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| | issue date = 09/09/1988 | | | issue date = 09/09/1988 |
| | title = LER 88-002-00:on 880811,unplanned RWCU Isolation Occurred. Caused by Personnel Error.Temp Indicating Switch Recalibr & Sys Returned to svc.W/880909 Ltr | | | title = LER 88-002-00:on 880811,unplanned RWCU Isolation Occurred. Caused by Personnel Error.Temp Indicating Switch Recalibr & Sys Returned to svc.W/880909 Ltr |
| | author name = BAKER R L, CAMPBELL G G | | | author name = Baker R, Campbell G |
| | author affiliation = TENNESSEE VALLEY AUTHORITY | | | author affiliation = TENNESSEE VALLEY AUTHORITY |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:Ac CELERATZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8809150012 DOC.DATE: 88/09/09 NOTARIZED: | | {{#Wiki_filter:Ac CELERATZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| NO FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee AUTH.NAME AUTHOR AFFILIATION BAKER,R.L. | | ACCESSION NBR:8809150012 DOC.DATE: 88/09/09 NOTARIZED: NO DOCKET g FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 AUTH. NAME AUTHOR AFFILIATION BAKER,R.L. Tennessee Valley Authority CAMPBELL,G.G. Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION |
| Tennessee Valley Authority CAMPBELL,G.G. | |
| Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION DOCKET g 05000296 | |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 88-002-00:on 880811,unplanned RWCU isolation due to personnel error.W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73 Licensee Event Report (LER),.Incident Rpt, etc.NOTES:1 Copy each to: S.'Black, J.G.Partlow,S.Richardson B.D.Llaw,.F.McCoy. | | LER 88-002-00:on 880811,unplanned RWCU isolation due to personnel error. |
| 05000296 S RECIPIENT ID CODE/NAME SIMMS,M GEARS,G INTERNAL ACRS MICHELSON ACRS WYLIE AEOD/DSP/NAS AEOD/DSP/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB ll NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES TELFORDiJ RES/DSIR/EIB EXTERNAL: EG&G WILLIAMS, S H ST LOBBY WARD NRC PDR NSIC MAYS,G NOTES COPIES LTTR ENCL 1 1 1-1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 4 4 1 1 1 1 1 1 5 5 RECIPIENT ID CODE/NAME PD ACRS MOELLER AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10~RR~RIS/IB 9A~RE 02 RES/DSIR DEPY RGN2 FILE 01 FORD BLDG HOY g A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1'1 1 1 1 1 1 1 1 1 1 1 D A D TOTAL NUMBER OF COPIES REQUIRED: LTTR 51 ENCL 50
| | W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE: |
| | TITLE: 50.73 Licensee Event Report (LER),. Incident Rpt, etc. |
| | S NOTES:1 Copy each to: S. 'Black, J.G.Partlow,S.Richardson 05000296 B.D.Llaw,.F.McCoy. |
| | RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL SIMMS,M 1 1 PD 1 1 D GEARS,G 1 -1 INTERNAL ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/QAB 10 NRR/DOEA/EAB ll NRR/DLPQ/HFB 10 NRR/DREP/RPB 10 1 |
| | 1 2 |
| | 1 1 |
| | 2 NRR/DREP/RAB 10 |
| | ~RR~RIS/ IB 9A 1 |
| | 1 1 |
| | 1 1 |
| | 1' NUDOCS-ABSTRACT 1 1 ~RE 02 1 RES TELFORDiJ 1 1 RES/DSIR DEPY 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY g A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 NOTES 5 5 A |
| | D TOTAL NUMBER OF COPIES REQUIRED: LTTR 51 ENCL 50 |
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| NRC Form 355 (903/LICENSEE EVENT*REPORT"ILERI'.S. | | NUCLEAR AEOULATORY COMMISSION NRC Form 355 (903/ APPROVED OMB NO. 3150-0104 LICENSEE EVENT*REPORT"ILERI'.S. EXPIRESl 5/31/55 DOCKET NUMBER l2) PA E I FACILITY NAME Il) 0 5 0 0 0 ,1 OF BROWNS FERRY UNIT 3 TITLE (4I UNPLANNED. REACTOR WATER CLEANUP ISOLATION DUE TO PERSONNEL ERROR EVENT DATE(5) LER NUMBER LS) REPORT DATE (7) OTHER FACILITIES INVOLVED (SI |
| NUCLEAR AEOULATORY COMMISSION APPROVED OMB NO.3150-0104 EXPIRESl 5/31/55 FACILITY NAME Il)BROWNS FERRY UNIT 3 DOCKET NUMBER l2)0 5 0 0 0 PA E I ,1 OF TITLE (4I UNPLANNED.
