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| ==Dear Sir:== | | ==Dear Sir:== |
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| SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT*NO. 2 LICENSEE.EVENT REPORT 92-004-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a} (2) (iv). This report is* required to be issued within thirty (30) days of event discovery. | | SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT*NO. 2 LICENSEE.EVENT REPORT 92-004-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a} (2) (iv). This report is* required to be issued within thirty (30) days of event discovery. |
| ]ely yours, C. A. Vondra General Manager ~ | | ]ely yours, C. A. Vondra General Manager ~ |
| Salem Operations MJP:pc Distribution 9204200203 920413 PDR ADOCK 05000311 S PDR | | Salem Operations MJP:pc Distribution 9204200203 920413 PDR ADOCK 05000311 S PDR |
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| Witn the loss of the 2B 460 VAC *vital Bus, the No... 22 RM Distribution panel de-energized. The 2R1B Radiation Monitoring System (RMS} {ILi channel is* powered via the No. 22 RM Distribution panel. A new UPS was installed* during the current refueling outage which includes a self* contained battery. DC power supplied to the inverter allowed the 22 RM Distribution Panel to remain energized. Wilen the battery voltage decayed to 105 VDC the inverter automatically shutdown (per design} . Consequently, de-eri.ergization of the 2R1B RMS channel . | | Witn the loss of the 2B 460 VAC *vital Bus, the No... 22 RM Distribution panel de-energized. The 2R1B Radiation Monitoring System (RMS} {ILi channel is* powered via the No. 22 RM Distribution panel. A new UPS was installed* during the current refueling outage which includes a self* contained battery. DC power supplied to the inverter allowed the 22 RM Distribution Panel to remain energized. Wilen the battery voltage decayed to 105 VDC the inverter automatically shutdown (per design} . Consequently, de-eri.ergization of the 2R1B RMS channel . |
| caused a signal for Control Room Ventilation Switch to the Emergency | | caused a signal for Control Room Ventilation Switch to the Emergency |
| *Mode of Operation (both Units) .at 2305 hours (per design). This signal is an Engineered Safety Feature. Therefore, the Nuclear Regulatory Commission. was notified on March 15, 1992, at 0008 hours-in accordance with Code of Federal Regulations lOCFR 50.72(b)(2) (ii) | | *Mode of Operation (both Units) .at 2305 hours (per design). This signal is an Engineered Safety Feature. Therefore, the Nuclear Regulatory Commission. was notified on March 15, 1992, at 0008 hours-in accordance with Code of Federal Regulations 10CFR 50.72(b)(2) (ii) |
| APPARENT CAUSE OF OCCURRENCE: | | APPARENT CAUSE OF OCCURRENCE: |
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| ANALYSIS OF OCCURRENCE: | | ANALYSIS OF OCCURRENCE: |
| The 2R1B_channel continuously monitors air from the HVAC intake duct into the Unit 2 Control Room. When the alarm setpoint is reached, the monitor actuates an alarm initiating closure of the duct intake valve to prevent cqntaminated air from entering the Control Room (both Salem Units). By design, channel loss of power actuates its ESF function~ | | The 2R1B_channel continuously monitors air from the HVAC intake duct into the Unit 2 Control Room. When the alarm setpoint is reached, the monitor actuates an alarm initiating closure of the duct intake valve to prevent cqntaminated air from entering the Control Room (both Salem Units). By design, channel loss of power actuates its ESF function~ |
| The .2R1B channel functioned as designed when *it lost power. Since Control Room ventil*ation system* switching. to the accident* mode of operation is an ESF actuation; this event is reportable to the Nuclear Regulatory* Commission in accordance with Code of Federal Regulations lOCFR S0.73(a) (2) (iv). | | The .2R1B channel functioned as designed when *it lost power. Since Control Room ventil*ation system* switching. to the accident* mode of operation is an ESF actuation; this event is reportable to the Nuclear Regulatory* Commission in accordance with Code of Federal Regulations 10CFR S0.73(a) (2) (iv). |
| An assessment, by System Engineering, of the safety consequences of the 2B 230 VAC Vital Bus relays and the 2B 460 VAC Vital Bus relays being switched was conducted. | | An assessment, by System Engineering, of the safety consequences of the 2B 230 VAC Vital Bus relays and the 2B 460 VAC Vital Bus relays being switched was conducted. |
| Under these conditions, 2B 460 VAC Vital Bus time overcurrent protection had a decreased pickup setpoint of 120A (4KV side)'in lieu of its normal 300 amp setpoint. The new setpoint made breaker 2B4D trip sensitive when starting large motors such as the CFCUs in high speed (300 HP) with the. bus already loaded. Although the CFCUs are not required in Mode 5 or 6,. they would still receive a low speed | | Under these conditions, 2B 460 VAC Vital Bus time overcurrent protection had a decreased pickup setpoint of 120A (4KV side)'in lieu of its normal 300 amp setpoint. The new setpoint made breaker 2B4D trip sensitive when starting large motors such as the CFCUs in high speed (300 HP) with the. bus already loaded. Although the CFCUs are not required in Mode 5 or 6,. they would still receive a low speed |
Similar Documents at Salem |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station April 13, 1992 U. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT*NO. 2 LICENSEE.EVENT REPORT 92-004-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a} (2) (iv). This report is* required to be issued within thirty (30) days of event discovery.
