated steam flow. i
- 4. Surveillance Test 4N, "HPCI Flow Rate and Inservice Test (IST)"
and 4B, "HPCI pump and MOV Operability Test" were revised to reflect the 30 second limit on response time for HPCI and closer control in determination of that response time. :
- 5. The FSAR was revised to reflect a 30 second response time for HPCI i as the design basis.
Long-Term: *
- 1. A detailed engineering review of the complete HPCI system and its operating history will be performed. Further corrective actions may be recommended by the task force assigned to this review.
- 2. Existing surveillance procedures will be revised or new procedures will be developed to monitor and trend the HPCI start-up transient performance stability including peak flow measurements. This will facilitate identification of potential 1 degrading of the HPCI control system prior to entering a condition where the HPCI system would not fulfill its design requirement.
Additional Information This supplement revises the original LER report of November 30, 1989 to reflect the knowledge gained during the extensive testing of HPCI in December 1989 (LER-89-025). This supplement revises the causes and corrective actions.
LER-89-002 HPCI wiring error between steam stop valve and speed control ramp generator LER-89-025 HPCI isolated due to high steam flow
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