| | 'OAY YEAR, YEAR '/@ SEOVENTIAL NVMSEII @ NVMSER MONTH OAY YEAR 'ONTH FACILITYNAMES DOCKET NUMBER(SI 0 5 0 0 0 08'88OP ERAT)NO 88 '0 0 2 0.0 09 I |
| REACTOR WATER CLEANUP ISOLATION DUE TO PERSONNEL ERROR EVENT DATE(5)LER NUMBER LS)REPORT DATE (7)SEOVENTIAL NVMSEII MONTH@NVMSER OAY YEAR'ONTH'OAY YEAR, YEAR'/@DOCKET NUMBER(SI 0 5 0 0 0 FACILITY NAMES OTHER FACILITIES INVOLVED (SI 08'88 88'0 0 2 0.0 09 I 9 8 8 0 5 0 0 0 OP ERAT)NO MODE (9)~OWER LEYEL0 0 0 20.402(h)20.405(~I(II(l)'0,405 (~I (1)(ll I 20.405(~l(1)(III)20.405(~l(1)(lvl 20.405(~l(1)(~)20.405(c)50.36(c)(II 50.35(cl(2)'0.73(~l(2)(II 50.73(~)(2 IIII)50.73(~)(2)(ill~)X LICENSEE CONTACT FOR THIS LER (12), 50 73(~l(2)(lvl'0.73(~l(2l(vl 60.73(cl(2l(vill 50.73(~)(2)(vill)(A) 60.73(~l(2)(vill)(5)50.73(~)(2)(x)0 THE REQUIREMENTS OF 10 CFR (): IChech one or more OI the Iollowinp/(ll THIS REPORT IS SUBMITTED PUASVANT T: 73.7)(h)73.71(c)OTHER/Soec/ly In Ahttrett Oelow end/n Text.IYRC Form 366AI NAME Richard'.Baker, En ineer, Plant 0 erations Review Staff TELEPHONE NUMBER AREA CODE 20 72 9-2 538 COMPLE'TE ONE LINE FOA EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)'CAUSE, SYSTEM COMPONENT TVRER SYSTEM COMPONENT MANVFAC.TVRER EPORTABLE TO NPAOS cl@+ei%SUPPLEMENTAL'EPORT EXPECTED (14)EXPECTED SUBMISSION DATE I'ISI MONTH OAY YEAR YES (l/,yet.complete EI(PECTEO SUBMISSION DATE/NO ASSTRACT/Limit to/400 toecet.I e., eoorox/merely | | 9 8 8 THIS REPORT IS SUBMITTED PUASVANT T 0 THE REQUIREMENTS OF 10 CFR (): IChech one or more OI the Iollowinp/ (ll 0 5 0 0 0 MODE (9) 20.402(h) 20.405(c) X 50 73( ~ l(2)(lvl : 73.7)(h) |
| /i/teen t/nple toece tyoewri Iten I/ntn/(15)On August ll, 1988, at 0800 hours, with all, three Browns Ferry units defueled, the temperature indicating switch (TIS)monitoring.the discharge of the'unit 3 reactor water cleanup (RWCU)nonregenerative heat exchanger initiated an isolation of the RWCU system.Th'is isolation function is an engineered'afety feature (ESF)of the primary containment isolation system.At the time of this.event plant personnel were decontaminating the panel which houses the TIS.During an.investigation of the cause of the event'he instrument mechanics discovered that the setpoint knob, located on the front of the TIS', was turned'rom the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit.
| | (ill |
| This change in the setpoint has been.attributed to inadvertent personnel.