]ely yours, C. A. Vondra General Manager ~
Salem Operations MJP:pc Distribution 9204200203 920413 PDR ADOCK 05000311 S PDR
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSl;E EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530). U.S. NUCLEAR
., REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). O.FFICE I
OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) I PAGE (31 Salem Generating Station TITLE (4)
- Unit 2 o 1s 10*10101 31111 1foF 01 5 ESF Signal Actuation:: Contt~ I Room Vent. Switch To Erner. Mode Due To *Personnel Error
- EVENT DATE (51 LER NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (81
~t~t~ ~)?~ NUMBER MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(SI NUMBER 0 I 5 IO I O I O I I I ol 3 ii 5 9 2 912
- ol ol 4
- 0 ~ q4 113 912 6 I5 I0 I 0 I 0 I I I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RcOUIREMENTS OF 10 CFR §: (Chock OM or moro of tho following} (111 MODE (81 5 20.402(bl
'---
20.405(cl . ,_x 60,73(1J(2)(iv)
....;.....
73.71(b)
'POWER LEVEL (10) Io,o ,o ,__.:. 20.4051*111 )(i) 20.405(1)(1 )(ii)
--
'---
50.38(c)(11 50.36(cll2l
- 60.73(1J(2)(v) 50.73(1)(2J(viil
.,.._ 73.711cl OTHER (Specify in Absrract
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'--- 1-- bslow snd in Text, *NRC Form 20.405(0)(1 )(iii) 50.73(1J(2J(i) &0,73(1112l(viiil(AI 366A}
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20.405(1 )(11 (Iv) 60.73(1)(2)(iil 50.73(1J(2J(viiiJ(BI
'---
20.40511l11lM 50,73(1J(2)1iiil 50.73(1)(2llxl LICENSEE CONTACT FOR THIS LEA (121 NAME TELEPHONE NUMBER AREA CODE
-
M. J. Pollack - LER Coordinator 61 019 3 I 3 I 9 1-* I 2 I 0 I? I 2 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
- .*.* t:*:-: :.:.::::: -:-::-:* ::-:::::: :*:*:*:
CAUSE SYSTEM COMPONENT MANUFAC*
TUR ER REPORTABLE It?/:{/:??????.
TO NPRDS 1*:*:*:*:*:*:*:*:::*:*:*:*:*:::*:*:*:*:-:*:*:*:*:*:*:* CAUSE SYSTEM COMPONENT MANUFAC*
TUR ER REPORTABLE -:-::-:- *:*:*:*:* -:*: :-:-:-:-:
TO NPRDS :-:--:-::-:-: -:*: :::::::::
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- :-:-:-:-: :-:-:-:- :-:*:*:
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SUPPLEMENTAL *REPORT EXPECTED (141 MONTH DAY YEAR EXPECTED n YES !If vas. complateEXPECTED SUBMISSION DATE}
ABSTRACT (Limit to 1400 spaces, i.e .. approximately fifteen single-space typewritten lines) 116) hi NO SUBMISSION DATE (151 I I I On 3/15/92, the 2B4D 4KV breaker tripped open on "phase c time overcurrent" upon starting the No. 24 Containment Fan Coil Unit. This de-energized the 2B-460 VAC and the 2B 230 VAC Vital. Busses. With the loss of the 2B 460 VAC Vital Bus~* the 2R1B Radiation Monitoring System (RMS} channel de-en~rgize~ and caused a signal for Control Rqom Ventilation Switch to the Emergency Mode of Operation (both Units} at 2305 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.770525e-4 months <br /> (per design) . This signal is an Engineered Safety Feature.
The root cause of this event is. personnel *error, as attributed to _poor work practice. Relay department personnel did not comply with reasonable self-verification work practices. .On 1/11/92, Relay
- Department personnel removed the 2B 460 VAC and 230 VAC Vital Buss es overcurrent relays in support of r1:>utipe maintenance and calibration.
