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| issue date = 07/26/1996
| issue date = 07/26/1996
| title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
| title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
| author name = Grimes B K
| author name = Grimes B
| author affiliation = NRC/NRR
| author affiliation = NRC/NRR
| addressee name =  
| addressee name =  
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| document type = NRC Information Notice
| document type = NRC Information Notice
| page count = 10
| page count = 10
| revision = 0
}}
}}
{{#Wiki_filter:K) K) July 26, 1996NRC INFORMATION NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER TEMPERATUREON NUCLEAR INSTRUMENTATION
{{#Wiki_filter:K)                               Ij
 
K)
                                  UNITED STATES
 
NUCLEAR REGULATORY COMMISSION
 
OFFICE OF NUCLEAR REACTOR REGULATION
 
WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41:   EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE
 
ON NUCLEAR INSTRUMENTATION


==Addressees==
==Addressees==
All holders of operating licenses or construction permits for pressurizedwater reactors (PWRs).
All holders of operating licenses or construction permits for pressurized
 
water reactors (PWRs).


==Purpose==
==Purpose==
The U.S. Nuclear Regulatory Commission (NRC) is issuing this informationnotice to alert addressees to the potential for operation above licensed poweras a result of a decrease in feedwater temperature event affecting nuclearinstrumentation. It is expected that recipients will review the informationfor applicability to their facilities and consider actions, as appropriate, toavoid similar problems. However, suggestions contained in this informationnotice are not NRC requirements; therefore, no specific action or writtenresponse is required.
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
 
notice to alert addressees to the potential for operation above licensed power
 
as a result of a decrease in feedwater temperature event affecting nuclear
 
instrumentation. It is expected that recipients will review the information
 
for applicability to their facilities and consider actions, as appropriate, to
 
avoid similar problems. However, suggestions contained in this information
 
notice are not NRC requirements; therefore, no specific action or written
 
response is required.


==Description of Circumstances==
==Description of Circumstances==
On February 14, 1996, the licensee for the Comanche Peak Steam ElectricStation was operating Unit 2 at 95 percent rated thermal power near end-of-core life when a significant reduction in feedwater temperature occurredbecause of the loss of feedwater heaters. This reduction, in turn, caused areduction in the reactor coolant system cold-leg temperatures. The colderreactor coolant temperature, with a large negative moderator temperaturecoefficient, caused reactor power to increase to approximately 102 percentaccording to ex-core nuclear instrumentation. The nitrogen-16 (N-16)detection system reached the overpower turbine runback setpoint (109 percent)and initiated a turbine runback. The N-16 detection system measures N-16activity in the primary coolant as a measure of the total power generation.This system is a substitute for the resistance temperature detector over-temperature and over-power reactor trip functions used at other WestinghousePWRs. The plant stabil zed at an indicated power of approximately 97 percentaccording to the ex-core nuclear instrumentation.After approximately 90 minutes, a second similar turbine runback occurredwhile restoring balance-of-plant equipment. Following this runback, reactorpower was stabilized at approximately 100 percent according to nuclearinstrumentation. During the next 30 minutes, the reactor was operated atapproximately 100 percent power as indicated by nuclear instrumentation, withreactor coolant temperatures below normal. The licensee noted that the N-169607220l60ujo i 7 9,oi4(R ~IE ctG IN 96-41July 26, 1996 detection system indicated approximately 106 percent power and the computer-based plant calorimetric system indicated approximately 102 percent power.Subsequently, the reactor power was reduced to less than 100 percent by allindications.DiscussionThere are three aspects of this event which have generic implications. First,with a loss of secondary plant efficiency, programmed T e can no longerreliably represent core thermal power. Second, the venturi-based input intothe computer-based calorimetric system may not be accurate with coldfeedwater. And third, the final safety analysis report had not analyzed thistransient accurately.Following the second runback, operators noted that reactor power indicated<100 percent according to nuclear instrumentation. Although the operatorsknew that cold feedwater could cause an increase in the amount of neutronattenuation, they believed that the nuclear instrumentation indicatedconservatively (i.e., higher than actual) because they were maintaining TA"eapproximately 1.7 eC [3 OF] above TRef. The licensee could not use thecomputer-based calorimetric until some time after the second turbine runbackdue to maintenance activities. Te , based on the main turbine impulsepressure, is programmed as a functlon of turbine load and, for normalefficiency, is a good representation of thermal power. When the unit lost thefeedwater heaters, the plant efficiency decreased. Because the main turbineelectro-hydraulic control system maintained generator output, core thermalpower increased to account for the loss of efficiency, and thus, TRef nolonger accurately represented the core thermal power.The cold-leg temperature is a more appropriate indicator of the accuracy ofthe nuclear instrumentation than programmed TY.e. As the cold-leg temperaturedecreased, the amount of neutron attenuation in the downcomer area surroundingthe core increased and hence affected the amount of neutrons reaching thedetectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold-leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8percent power. A review of the second transient showed that the cold-legtemperature was approximately 2.5 &deg;C [4.5 OF] lower than when the detectorswere last calibrated. This corresponded to a 3 to 4 percent error, whichcorresponded to the difference in the actual versus the indicated power (104percent actual versus 100 percent indicated).During the review, the licensee noted that the computer-based calorimetric was4 percent lower than the actual thermal power (N-16 power monitor). Thecalorimetric was based on feedwater flow measured by venturis. Although thecalorimetric calculation used feedwater temperature as an input, temperaturessignificantly different than the normal 227 OC [440 OF] introduced errors intothe calculation.Finally, the actual events involved temperature and power levels that exceededthose in the analysis of the Decrease in Feedwater Temperature" eventpresented in Chapter 15 of the licensee final safety analysis report. In that IN 96-41July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve,coupled with the trip of the heater drain pumps, resulted in a feedwatertemperature drop of less than 19 'C (35 OF], and a corresponding powerincrease of less than 10 percent. In the actual event, the feedwatertemperature dropped by approximately 111 &deg;C (200 OF], and the licenseecalculated that reactor power would have increased by approximately 35 percentwithout operator or protective actions. The licensee determined that althoughthe initiating events were the same, the Chapter 15 analysis did not accountfor the loss of extraction steam to the high-pressure heaters, which was thecause of the temperature difference. During the event, a level imbalanceoccurred between the two heater drain tanks, which resulted in the isolationof extraction steam.The NRC staff review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the Comanche Peak analysis and had similar conclusions concerningthe amount of feedwater temperature drop. The licensee has reanalyzed theevent to include a 119 OC [246 OF] feedwater temperature drop and concludedthat all accident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts: Harry A. Freeman, RIV(817) 897-1500E-mail: haf~nrc.govChu-Yu Liang, NRR(301) 415-2878E-mail: cylenrc.gov
On February 14, 1996, the licensee for the Comanche Peak Steam Electric
 
Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred
 
because of the loss of feedwater heaters. This reduction, in turn, caused a
 
reduction in the reactor coolant system cold-leg temperatures. The colder
 
reactor coolant temperature, with a large negative moderator temperature
 
coefficient, caused reactor power to increase to approximately 102 percent
 
according to ex-core nuclear instrumentation. The nitrogen-16 (N-16)
detection system reached the overpower turbine runback setpoint (109 percent)
and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation.
 
This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse
 
PWRs. The plant stabil zed at an indicated power of approximately 97 percent
 
according to the ex-core nuclear instrumentation.
 
After approximately 90 minutes, a second similar turbine runback occurred
 
while restoring balance-of-plant equipment. Following this runback, reactor
 
power was stabilized at approximately 100 percent according to nuclear
 
instrumentation. During the next 30 minutes, the reactor was operated at
 
approximately 100 percent power as indicated by nuclear instrumentation, with
 
reactor coolant temperatures below normal. The licensee noted that the N-16
9607220l 60ujo    i                         7             9,oi4 (R ~IE               ctG
 
IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power.
 
Subsequently, the reactor power was reduced to less than 100 percent by all
 
indications.
 
Discussion
 
There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer
 
reliably represent core thermal power. Second, the venturi-based input into
 
the computer-based calorimetric system may not be accurate with cold
 
feedwater. And third, the final safety analysis report had not analyzed this
 
transient accurately.
 
Following the second runback, operators noted that reactor power indicated
 
<100 percent according to nuclear instrumentation. Although the operators
 
knew that cold feedwater could cause an increase in the amount of neutron
 
attenuation, they believed that the nuclear instrumentation indicated
 
conservatively (i.e., higher than actual) because they were maintaining TA"e
 
approximately 1.7 eC [3 OF] above TRef. The licensee could not use the
 
computer-based calorimetric until some time after the second turbine runback
 
due to maintenance activities. Te , based on the main turbine impulse
 
pressure, is programmed as a functlon of turbine load and, for normal
 
efficiency, is a good representation of thermal power. When the unit lost the
 
feedwater heaters, the plant efficiency decreased. Because the main turbine
 
electro-hydraulic control system maintained generator output, core thermal
 
power increased to account for the loss of efficiency, and thus, TRef no
 
longer accurately represented the core thermal power.
 
The cold-leg temperature is a more appropriate indicator of the accuracy of
 
the nuclear instrumentation than programmed TY.e. As the cold-leg temperature
 
decreased, the amount of neutron attenuation in the downcomer area surrounding
 
the core increased and hence affected the amount of neutrons reaching the
 
detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg
 
temperature was approximately 2.5 &deg;C [4.5 OF] lower than when the detectors
 
were last calibrated. This corresponded to a 3 to 4 percent error, which
 
corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated).
 