| | '0.73( ~ l(2l(vl(vill) |
| error during the decontami.nation process.The TIS was recalibrated to the original setpoint and the RWCU system was returned to service at 1430 hours.This i.'s considered an isolated event since no other events of a similar nature have been recorded.All decontamination crews have been reminded to use caution when decontaminating any plant panels due to possibl'e ESF actuati;ons.
| | (vill)(A) 73.71(c) |
| Pc 09/500%'2'00029/I 880909 pDR ADOCK 0 8 NRC Form 355 (9 83)
| | ~ OWER 20.405( ~ I(II(l) 50.36(c)(II LEYEL0 0 0 '0,405 ( ~ I (1)(llI 50.35(cl(2)'0.73( |
| <0 II Vt 0 NRC Form 3ddA)043)LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U S, NUCLEAR REOULATORY COMMISSION APPROVED OMS NO.3ISOW104 EXPIRES: 8/31/88 FACILITY NAME IIl DOCKET NUMBER (2)LER NUMBER Idl YEAR r'iM SEQVENT/AL
| | 60.73(cl(2l(vill OTHER /Soec/ly In Ahttrett Oelow end /n Text. IYRC Form 20.405( ~ l(1) (III) ~ l(2) (II 50.73( ~ ) (2) 366AI 20.405( ~ l(1) (lvl 50.73( ~ ) (2 IIII) 60.73( ~ l(2) (5) 20.405( ~ l(1)(~ ) 50.73( ~ ) (2) ) 50.73( ~ )(2)(x) |
| ~%I rrdVISION NVMddrI~.or rrVM d/I PACE I3)BROMNS FERRY UNIT 3 TEXT///moro Nrooo*/o)/rkorL rr>>//POooo////IC Forrrr 3/)I/A3/IIT)Descri tion of Event o s o o o 2 9 6 88-002-0 002 oFO 3 On August 11, 1988, at 0800 hours, with all three Browns Ferry units defueled, the unit 3 reactor water cleanup (RMCU)system (EIIS code CE)isolated.This isolation function is an engineered safety feature (ESF)of the primary containment isolation system (EIIS code JM).The RWCU isolation was caused by a reduced trip setpoint on temperature indicating switch (TIS)(EIIS code TIS)69-11.This TIS is designed to isolate the RWCU system on high temperature of the water downstream of the nonregenerative heat exchanger.
| | LICENSEE CONTACT FOR THIS LER (12), |
| Flow control valves (FCV)69-1 and 69-12 closed and B RWCU pump tripped as designed.FCV 69-2 would have normally closed as designed, but it remained open because its power was removed under a hold order.At the time of this event, plant personnel were decontaminating the panel which houses TIS-69-11.
| | NAME TELEPHONE NUMBER AREA CODE Richard'. Baker, En ineer, Plant 0 erations Review Staff 20 72 9-2 538 COMPLE'TE ONE LINE FOA EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| The instrument mechanics checked TIS-69-11 and found the setpoint knob, located on the front of the TZS, was turned from the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit.
| | MANVFAC. EPORTABLE |
| The instrument was.recalibrated to the original setpoint and the RMCU system was returned to service at 1430 hours.Cause of Event The isolation of the RWCU system was caused by the inadvertent personnel error of accidently turning the TIS setpoint knob during the decontamination process.No member of the decontamination crew was aware that the setpoint on TIS-69-11 had been changed.However, because'of the physical location of the setpoint control knob, the setpoint could, have accidently been changed by contact with a rag, brush, etc.without the individual realizing it.Anal sis of Event The RWCU system is designed to provide continuous mechanical filtration and chemical demineralization of reactor water.This system is also designed to isolate upon a.high temperature indication-at the discharge of the RWCU nonregenerative heat exchanger.
| | 'CAUSE, SYSTEM COMPONENT SYSTEM COMPONENT TVRER TO NPAOS TVRER cl@+ei% |
| This system functioned exactly as designed.The isolation-of the RWCU system due to high water temperature downstream of the nonregenerative heat exchanger is a non-safety function to reduce reactor water temperature to acceptable levels for the resin material used in the filter demineralizers.
