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| "This letter serves as an Interim Report in accordance with 10 CFR 21.21 pertaining to a potential defect associated with a design basis calculation delivered to First Energy Nuclear Operating Company's Perry Nuclear Power Plant. Subsequent to delivering this calculation, FL0-2D software errors were identified which resulted in erroneous outputs that affect the local intense precipitation calculation. These errors were discovered on September 28, 2016, at which time, ENERCON generated a Corrective Action Report (CAR) to address the issue. | | "This letter serves as an Interim Report in accordance with 10 CFR 21.21 pertaining to a potential defect associated with a design basis calculation delivered to First Energy Nuclear Operating Company's Perry Nuclear Power Plant. Subsequent to delivering this calculation, FL0-2D software errors were identified which resulted in erroneous outputs that affect the local intense precipitation calculation. These errors were discovered on September 28, 2016, at which time, ENERCON generated a Corrective Action Report (CAR) to address the issue. |
| ENERCON has initiated a reevaluation of the calculation using the latest version of the software that will correct the errors in the calculation. | | ENERCON has initiated a reevaluation of the calculation using the latest version of the software that will correct the errors in the calculation. |
| "An evaluation of the reportability of this issue in accordance with 1O CFR Part 21 is not able to be completed within the 60-day evaluation period due the need to verify and validate the latest version of the software and then complete all the analysis required for updating the calculation. This evaluation is being tracked by CAR 2016-0335 and will be completed no later than February 10, 2017. | | "An evaluation of the reportability of this issue in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due the need to verify and validate the latest version of the software and then complete all the analysis required for updating the calculation. This evaluation is being tracked by CAR 2016-0335 and will be completed no later than February 10, 2017. |
| "If you have any questions or need further clarifying information, please contact Nick Eggemeyer, Corporate Quality Assurance Manager, at (770) 590-2031." | | "If you have any questions or need further clarifying information, please contact Nick Eggemeyer, Corporate Quality Assurance Manager, at (770) 590-2031." |
| ***UPDATE AT 0910 EST ON 12/13/2016 FROM TIMOTHY CLEARY TO MARK ABRAMOVITZ*** | | ***UPDATE AT 0910 EST ON 12/13/2016 FROM TIMOTHY CLEARY TO MARK ABRAMOVITZ*** |
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| ==Subject:== | | ==Subject:== |
| [External_Sender] 10 CFR Part 21 Interim Report Attachments: lOCFR Part 21 Interim Report - Perry Nuclear Plant Calculation Error.pdf To: NRC Operations Center Attached find a 10 CFR Part 21 Interim Report regarding a design basis calculation error using FL0-20 software. | | [External_Sender] 10 CFR Part 21 Interim Report Attachments: 10CFR Part 21 Interim Report - Perry Nuclear Plant Calculation Error.pdf To: NRC Operations Center Attached find a 10 CFR Part 21 Interim Report regarding a design basis calculation error using FL0-20 software. |
| Please acknowledge receipt of this email. | | Please acknowledge receipt of this email. |
| Best regards, | | Best regards, |
Revision as of 14:02, 10 November 2019
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1211312016 U.S. Nuclear Regulatory Commission Operations Center Event Report Pagel Part 21 (PAR) Event# 52394 Rep Org: ENERCON Notification Date I Time: 11/23/2016 11 :56 (EST)
Supplier: ENERCON Event Date I Time: 09/28/2016 (EST)
Last Modification: 12/13/2016 Region: 1 Docket#:
City: KENNESAW Agreement State: Yes County: License#:
State: GA NRC Notified by: NICK EGGEMEYER Notifications: JAMES DWYER R1DO HQ Ops Officer: MARK ABRAMOVITZ AARON McGRAW R3DO Emergency Class: NON EMERGENCY PART 21/50.55 REACTORS EMAIL 10 CFR Section:
21.21 (a)(2) INTERIM EVAL OF DEVIATION PART-21 NOTIFICATION - DESIGN BASIS ERRORS USING FL0-2D SOFTWARE The following report was received via e-mail:
"This letter serves as an Interim Report in accordance with 10 CFR 21.21 pertaining to a potential defect associated with a design basis calculation delivered to First Energy Nuclear Operating Company's Perry Nuclear Power Plant. Subsequent to delivering this calculation, FL0-2D software errors were identified which resulted in erroneous outputs that affect the local intense precipitation calculation. These errors were discovered on September 28, 2016, at which time, ENERCON generated a Corrective Action Report (CAR) to address the issue.
ENERCON has initiated a reevaluation of the calculation using the latest version of the software that will correct the errors in the calculation.
"An evaluation of the reportability of this issue in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due the need to verify and validate the latest version of the software and then complete all the analysis required for updating the calculation. This evaluation is being tracked by CAR 2016-0335 and will be completed no later than February 10, 2017.
"If you have any questions or need further clarifying information, please contact Nick Eggemeyer, Corporate Quality Assurance Manager, at (770) 590-2031."
- UPDATE AT 0910 EST ON 12/13/2016 FROM TIMOTHY CLEARY TO MARK ABRAMOVITZ***
The following update was received via e-mail:
"This letter serves as an amendment to the 10 CFR 21.21 Interim Report filed on November 23, 2016, pertaining
1211312016 U.S. Nuclear Regulatory Commission Operations Center Event Report Page 2 to a potential defect associated with a design basis calculation delivered to First Energy Nuclear Operating Company's Perry Nuclear Power Plant. Subsequent to delivery of the calculation, a standard, periodic review of the FL0-20 Pro software supplier website indicated that a new build of this software (version 16.06.16) had been issued. It replaced the software build (version 14.08.09) that was used for the above referenced design calculation. As a result of the model revision associated with FL0-20, it was determined that the outputs were impacted which could affect this design basis calculation. These output changes were discovered on September 28, 2016, at which time ENERCON generated a Corrective Action Report (CAR) to address the issue. ENERCON has initiated a reevaluation of the calculation using this new build of the FL0-20 Pro software.
"An evaluation of the reportability of this issue in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due the need to verify and validate the latest version of the software and then complete all the analysis required for updating the calculation. This evaluation is being tracked by CAR 2016-0335 and will be completed no later than February 10, 2017.
"If you have any questions or need further clarifying information, please contact Nick Eggemeyer, Corporate Quality Assurance Manager, at (770) 590-2031."
Notified the R1 DO (Schroeder}, R3DO (Cameron}, and Part 21 Group (via e-mail).