During the review, the licensee noted that the computer-based calorimetric was
 
4 percent lower than the actual thermal power (N-16 power monitor). The
 
calorimetric was based on feedwater flow measured by venturis. Although the
 
calorimetric calculation used feedwater temperature as an input, temperatures
 
significantly different than the normal 227 OC [440 OF] introduced errors into
 
the calculation.
 
Finally, the actual events involved temperature and power levels that exceeded
 
those in the analysis of the Decrease in Feedwater Temperature" event
 
presented in Chapter 15 of the licensee final safety analysis report. In that
 
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
 
temperature drop of less than 19 'C (35 OF], and a corresponding power
 
increase of less than 10 percent. In the actual event, the feedwater
 
temperature dropped by approximately 111 &deg;C (200 OF], and the licensee
 
calculated that reactor power would have increased by approximately 35 percent
 
without operator or protective actions. The licensee determined that although
 
the initiating events were the same, the Chapter 15 analysis did not account
 
for the loss of extraction steam to the high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction steam.
 
The NRC staff review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the Comanche Peak analysis and had similar conclusions concerning
 
the amount of feedwater temperature drop. The licensee has reanalyzed the
 
event to include a 119 OC [246 OF] feedwater temperature drop and concluded
 
that all accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts: Harry A. Freeman, RIV
 
(817) 897-1500
                    E-mail: haf~nrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 E-mail: cylenrc.gov
 
Attachment:  List Of Recently Issued HRC Information Notices
 
A1h4              Stir      A  Je6tQ
 
K>                            KJ
 
Attachment
 
IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED
 
NRC INFORMATION NOTICES
 
Information                                  Date of
 
Notice No.            Subject                Issuance  Issued to
 
96-40          Deficiencies in Material      07/25/96    All holders of OLs or CPs
 
Dedication and Procure-                  for nuclear power reactors
 
ment Practices and in
 
Audits of Vendors
 
96-09,        Damage in Foreign Steam        07/10/96  All holders of OLs or CPs
 
Supp. 1        Generator Internals                      for pressurized-water
 
reactors
 
96-39          Estimates of Decay Heat      07/05/96    All holders of OLs or CPs
 
Using ANS 5.1 Decay Heat                  for nuclear power reactors
 
Standard May Vary Signi- ficantly
 
96-38          Results of Steam Generator    06/21/96    All holders of OLs or CPs
 
Tube Examinations                        for pressurized water
 
reactors
 
96-37          Inaccurate Reactor Water      06/18/96  All pressurized water
 
Level Indication and Inad-                reactor facilities holding
 
vertent Draindown During                  an operating license or a
 
Shutdown                                  construction permit
 
96-36          Degradation of Cooling        06/12/96  All holders of OLs or CPs
 
Water Systems Due to Icing                for nuclear power reactors
 
96-35          Failure of Safety Systems      06/11/96  All U.S. Nuclear Regulatory
 
on Self-Shielded Irradia-                Commission irradiator
 
tors Because of Inadequate                licensees and vendors
 
Maintenance and Training
 
96-34          Hydrogen Gas Ignition          05/31/96  All holders of OLs or CPs
 
during Closure Welding                    for nuclear power reactors
 
of a VSC-24 Multi-Assembly
 
Sealed Basket
 
OL - Operating License
 
CP - Construction Permit
 
*~  -                        K>                                          K
 
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
 
temperature drop of less than 19 *C [35 OF], and a corresponding power
 
increase of less than 10 percent. In the actual event, the feedwater
 
temperature dropped by approximately 111 *C [200 OF], and the licensee
 
calculated that reactor power would have increased by approximately 35 percent
 
without operator or protective actions. The licensee determined that although
 
the initiating events were the same, the Chapter 15 analysis did not account
 
for the loss of extraction steam to the high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction steam.
 
The NRC staff review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the Comanche Peak analysis and had similar conclusions concerning
 
the amount of feedwater temperature drop. The licensee has reanalyzed the
 
event to include a 119 *C [246 OF] feedwater temperature drop and concluded
 
that all accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice,-please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Original signed by Brian K.Grimes
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        E-mail: haf@nrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 E-mail: cyl~nrc.gov
 
Attachment:      List of Recently Issued NRC Information Notices
 
DOCUMENT NAME:        G:\SSK2\INFONOT.C P
 
To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N
 
* No
 
cops
 
OFFICE        C                  BC:SRXBI          BC:LPECB lI        (A)DW M          i
 
NAME          CYLiang*            RJones*          AChaffee*
                HAFreeman*        ____                                          _
  DATE        16/ 3/96            16/21/96          17/08/96          17LI/96            I
 
OFFILIAL MLLUM LWUF
 
* See previous concurrence Tech Editor reviewed & concurred on 05/28/96
 
~1~1                  -,K)
                                                                                            IN 96-XX
 
July XX, 1996 for the loss of extraction steam to ti              he high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction steam.
 