| | SUPPLEMENTAL'EPORT EXPECTED (14) MONTH OAY YEAR EXPECTED SUBMISSION DATE I'ISI YES (l/,yet. complete EI(PECTEO SUBMISSION DATE/ NO ASSTRACT /Limit to /400 toecet. I e., eoorox/merely /i/teen t/nple toece tyoewri Iten I/ntn/ (15) |
| The temporary loss of RWCU had a negligible effect on reactor water.chemistry.
| | On August ll, 1988, at 0800 hours, with all, three Browns Ferry units defueled, the temperature indicating switch (TIS) monitoring .the discharge of the 'unit 3 reactor water cleanup (RWCU) nonregenerative heat exchanger initiated an isolation of the RWCU system. Th'is isolation function is an engineered'afety feature (ESF) of the primary containment isolation system. At the time of this. event plant personnel were decontaminating the panel which houses the TIS. During an. investigation of the cause of the event'he instrument mechanics discovered that the setpoint knob, located on the front of the TIS', was turned'rom the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit. This change in the setpoint has been .attributed to inadvertent personnel. error during the decontami.nation process. The TIS was recalibrated to the original setpoint and the RWCU system was returned to service at 1430 hours. This i.'s considered an isolated event since no other events of a similar nature have been recorded. All decontamination crews have been reminded to use caution when decontaminating any plant panels due to possibl'e ESF actuati;ons. |
| The associated technical specification requirements for monitoring water chemistry parameters and the implementing procedures provide early detection for any chemistry problems that could result from the loss of RWCU.If this event had occurred during.power operation, there would have been no effect on plant safety.As stated above, water chemistry monitoring would provide required protection to equipment from any chemical parameter approaching, a technical specification limit.NIIC FORM Sddk (043)o U.S OPO'.1088 OP82l 538/l SS i?
| | Pc 09/500%'2 '00029/I 880909 pDR ADOCK 0 8 |
| NRC Form 3ddA (983)LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPROVFD OMS NO.3150M)04 EXPIRES: 8/31/88 FACILITY NAME (11'ROWNS FERRY UNIT 3 TEXT//I mOre eeeee le deq/reer/rree eederden/I HRC FOnrr 3///IA'e/(17)Corrective Action DOCKET.NUM8ER (3)0 5 0 0 0'2 9 LER NUMBER (8)YEAR'4, SEQVENTr*L
| | NRC Form 355 (9 83) |
| @(4dyrSK)N iX'r NVMSE4 i NVM e4 88-0 02-00 PAGE IS)03"03 During an investigation of the cause of the event the instrument mechanics discovered that the setpoint knob, located on the f'ront of the'TIS, was turned from the original calibrated setpoint of 140:degrees fahrenheit to 52 degrees fahrenheit.
| | |
| The TIS was reset and, cal'ibrated to the original setpoint of 140 degrees fahrenheit and the RMCV system was returned to service at 1430 hours.This is considered.an isolated event since,no other events.of a similar nature have been recorded.All decontamination crews have been reminded to use caution when decontaminating any plant panels.due to,possible ESF actuations.
| | <0 II Vt |
| 'No further corrective action is planned.Previous Simil'ar Events-None Commitments | | |
| -None NRC FORM Sddo (9831 4 U.S GPO.198~82 d.538/4 55 iI ik a/
| | 0 NRC Form 3ddA U S, NUCLEAR REOULATORY COMMISSION |
| TENNESSEE'VALLEY AUTHORITY Browns Ferry,.Nuc1ear'Plant Post Office Box 2000 Decatur, Alabama 35602 U.S.Nuclear Regulatory Commission Document Control Desk Washington, D.C.20555 Dear Sirt'TENNESSEE VALLEY AUTHORITY-BROWNS FERRY NUCLEAR.PLANT UNIT 3-DOCKET NO.50-296-FACILITY OPERATING LICENSE DPR-68-REPORTABLE OCCURRENCE REPORT BFRO-50-296/88002 The enclosed'eport provides details concerning the unplanned reactor water cleanup isolation due to personnel error.This report is submitted in accordance with 10 CFR 50.73 (a)(2),(iv). | | )043) |