Upon completion, the relays were placed back in the bus; however, 4 of the six (6) relays were put into the wrong Bus. Corrective disciplinary. action* has. been taken with the l.ndividuals involved. This event bas been reviewed with applicable Relay Department personnel.
The other 460 and 230 VAC Vital Bus relays were inspected. No additional discrepancies were identified. Revision of applicable Relay Department and Maintenance Department procedures has been initiat~d to require verification of relay installation. *This event will be reviewed by the Nuclear Training Center for incorporation into continuing training programs as applicable. The 2R1B RMS channel was returned to service following satisfactory verification of operation.
NRC Form 366 (6-891
LICENSEE EVENT REPORT. (LER) TEXT CONTINUATION Salem Generating Station .DOCKET NUMBE~ LER NUMBER PAGE
. _U_n_i_t_2_ _*-----------------"-5000,-"3~1~1o.__ _ _--=9:-=2=----=0_Q_4_-_Q_0.~-----=2=-- of 5 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurize.d Water Reactor Energy Industry Identification System (EIIS) codes are .identified in the. text as {xxl.
IDENTIFICATION OF OCCURRENCE:
Engineered Safety Feature. signal actuation for Control Room Ventilation switching due to personnel error Discovery Date~* 3/15/92 Report Date: 4/13/92 This_ report was initiated by Incident Report No ..91-186.
CONDITIONS PRIOR TO OCCURRENCE: ---
1/11/92 - Mode* 6, Gt h
- Refueling Outage in Progress 3/15/92 Mode 5 DESCRIPTION OF OCCURRENCE:
On March 15, 1992, at 2242 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.53081e-4 months <br />, 4KV.breaker 2B4D tripped open ori "phase C time* overcurrent".
- This breaker feeds the 2B 460 VAC and the 2B 230 VAC Vital Busses. At the time of the breaker trip, 24 Containment ~an Coil Unit {BK} was being started (in high speed).
-
Witn the loss of the 2B 460 VAC *vital Bus, the No... 22 RM Distribution panel de-energized. The 2R1B Radiation Monitoring System (RMS} {ILi channel is* powered via the No. 22 RM Distribution panel. A new UPS was installed* during the current refueling outage which includes a self* contained battery. DC power supplied to the inverter allowed the 22 RM Distribution Panel to remain energized. Wilen the battery voltage decayed to 105 VDC the inverter automatically shutdown (per design} . Consequently, de-eri.ergization of the 2R1B RMS channel .
caused a signal for Control Room Ventilation Switch to the Emergency
- Mode of Operation (both Units) .at 2305 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.770525e-4 months <br /> (per design). This signal is an Engineered Safety Feature. Therefore, the Nuclear Regulatory Commission. was notified on March 15, 1992, at 0008 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />s-in accordance with Code of Federal Regulations 10CFR 50.72(b)(2) (ii)
APPARENT CAUSE OF OCCURRENCE:
. .
The root.cause of this event is personnel error, as attributed to poor work practice. Relay department personnel did not comply with
~easoriable self-verifi6ation work practices.
On January 11, 1992, Relay Department personnel removed the 2B 460 VAC and 230 VAC Vital Busses phase A and.phase C overcurrent relays in support of routine maintenance and 6alibrati6n. Normally, these relays are removed one at a time and calibrated at the job site.
Salem Generating Station
- LICENSEE EVENT REPORT (LER} TEXT CONTINUATION LER NUMBER PAGE u==ri=i~t'-----"2;:.._~~~~~~~~~~~~~~s~o~o~o=J=l=l=---~~~~=9=2~-004-qp~*~~~J~qf~S~~
APPARENT CAUSE OF OCCURRENCE: (corit'd}
- However, due to significant.work activity in the area, it was decided to remove all' th~ relays and calibrate them at a different location.
The relay serial numbers were recorded as to th~ir bus location.
After completing the calibration, the relays were placed back in the bus. Four (4) of the six (6) relays were put into* the wrong* Bus_ -
(i.e. 230 VAC vs. 460 VAC}. The Relay Department technicians did not verify that each relay was returned to its original location._ The paper work identifying this information* had been left at the calibration location during reinstallation of the relays.
ANALYSIS OF OCCURRENCE:
The 2R1B_channel continuously monitors air from the HVAC intake duct into the Unit 2 Control Room. When the alarm setpoint is reached, the monitor actuates an alarm initiating closure of the duct intake valve to prevent cqntaminated air from entering the Control Room (both Salem Units). By design, channel loss of power actuates its ESF function~
The .2R1B channel functioned as designed when *it lost power. Since Control Room ventil*ation system* switching. to the accident* mode of operation is an ESF actuation; this event is reportable to the Nuclear Regulatory* Commission in accordance with Code of Federal Regulations 10CFR S0.73(a) (2) (iv).