The NRC staff review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the Comanche Peak analysis and had similar conclusions concerning
 
the amount of feedwater temperature drop. The licensee has reanalyzed the
 
event to include a 119 'C [246 'F] feedwater temperature drop and concluded
 
that all accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        E-mail: haf~nrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 E-mail: cyl~nrc.gov
 
Attachment: List of Recently Issued NRC Information Notices
 
DOCUMENT NAME: G:\SSK2\INFONOT.C P
 
To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N
 
* No
 
OFFICE      l        kd          BC: SRXB          BC:PECB              )D:DR
 
NAME          CYLiang*            RJones*            AChaffee*          BGrimes
 
HAFreeman*
  DATE          6/ 3/96            6/21/96            7/08/96            7/ /96 OFFICIAL RECORD COPY
 
*See    previous concurrence
 
IN 96-XX
 
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction steam.
 
The NRC staff review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the licensee analysis and had similar conclusions concerning the
 
amount of feedwater temperature drop. The licensee has reanalyzed the event
 
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
 
include a 119 'c [246 OF] feedwater temperature drop and concluded that all
 
accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        E-mail: haftnrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 E-mail: cyl~nrc.gov
 
Attachment: List of Recently Issued NRC Information Notices
 
DOCUMENT NAME: G:\SSK2\INFONOT.C P
 
To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No
 
copy
 
OFFICE        CONT:i  kd l        BC:SRXBLl          BC:iPECB lI        (A)iD:iDRPM I    _
  NAME          CYLiang*            RJones*            AChaffee*          BGrimes
 
l      _    HAFreeman*
  DATE          6/ 3/96            6/21/96            7/08/96            7/ /96 OFFICIAL KLLUKV        UV    X!
* See previous concurrence
 
IN 96-XX
 
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction steam.
 
The NRC staff review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the licensee analysis and had similar conclusions concerning the
 
amount of feedwater temperature drop. The licensee has reanalyzed the event
 
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
 
include a 119 *C [246 *F] feedwater temperature drop and concluded that all
 
accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        Internet:haf@nrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 Internet:cyl nrc.gov
 
Attachment: List of Recently Issued NRC Information Notices
 
DOCUMENT NAME: G:\SSK2\INFONOT.C P
 
To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N
 
* No
 
OFFICE        CONT:      Ekd      BC: SLB            BC:PECB            (A)D:DRPM
 
NAME          CYLiang*            RJones*            ACh)f              BGrimes
 
l    ~~HAFreeman*tVt
 
DATE          6/ 3/96            6/21/96            7/7/96            7/ /96 OFFICIAL RECOR        COPY
 
*  See previous concurrence
 
K-, /
                                                                                            IN 96-XX
 
June XX, 1996 for the loss of extraction steam to ti              he high-pressure heaters, which was the
 
cause of the temperature difference. During the event, a level imbalance
 
occurred between the two heater drain tanks, which resulted inthe isolation
 
of extraction steam.
 
The NRC staff's review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the licensee's analysis and had similar conclusions concerning the
 
amount of feedwater temperature drop. The licensee has reanalyzed the event
 
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
 
include a 119 'C [246 OF] feedwater temperature drop and concluded that all
 
accident analysis parameters remained within requirements.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        Internet:haffnrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 Internet:cyl@nrc.gov
 
Attachment: List of Recently Issued NRC Information Notices
 
DOCUMENT NAME: G:\SSK2\INFONOT.CP
 
To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC  Ioith attachment/enclosure 1
* No copy
 
OFFICE        CONT:jkd _l        BC: SRXB          EC:PECB I      _    A)D:DRPM I
 
NAME          CYLiang*            RJones            AChaffee          BGrimes
 
HAFreeman*                  I-        _
  DATE          6/ 3/96            6/2j /96          6/ /96            6/ /96 OFFICIAL RECORD COPY
 
*  See previous concurrence
 
IN 96-XX
 
June XX, 1996 detection system. The licensee believed that this system would probably not
 
be significantly affected by feedwater temperatures because of a different
 
mass flow rate determination method.
 
Finally, the licensee's final safety analysis report did not accurately
 
analyze this transient. The actual events were similar to the analysis of the
 
'Decrease in Feedwater Temperature event presented in Chapter 15. In that
 
analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
 
temperature drop of less than 35 OF, and a corresponding power increase of
 
less than 10 percent. In the actual event, the feedwater temperature dropped
 
by approximately 200 OF, and the licensee calculated that reactor power would
 
have increased by approximately 35 percent without operator or protective
 
actions. The licensee determined that although the initiating events were the
 
same, the Chapter 15 analysis did not account for the loss of extraction steam
 
to the high-pressure heaters, which was the cause of the temperature
 
difference. During the event, a level imbalance occurred between the two
 
heater drain tanks, which resulted in the isolation of extraction steam.
 
The NRC staff's review of analyses of feedwater temperature events at similar
 
facilities revealed that most of these analyses assumed similar initiating
 
events as the licensee's analysis and had similar conclusions concerning the
 
amount of feedwater temperature drop.
 