| Very truly yours, TENNESSEE VALLEY AUTHORITY k jn-~Guy G.Campbell Plant Manager Browns Ferry Nuclear'Plant Enclosures cc (Enclosures): | | LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMS NO. 3ISOW104 EXPIRES: 8/31/88 FACILITY NAME IIl DOCKET NUMBER (2) LER NUMBER Idl PACE I3) |
| Regional Administration U.S.Nuclear:Regulatory Commission Office of Inspection-and Enforcement Region II 101 Marietta Street, Suite 2900'Atlanta, Georgia 30303 INPO Records Center Suite 1500 1100'ircle 75'Parkway'Atlanta, Georgia 30339 NRC Resident Inspec'tor, Browns Ferry Nuclear Plant~@g yP An'Equal Opportunity Employer t I}} | | YEAR r'iM SEQVENT/AL ~%I rrdVISION NVMddrI ~ .or rrVM d/I BROMNS FERRY UNIT 3 o s o o o 2 9 6 88 002 0 002 oFO 3 TEXT ///moro Nrooo */o)/rkorL rr>> //POooo////IC Forrrr 3/)I/A3/ IIT) |
| | Descri tion of Event On August 11, 1988, at 0800 hours, with all three Browns Ferry units defueled, the unit 3 reactor water cleanup (RMCU) system (EIIS code CE) isolated. This isolation function is an engineered safety feature (ESF) of the primary containment isolation system (EIIS code JM). The RWCU isolation was caused by a reduced trip setpoint on temperature indicating switch (TIS) (EIIS code TIS) 69-11. This TIS is designed to isolate the RWCU system on high temperature of the water downstream of the nonregenerative heat exchanger. Flow control valves (FCV) 69-1 and 69-12 closed and B RWCU pump tripped as designed. FCV 69-2 would have normally closed as designed, but it remained open because its power was removed under a hold order. At the time of this event, plant personnel were decontaminating the panel which houses TIS-69-11. The instrument mechanics checked TIS-69-11 and found the setpoint knob, located on the front of the TZS, was turned from the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit. The instrument was. recalibrated to the original setpoint and the RMCU system was returned to service at 1430 hours. |
| | Cause of Event The isolation of the RWCU system was caused by the inadvertent personnel error of accidently turning the TIS setpoint knob during the decontamination process. No member of the decontamination crew was aware that the setpoint on TIS-69-11 had been changed. However, because 'of the physical location of the setpoint control knob, the setpoint could, have accidently been changed by contact with a rag, brush, etc. without the individual realizing it. |
| | Anal sis of Event The RWCU system is designed to provide continuous mechanical filtration and chemical demineralization of reactor water. This system is also designed to isolate upon a .high temperature indication- at the discharge of the RWCU nonregenerative heat exchanger. This system functioned exactly as designed. The isolation- of the RWCU system due to high water temperature downstream of the nonregenerative heat exchanger is a non-safety function to reduce reactor water temperature to acceptable levels for the resin material used in the filter demineralizers. The temporary loss of RWCU had a negligible effect on reactor water .chemistry. The associated technical specification requirements for monitoring water chemistry parameters and the implementing procedures provide early detection for any chemistry problems that could result from the loss of RWCU. If this event had occurred during .power operation, there would have been no effect on plant safety. As stated above, water chemistry monitoring would provide required protection to equipment from any chemical parameter approaching, a technical specification limit. |
| | NIIC FORM Sddk o U.S OPO'.1088 OP82l 538/l SS (043) |
| | |
| | i? |
| | NRC Form 3ddA U.S. NUCLEAR REGULATORY COMMISSION (983) |
| | LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVFD OMS NO. 3150M)04 EXPIRES: 8/31/88 FACILITYNAME DOCKET. NUM8ER (3) LER NUMBER (8) PAGE IS) |
| | YEAR '4, iX'r SEQVENTr*L @(i 4dyrSK)N NVM e4 NVMSE4 "03 (11'ROWNS FERRY UNIT 3 0 5 0 0 0 '2 9 88 0 02 00 03 TEXT //I mOre eeeee le deq/reer/ rree eederden/I HRC FOnrr 3///IA'e/ (17) |