An assessment, by System Engineering, of the safety consequences of the 2B 230 VAC Vital Bus relays and the 2B 460 VAC Vital Bus relays being switched was conducted.
Under these conditions, 2B 460 VAC Vital Bus time overcurrent protection had a decreased pickup setpoint of 120A (4KV side)'in lieu of its normal 300 amp setpoint. The new setpoint made breaker 2B4D trip sensitive when starting large motors such as the CFCUs in high speed (300 HP) with the. bus already loaded. Although the CFCUs are not required in Mode 5 or 6,. they would still receive a low speed
- (100 HP) st~rt signal from the Safeguards Equipment Control (SEC)
Cabinet fJCI load sequencer in the event of a design basis.iccident.
The SEC and SSPS are not required to be operable in Modes 5 and 6; although, they are kept functional.
- The 2B 460 VAC Vital Bus was required to be operable between February 4, 1992 and March 3, 1992 during which time the No. 2A Vi ta:l .Bus electrical trains were removed from service for maintenance. In Modes 5 and 6, only two (2) of the three (3) Vital Bus electrical trains are required per Technical Specification 3.8.2.2. During this period, the 2B 460 VAC Vital Bus loads continuously energized included:
No. 22 Spent Fuel Pump (lOOHP)
No. 22 Auxiliary Building Exhaust Fan (75HP)
No. 22 Auxiliary Building Supply Fan {SOHP)
No. 22 Fuel Handling Are~ Fan (20 HP)
No. 22 RM Distribution Panel (10 KVA)
LICENSEE EVENT REPORT (LER) .TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE u_~n~i_t~2~~~-*~~~~~~~~~--"s~o~o~o~3~1=1~-~~---,~~92-004-00 4 of 5 ANALYSIS OF OCCURRENCE: (cont'd)
The No. 24 CFCU was not started until March-15, 1992 when this event occurred. The oth~r two (2) major loads include the No. 22 Chiller (100 HP) and the.No. 22 CFCU. They were cleared and tagged during this period in support of maintenance activity. Therefore, had a "mode op" condition occurred, only the No. 24 CFCU.would start (in low speed) and would not have. caused the 2B4D breaker to trip.
Th.e 2B 230 VAC Vital Bus overcurrent protection relay was raised from 80 t~ 20.0 amps (4KV side) when the relays* were swapped. The bus would have supplied* power, during an emergency, to its associated
.loads. However, it would have been affected if the 2B 460 VAC Vital Bus had tripped on overcurrent since both transformers are fed from the same 4KV breaker. Therefore, the operation of this bus was also dependent on the 2B 460 VAC Vital Bus operation which was found acceptabl~ as described above.
Based on the above discussion, the health and Safety of the public was not affected by this event since the 2B 460 VAC and 230 VAC Vital Busses remained functional even though the overcurrent protection re rays were switched. *
"As a minimum, two A.C. electrical bus trains shall be OPERABLE and eneigized from sources of power other than a diesel generator but aligned to an OPERABLE diesel generator with each train consisting.of:
1 - 4 kvolt Vital Bus 1 - 460 volt Vital Bus and associated control centers 1 - 230 volt Vital Bus and associated control centers 1 - 115 *volt Instrument Bus energized from its respective inverter connected to its respective D.C. Bus Train."
CORRECTIVE ACTION:
Appropriate corrective disciplinary action has* been taken with the individuals involved in this event.
This event has been reviewed with applicable Relay Department personnel.
The other 460 and 230 VAC Vital Bus relays for the Unit 1 busses and the other Unit 2 busses were inspected and verified as to their required settings. No additional discrepancies were identified.
Revision of applicable ~elay Departmeht and Maintenance Department procedures has been initiated to require verification of relay installation.
This event will be reviewed by the Nuclear Training Center for incorporation into continuing training programs as applicable.
- .Salem Generating Station
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
*------------*
LER NUMBER PAGE
_U_n_i_t_2_ _ _ _ _ _ _ _ _ _ _ _ _ _5000311_____ 92-Q_Q_4-Q_Q~-- 5 of--*-----*
-- -*-*-- 5 CORRECTIVE ACTION: (cont'd)
The 2R1B RMS channel was returned to service following satisfactory verification of* operation.
Gener 1 Manager -
Salem Operations MJP:pc SORC Mtg.91-044