This information notice requires no specific action or written response. If
 
you have any questions about the information in this notice, please contact
 
one of the technical contacts listed below or the appropriate Office of
 
Nuclear Reactor Regulation project manager.
 
Brian K. Grimes, Acting Director
 
Division of Reactor Program Management
 
Office of Nuclear Reactor Regulation
 
Technical contacts:          Harry A. Freeman, RIV
 
(817) 897-1500
                                        Internet:haf@nrc.gov
 
Chu-Yu Liang, NRR
 
(301) 415-2878 Internet:cyl nrc.gov


===Attachment:===
Attachment: List of Recently Issued NRC Information Notices
List Of Recently Issued HRC Information NoticesA1h4 Stir A Je6tQ K> KJAttachmentIN 96-41July 26, 1996 LIST OF RECENTLY ISSUEDNRC INFORMATION NOTICESInformation Date ofNotice No. Subject Issuance Issued to96-4096-09,Supp. 196-3996-38Deficiencies in MaterialDedication and Procure-ment Practices and inAudits of VendorsDamage in Foreign SteamGenerator InternalsEstimates of Decay HeatUsing ANS 5.1 Decay HeatStandard May Vary Signi-ficantlyResults of Steam GeneratorTube ExaminationsInaccurate Reactor WaterLevel Indication and Inad-vertent Draindown DuringShutdownDegradation of CoolingWater Systems Due to IcingFailure of Safety Systemson Self-Shielded Irradia-tors Because of InadequateMaintenance and TrainingHydrogen Gas Ignitionduring Closure Weldingof a VSC-24 Multi-AssemblySealed Basket07/25/9607/10/9607/05/9606/21/9606/18/9606/12/9606/11/9605/31/96All holders of OLs or CPsfor nuclear power reactorsAll holders of OLs or CPsfor pressurized-waterreactorsAll holders of OLs or CPsfor nuclear power reactorsAll holders of OLs or CPsfor pressurized waterreactorsAll pressurized waterreactor facilities holdingan operating license or aconstruction permitAll holders of OLs or CPsfor nuclear power reactorsAll U.S. Nuclear RegulatoryCommission irradiatorlicensees and vendorsAll holders of OLs or CPsfor nuclear power reactors96-3796-3696-3596-34OL -Operating LicenseCP -Construction Permit
*~ -K> KIN 96-41July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve,coupled with the trip of the heater drain pumps, resulted in a feedwatertemperature drop of less than 19 *C [35 OF], and a corresponding powerincrease of less than 10 percent. In the actual event, the feedwatertemperature dropped by approximately 111 *C [200 OF], and the licenseecalculated that reactor power would have increased by approximately 35 percentwithout operator or protective actions. The licensee determined that althoughthe initiating events were the same, the Chapter 15 analysis did not accountfor the loss of extraction steam to the high-pressure heaters, which was thecause of the temperature difference. During the event, a level imbalanceoccurred between the two heater drain tanks, which resulted in the isolationof extraction steam.The NRC staff review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the Comanche Peak analysis and had similar conclusions concerningthe amount of feedwater temperature drop. The licensee has reanalyzed theevent to include a 119 *C [246 OF] feedwater temperature drop and concludedthat all accident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice,-please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Original signed by Brian K. GrimesBrian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts: Harry A. Freeman, RIV(817) 897-1500E-mail: haf@nrc.govChu-Yu Liang, NRR(301) 415-2878E-mail: cyl~nrc.gov


===Attachment:===
DOCUMENT NAME: G:\SSK2\INFONOT.C P
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.C PTo receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N
* NocopsOFFICE C BC:SRXB I BC:LPECB lI (A) DW M iNAME CYLiang* RJones* AChaffee*HAFreeman* ____ _DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 IOFFILIAL MLLUM LWUF* See previous concurrence Tech Editor reviewed & concurred on 05/28/96
~1~1 -,K)IN 96-XXJuly XX, 1996 for the loss of extraction steam to ticause of the temperature difference.occurred between the two heater drainof extraction steam.he high-pressure heaters, which was theDuring the event, a level imbalancetanks, which resulted in the isolationThe NRC staff review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the Comanche Peak analysis and had similar conclusions concerningthe amount of feedwater temperature drop. The licensee has reanalyzed theevent to include a 119 'C [246 'F] feedwater temperature drop and concludedthat all accident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts:Harry A. Freeman, RIV(817) 897-1500E-mail: haf~nrc.govChu-Yu Liang, NRR(301) 415-2878E-mail: cyl~nrc.gov