| | Corrective Action During an investigation of the cause of the event the instrument mechanics discovered that the setpoint knob, located on the f'ront of the 'TIS, was turned from the original calibrated setpoint of 140:degrees fahrenheit to 52 degrees fahrenheit. The TIS was reset and, cal'ibrated to the original setpoint of 140 degrees fahrenheit and the RMCV system was returned to service at 1430 hours. |
| | This is considered .an isolated event since,no other events .of a similar nature have been recorded. |
| | All decontamination crews have been reminded to use caution when decontaminating any plant panels. due to,possible ESF actuations. 'No further corrective action is planned. |
| | Previous Simil'ar Events None Commitments None NRC FORM Sddo 4 U.S GPO.198~82 d.538/4 55 (9831 |
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| | iI ik a/ |
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| | TENNESSEE 'VALLEY AUTHORITY Browns Ferry,.Nuc1ear'Plant Post Office Box 2000 Decatur, Alabama 35602 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Dear Sirt |
| | 'TENNESSEE VALLEY AUTHORITY BROWNS FERRY NUCLEAR. PLANT UNIT 3 DOCKET NO. 50-296 FACILITY OPERATING LICENSE DPR-68 REPORTABLE OCCURRENCE REPORT BFRO-50-296/88002 The enclosed'eport provides details concerning the unplanned reactor water cleanup isolation due to personnel error. This report is submitted in accordance with 10 CFR 50.73 (a)(2),(iv). |
| | Very truly yours, TENNESSEE VALLEY AUTHORITY k jn-~ |
| | Guy G. Campbell Plant Manager Browns Ferry Nuclear 'Plant Enclosures cc (Enclosures): |
| | Regional Administration INPO Records Center U.S. Nuclear:Regulatory Commission Suite 1500 Office of Inspection -and Enforcement 1100'ircle 75 'Parkway Region II 'Atlanta, Georgia 30339 101 Marietta Street, Suite 2900 |
| | 'Atlanta, Georgia 30303 NRC Resident Inspec'tor, Browns Ferry Nuclear Plant |
| | ~@gyP An'Equal Opportunity Employer |
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| | t I}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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Ac CELERATZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8809150012 DOC.DATE: 88/09/09 NOTARIZED: NO DOCKET g FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 AUTH. NAME AUTHOR AFFILIATION BAKER,R.L. Tennessee Valley Authority CAMPBELL,G.G. Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-002-00:on 880811,unplanned RWCU isolation due to personnel error.
W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73 Licensee Event Report (LER),. Incident Rpt, etc.
S NOTES:1 Copy each to: S. 'Black, J.G.Partlow,S.Richardson 05000296 B.D.Llaw,.F.McCoy.
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL SIMMS,M 1 1 PD 1 1 D GEARS,G 1 -1 INTERNAL ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/QAB 10 NRR/DOEA/EAB ll NRR/DLPQ/HFB 10 NRR/DREP/RPB 10 1
1 2
1 1
2 NRR/DREP/RAB 10
~RR~RIS/ IB 9A 1
1 1
1 1
1' NUDOCS-ABSTRACT 1 1 ~RE 02 1 RES TELFORDiJ 1 1 RES/DSIR DEPY 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY g A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 NOTES 5 5 A
D TOTAL NUMBER OF COPIES REQUIRED: LTTR 51 ENCL 50
NUCLEAR AEOULATORY COMMISSION NRC Form 355 (903/ APPROVED OMB NO. 3150-0104 LICENSEE EVENT*REPORT"ILERI'.S. EXPIRESl 5/31/55 DOCKET NUMBER l2) PA E I FACILITY NAME Il) 0 5 0 0 0 ,1 OF BROWNS FERRY UNIT 3 TITLE (4I UNPLANNED. REACTOR WATER CLEANUP ISOLATION DUE TO PERSONNEL ERROR EVENT DATE(5) LER NUMBER LS) REPORT DATE (7) OTHER FACILITIES INVOLVED (SI
'OAY YEAR, YEAR '/@ SEOVENTIAL NVMSEII @ NVMSER MONTH OAY YEAR 'ONTH FACILITYNAMES DOCKET NUMBER(SI 0 5 0 0 0 08'88OP ERAT)NO 88 '0 0 2 0.0 09 I
9 8 8 THIS REPORT IS SUBMITTED PUASVANT T 0 THE REQUIREMENTS OF 10 CFR (): IChech one or more OI the Iollowinp/ (ll 0 5 0 0 0 MODE (9) 20.402(h) 20.405(c) X 50 73( ~ l(2)(lvl : 73.7)(h)