===Attachment:===
To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-with attachment/enclosure N
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.C PTo receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N
* NoOFFICE l kd BC: SRXB BC:PECB )D:DRNAME CYLiang* RJones* AChaffee* BGrimesHAFreeman*DATE 6/ 3/96 6/21/96 7/08/96 7/ /96OFFICIAL RECORD COPY*See previous concurrence IN 96-XXJuly XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was thecause of the temperature difference. During the event, a level imbalanceoccurred between the two heater drain tanks, which resulted in the isolationof extraction steam.The NRC staff review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the licensee analysis and had similar conclusions concerning theamount of feedwater temperature drop. The licensee has reanalyzed the eventpursuant to Section 50.59 of Title 10 of the Code of Federal Regulations toinclude a 119 'c [246 OF] feedwater temperature drop and concluded that allaccident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts: Harry A. Freeman, RIV(817) 897-1500E-mail: haftnrc.govChu-Yu Liang, NRR(301) 415-2878E-mail: cyl~nrc.gov


===Attachment:===
* No copy
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.C PTo receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N NocopyOFFICE CONT:i kd l BC:SRXBLl BC:iPECB lI (A)iD:iDRPM I _NAME CYLiang* RJones* AChaffee* BGrimesl _ HAFreeman*DATE 6/ 3/96 6/21/96 7/08/96 7/ /96* See previous concurrenceOFFICIAL KLLUKV UV X!
IN 96-XXJuly XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was thecause of the temperature difference. During the event, a level imbalanceoccurred between the two heater drain tanks, which resulted in the isolationof extraction steam.The NRC staff review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the licensee analysis and had similar conclusions concerning theamount of feedwater temperature drop. The licensee has reanalyzed the eventpursuant to Section 50.59 of Title 10 of the Code of Federal Regulations toinclude a 119 *C [246 *F] feedwater temperature drop and concluded that allaccident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts: Harry A. Freeman, RIV(817) 897-1500Internet:haf@nrc.govChu-Yu Liang, NRR(301) 415-2878Internet:cyl nrc.gov


===Attachment:===
OFFICE      lCONT:kd l            BC:SRXB l          BC:PECB l          (A)D:DRPM
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.C PTo receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N
* NoOFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPMNAME CYLiang* RJones* ACh)f BGrimesl ~~HAFreeman*tVtDATE 6/ 3/96 6/21/96 7/7/96 7/ /96OFFICIAL RECOR COPY* See previous concurrence K-, /IN 96-XXJune XX, 1996 for the loss of extraction steam to ticause of the temperature difference.occurred between the two heater drainof extraction steam.he high-pressure heaters, which was theDuring the event, a level imbalancetanks, which resulted in the isolationThe NRC staff's review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the licensee's analysis and had similar conclusions concerning theamount of feedwater temperature drop. The licensee has reanalyzed the eventpursuant to Section 50.59 of Title 10 of the Code of Federal Regulations toinclude a 119 'C [246 OF] feedwater temperature drop and concluded that allaccident analysis parameters remained within requirements.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts:Harry A. Freeman, RIV(817) 897-1500Internet:haffnrc.govChu-Yu Liang, NRR(301) 415-2878Internet:cyl@nrc.gov


===Attachment:===
NAME         CYLiang 9          RJones             AChaffee           BGrimes
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.CPTo receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnCOFFICE CONT:jkd _l BC: SRXB E C:PECB I _ A)D:DRPM INAME CYLiang* RJones AChaffee BGrimesHAFreeman* I- _DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96OFFICIAL RECORD COPYIoith attachment/enclosure 1
* No copy* See previous concurrence IN 96-XXJune XX, 1996 detection system. The licensee believed that this system would probably notbe significantly affected by feedwater temperatures because of a differentmass flow rate determination method.Finally, the licensee's final safety analysis report did not accuratelyanalyze this transient. The actual events were similar to the analysis of the'Decrease in Feedwater Temperature event presented in Chapter 15. In thatanalysis, the inadvertent opening of the low-pressure heater bypass valve,coupled with the trip of the heater drain pumps, resulted in a feedwatertemperature drop of less than 35 OF, and a corresponding power increase ofless than 10 percent. In the actual event, the feedwater temperature droppedby approximately 200 OF, and the licensee calculated that reactor power wouldhave increased by approximately 35 percent without operator or protectiveactions. The licensee determined that although the initiating events were thesame, the Chapter 15 analysis did not account for the loss of extraction steamto the high-pressure heaters, which was the cause of the temperaturedifference. During the event, a level imbalance occurred between the twoheater drain tanks, which resulted in the isolation of extraction steam.The NRC staff's review of analyses of feedwater temperature events at similarfacilities revealed that most of these analyses assumed similar initiatingevents as the licensee's analysis and had similar conclusions concerning theamount of feedwater temperature drop.This information notice requires no specific action or written response. Ifyou have any questions about the information in this notice, please contactone of the technical contacts listed below or the appropriate Office ofNuclear Reactor Regulation project manager.Brian K. Grimes, Acting DirectorDivision of Reactor Program ManagementOffice of Nuclear Reactor RegulationTechnical contacts: Harry A. Freeman, RIV(817) 897-1500Internet:haf@nrc.govChu-Yu Liang, NRR(301) 415-2878Internet:cyl nrc.gov


===Attachment:===
HAFreema        r   _                  _
List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:\SSK2\INFONOT.C PTo receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C with attachment/enclosure N
  DATE            /96                   /96         6/ /96             6/ /96 OFFICIAL RECORD COPY}}
* No copyOFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPMNAME CYLiang 9 RJones AChaffee BGrimesHAFreema r _ _DATE /96 /96 6/ /96 6/ /96OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 04:38, 24 November 2019

Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
ML031060009
Person / Time
Site: Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant  Entergy icon.png
Issue date: 07/26/1996
From: Grimes B
Office of Nuclear Reactor Regulation
To:
References
IN-96-041, NUDOCS 9607220160
Download: ML031060009 (10)


K) Ij

K)

UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE

ON NUCLEAR INSTRUMENTATION

Addressees

All holders of operating licenses or construction permits for pressurized

water reactors (PWRs).

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information

notice to alert addressees to the potential for operation above licensed power

as a result of a decrease in feedwater temperature event affecting nuclear

instrumentation. It is expected that recipients will review the information

for applicability to their facilities and consider actions, as appropriate, to

avoid similar problems. However, suggestions contained in this information

notice are not NRC requirements; therefore, no specific action or written

response is required.

Description of Circumstances

On February 14, 1996, the licensee for the Comanche Peak Steam Electric

Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred

because of the loss of feedwater heaters. This reduction, in turn, caused a

reduction in the reactor coolant system cold-leg temperatures. The colder

reactor coolant temperature, with a large negative moderator temperature

coefficient, caused reactor power to increase to approximately 102 percent

according to ex-core nuclear instrumentation. The nitrogen-16 (N-16)

detection system reached the overpower turbine runback setpoint (109 percent)

and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation.

This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse

PWRs. The plant stabil zed at an indicated power of approximately 97 percent

according to the ex-core nuclear instrumentation.

After approximately 90 minutes, a second similar turbine runback occurred

while restoring balance-of-plant equipment. Following this runback, reactor

power was stabilized at approximately 100 percent according to nuclear

instrumentation. During the next 30 minutes, the reactor was operated at

approximately 100 percent power as indicated by nuclear instrumentation, with

reactor coolant temperatures below normal. The licensee noted that the N-16

9607220l 60ujo i 7 9,oi4 (R ~IE ctG

IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power.

Subsequently, the reactor power was reduced to less than 100 percent by all

indications.

Discussion

There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer

reliably represent core thermal power. Second, the venturi-based input into

the computer-based calorimetric system may not be accurate with cold

feedwater. And third, the final safety analysis report had not analyzed this

transient accurately.

Following the second runback, operators noted that reactor power indicated

<100 percent according to nuclear instrumentation. Although the operators

knew that cold feedwater could cause an increase in the amount of neutron

attenuation, they believed that the nuclear instrumentation indicated

conservatively (i.e., higher than actual) because they were maintaining TA"e

approximately 1.7 eC [3 OF] above TRef. The licensee could not use the

computer-based calorimetric until some time after the second turbine runback

due to maintenance activities. Te , based on the main turbine impulse

pressure, is programmed as a functlon of turbine load and, for normal

efficiency, is a good representation of thermal power. When the unit lost the

feedwater heaters, the plant efficiency decreased. Because the main turbine

electro-hydraulic control system maintained generator output, core thermal

power increased to account for the loss of efficiency, and thus, TRef no

longer accurately represented the core thermal power.

The cold-leg temperature is a more appropriate indicator of the accuracy of

the nuclear instrumentation than programmed TY.e. As the cold-leg temperature

decreased, the amount of neutron attenuation in the downcomer area surrounding

the core increased and hence affected the amount of neutrons reaching the

detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg

temperature was approximately 2.5 °C [4.5 OF] lower than when the detectors

were last calibrated. This corresponded to a 3 to 4 percent error, which

corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated).

During the review, the licensee noted that the computer-based calorimetric was

4 percent lower than the actual thermal power (N-16 power monitor). The

calorimetric was based on feedwater flow measured by venturis. Although the

calorimetric calculation used feedwater temperature as an input, temperatures

significantly different than the normal 227 OC [440 OF] introduced errors into

the calculation.