(ill
'0.73( ~ l(2l(vl(vill)
(vill)(A) 73.71(c)
~ OWER 20.405( ~ I(II(l) 50.36(c)(II LEYEL0 0 0 '0,405 ( ~ I (1)(llI 50.35(cl(2)'0.73(
60.73(cl(2l(vill OTHER /Soec/ly In Ahttrett Oelow end /n Text. IYRC Form 20.405( ~ l(1) (III) ~ l(2) (II 50.73( ~ ) (2) 366AI 20.405( ~ l(1) (lvl 50.73( ~ ) (2 IIII) 60.73( ~ l(2) (5) 20.405( ~ l(1)(~ ) 50.73( ~ ) (2) ) 50.73( ~ )(2)(x)
LICENSEE CONTACT FOR THIS LER (12),
NAME TELEPHONE NUMBER AREA CODE Richard'. Baker, En ineer, Plant 0 erations Review Staff 20 72 9-2 538 COMPLE'TE ONE LINE FOA EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
MANVFAC. EPORTABLE
'CAUSE, SYSTEM COMPONENT SYSTEM COMPONENT TVRER TO NPAOS TVRER cl@+ei%
SUPPLEMENTAL'EPORT EXPECTED (14) MONTH OAY YEAR EXPECTED SUBMISSION DATE I'ISI YES (l/,yet. complete EI(PECTEO SUBMISSION DATE/ NO ASSTRACT /Limit to /400 toecet. I e., eoorox/merely /i/teen t/nple toece tyoewri Iten I/ntn/ (15)
On August ll, 1988, at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />, with all, three Browns Ferry units defueled, the temperature indicating switch (TIS) monitoring .the discharge of the 'unit 3 reactor water cleanup (RWCU) nonregenerative heat exchanger initiated an isolation of the RWCU system. Th'is isolation function is an engineered'afety feature (ESF) of the primary containment isolation system. At the time of this. event plant personnel were decontaminating the panel which houses the TIS. During an. investigation of the cause of the event'he instrument mechanics discovered that the setpoint knob, located on the front of the TIS', was turned'rom the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit. This change in the setpoint has been .attributed to inadvertent personnel. error during the decontami.nation process. The TIS was recalibrated to the original setpoint and the RWCU system was returned to service at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />. This i.'s considered an isolated event since no other events of a similar nature have been recorded. All decontamination crews have been reminded to use caution when decontaminating any plant panels due to possibl'e ESF actuati;ons.
Pc 09/500%'2 '00029/I 880909 pDR ADOCK 0 8
NRC Form 355 (9 83)
<0 II Vt
0 NRC Form 3ddA U S, NUCLEAR REOULATORY COMMISSION
)043)
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMS NO. 3ISOW104 EXPIRES: 8/31/88 FACILITY NAME IIl DOCKET NUMBER (2) LER NUMBER Idl PACE I3)
YEAR r'iM SEQVENT/AL ~%I rrdVISION NVMddrI ~ .or rrVM d/I BROMNS FERRY UNIT 3 o s o o o 2 9 6 88 002 0 002 oFO 3 TEXT ///moro Nrooo */o)/rkorL rr>> //POooo////IC Forrrr 3/)I/A3/ IIT)
Descri tion of Event On August 11, 1988, at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />, with all three Browns Ferry units defueled, the unit 3 reactor water cleanup (RMCU) system (EIIS code CE) isolated. This isolation function is an engineered safety feature (ESF) of the primary containment isolation system (EIIS code JM). The RWCU isolation was caused by a reduced trip setpoint on temperature indicating switch (TIS) (EIIS code TIS) 69-11. This TIS is designed to isolate the RWCU system on high temperature of the water downstream of the nonregenerative heat exchanger. Flow control valves (FCV) 69-1 and 69-12 closed and B RWCU pump tripped as designed. FCV 69-2 would have normally closed as designed, but it remained open because its power was removed under a hold order. At the time of this event, plant personnel were decontaminating the panel which houses TIS-69-11. The instrument mechanics checked TIS-69-11 and found the setpoint knob, located on the front of the TZS, was turned from the original calibrated setpoint of 140 degrees fahrenheit to 52 degrees fahrenheit. The instrument was. recalibrated to the original setpoint and the RMCU system was returned to service at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />.
Cause of Event The isolation of the RWCU system was caused by the inadvertent personnel error of accidently turning the TIS setpoint knob during the decontamination process. No member of the decontamination crew was aware that the setpoint on TIS-69-11 had been changed. However, because 'of the physical location of the setpoint control knob, the setpoint could, have accidently been changed by contact with a rag, brush, etc. without the individual realizing it.
Anal sis of Event The RWCU system is designed to provide continuous mechanical filtration and chemical demineralization of reactor water. This system is also designed to isolate upon a .high temperature indication- at the discharge of the RWCU nonregenerative heat exchanger. This system functioned exactly as designed. The isolation- of the RWCU system due to high water temperature downstream of the nonregenerative heat exchanger is a non-safety function to reduce reactor water temperature to acceptable levels for the resin material used in the filter demineralizers. The temporary loss of RWCU had a negligible effect on reactor water .chemistry. The associated technical specification requirements for monitoring water chemistry parameters and the implementing procedures provide early detection for any chemistry problems that could result from the loss of RWCU. If this event had occurred during .power operation, there would have been no effect on plant safety. As stated above, water chemistry monitoring would provide required protection to equipment from any chemical parameter approaching, a technical specification limit.
NIIC FORM Sddk o U.S OPO'.1088 OP82l 538/l SS (043)
i?
NRC Form 3ddA U.S. NUCLEAR REGULATORY COMMISSION (983)
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVFD OMS NO. 3150M)04 EXPIRES: 8/31/88 FACILITYNAME DOCKET. NUM8ER (3) LER NUMBER (8) PAGE IS)
YEAR '4, iX'r SEQVENTr*L @(i 4dyrSK)N NVM e4 NVMSE4 "03 (11'ROWNS FERRY UNIT 3 0 5 0 0 0 '2 9 88 0 02 00 03 TEXT //I mOre eeeee le deq/reer/ rree eederden/I HRC FOnrr 3///IA'e/ (17)
Corrective Action During an investigation of the cause of the event the instrument mechanics discovered that the setpoint knob, located on the f'ront of the 'TIS, was turned from the original calibrated setpoint of 140:degrees fahrenheit to 52 degrees fahrenheit. The TIS was reset and, cal'ibrated to the original setpoint of 140 degrees fahrenheit and the RMCV system was returned to service at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />.
This is considered .an isolated event since,no other events .of a similar nature have been recorded.
All decontamination crews have been reminded to use caution when decontaminating any plant panels. due to,possible ESF actuations. 'No further corrective action is planned.
Previous Simil'ar Events None Commitments None NRC FORM Sddo 4 U.S GPO.198~82 d.538/4 55 (9831
iI ik a/
TENNESSEE 'VALLEY AUTHORITY Browns Ferry,.Nuc1ear'Plant Post Office Box 2000 Decatur, Alabama 35602 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Dear Sirt
'TENNESSEE VALLEY AUTHORITY BROWNS FERRY NUCLEAR. PLANT UNIT 3 DOCKET NO. 50-296 FACILITY OPERATING LICENSE DPR-68 REPORTABLE OCCURRENCE REPORT BFRO-50-296/88002 The enclosed'eport provides details concerning the unplanned reactor water cleanup isolation due to personnel error. This report is submitted in accordance with 10 CFR 50.73 (a)(2),(iv).
Very truly yours, TENNESSEE VALLEY AUTHORITY k jn-~
Guy G. Campbell Plant Manager Browns Ferry Nuclear 'Plant Enclosures cc (Enclosures):
Regional Administration INPO Records Center U.S. Nuclear:Regulatory Commission Suite 1500 Office of Inspection -and Enforcement 1100'ircle 75 'Parkway Region II 'Atlanta, Georgia 30339 101 Marietta Street, Suite 2900
'Atlanta, Georgia 30303 NRC Resident Inspec'tor, Browns Ferry Nuclear Plant
~@gyP An'Equal Opportunity Employer
t I