Finally, the actual events involved temperature and power levels that exceeded

those in the analysis of the Decrease in Feedwater Temperature" event

presented in Chapter 15 of the licensee final safety analysis report. In that

IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 19 'C (35 OF], and a corresponding power

increase of less than 10 percent. In the actual event, the feedwater

temperature dropped by approximately 111 °C (200 OF], and the licensee

calculated that reactor power would have increased by approximately 35 percent

without operator or protective actions. The licensee determined that although

the initiating events were the same, the Chapter 15 analysis did not account

for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 OC [246 OF] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf~nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cylenrc.gov

Attachment: List Of Recently Issued HRC Information Notices

A1h4 Stir A Je6tQ

K> KJ

Attachment

IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

Information Date of

Notice No. Subject Issuance Issued to

96-40 Deficiencies in Material 07/25/96 All holders of OLs or CPs

Dedication and Procure- for nuclear power reactors

ment Practices and in

Audits of Vendors

96-09, Damage in Foreign Steam 07/10/96 All holders of OLs or CPs

Supp. 1 Generator Internals for pressurized-water

reactors

96-39 Estimates of Decay Heat 07/05/96 All holders of OLs or CPs

Using ANS 5.1 Decay Heat for nuclear power reactors

Standard May Vary Signi- ficantly

96-38 Results of Steam Generator 06/21/96 All holders of OLs or CPs

Tube Examinations for pressurized water

reactors

96-37 Inaccurate Reactor Water 06/18/96 All pressurized water

Level Indication and Inad- reactor facilities holding

vertent Draindown During an operating license or a

Shutdown construction permit

96-36 Degradation of Cooling 06/12/96 All holders of OLs or CPs

Water Systems Due to Icing for nuclear power reactors

96-35 Failure of Safety Systems 06/11/96 All U.S. Nuclear Regulatory

on Self-Shielded Irradia- Commission irradiator

tors Because of Inadequate licensees and vendors

Maintenance and Training

96-34 Hydrogen Gas Ignition 05/31/96 All holders of OLs or CPs

during Closure Welding for nuclear power reactors

of a VSC-24 Multi-Assembly

Sealed Basket

OL - Operating License

CP - Construction Permit

  • ~ - K> K

IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 19 *C [35 OF], and a corresponding power

increase of less than 10 percent. In the actual event, the feedwater

temperature dropped by approximately 111 *C [200 OF], and the licensee

calculated that reactor power would have increased by approximately 35 percent

without operator or protective actions. The licensee determined that although

the initiating events were the same, the Chapter 15 analysis did not account

for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 *C [246 OF] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice,-please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Original signed by Brian K.Grimes

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N

  • No

cops

OFFICE C BC:SRXBI BC:LPECB lI (A)DW M i

NAME CYLiang* RJones* AChaffee*

HAFreeman* ____ _

DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 I

OFFILIAL MLLUM LWUF

  • See previous concurrence Tech Editor reviewed & concurred on 05/28/96

~1~1 -,K)

IN 96-XX

July XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 'C [246 'F] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf~nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N

  • No

OFFICE l kd BC: SRXB BC:PECB )D:DR

NAME CYLiang* RJones* AChaffee* BGrimes

HAFreeman*

DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL RECORD COPY

  • See previous concurrence

IN 96-XX

July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 'c [246 OF] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haftnrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No

copy

OFFICE CONT:i kd l BC:SRXBLl BC:iPECB lI (A)iD:iDRPM I _

NAME CYLiang* RJones* AChaffee* BGrimes

l _ HAFreeman*

DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL KLLUKV UV X!

  • See previous concurrence

IN 96-XX

July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 *C [246 *F] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N

  • No

OFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPM

NAME CYLiang* RJones* ACh)f BGrimes

l ~~HAFreeman*tVt

DATE 6/ 3/96 6/21/96 7/7/96 7/ /96 OFFICIAL RECOR COPY

  • See previous concurrence

K-, /

IN 96-XX

June XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted inthe isolation

of extraction steam.

The NRC staff's review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee's analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 'C [246 OF] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haffnrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.CP

To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC Ioith attachment/enclosure 1

  • No copy

OFFICE CONT:jkd _l BC: SRXB EC:PECB I _ A)D:DRPM I

NAME CYLiang* RJones AChaffee BGrimes

HAFreeman* I- _

DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96 OFFICIAL RECORD COPY

  • See previous concurrence

IN 96-XX

June XX, 1996 detection system. The licensee believed that this system would probably not

be significantly affected by feedwater temperatures because of a different

mass flow rate determination method.

Finally, the licensee's final safety analysis report did not accurately

analyze this transient. The actual events were similar to the analysis of the

'Decrease in Feedwater Temperature event presented in Chapter 15. In that

analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 35 OF, and a corresponding power increase of

less than 10 percent. In the actual event, the feedwater temperature dropped

by approximately 200 OF, and the licensee calculated that reactor power would

have increased by approximately 35 percent without operator or protective

actions. The licensee determined that although the initiating events were the

same, the Chapter 15 analysis did not account for the loss of extraction steam

to the high-pressure heaters, which was the cause of the temperature

difference. During the event, a level imbalance occurred between the two

heater drain tanks, which resulted in the isolation of extraction steam.

The NRC staff's review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee's analysis and had similar conclusions concerning the

amount of feedwater temperature drop.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C with attachment/enclosure N

  • No copy

OFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPM

NAME CYLiang 9 RJones AChaffee BGrimes

HAFreema r _ _

DATE /96 /96 6/ /96 6/ /96 OFFICIAL RECORD COPY