ML18101A806: Difference between revisions

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| issue date = 07/03/1995
| issue date = 07/03/1995
| title = Special Rept:On 950607,identified That 950601 Failure of EDG 1B Potential Common Mode Failure.Util Unable to Determine Cause at Present Time.Ler Will Be Submitted to NRC
| title = Special Rept:On 950607,identified That 950601 Failure of EDG 1B Potential Common Mode Failure.Util Unable to Determine Cause at Present Time.Ler Will Be Submitted to NRC
| author name = SUMMERS J C
| author name = Summers J
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:e J*
{{#Wiki_filter:e CJ* PS~G *
* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit July 3, 1995 LR-N95101 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
    ~*
SPECIAL REPORT EMERGENCY DIESEL GENERATORS SALEM GENERATING STATION UNIT NQ. 1 DOCKET NO. 50-272 Salem Generating Station Technical Specification  
Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit July 3, 1995 LR-N95101 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
: 4. 8 .1.1. 4 requires that all diesel generator failures, valid or non-valid, be reported to the Commission in a Special Report pursuant to Specification  
SPECIAL REPORT EMERGENCY DIESEL GENERATORS SALEM GENERATING STATION UNIT NQ. 1 DOCKET NO. 50-272 Salem Generating Station Technical Specification 4. 8 .1.1. 4 requires that all diesel generator failures, valid or non-valid, be reported to the Commission in a Special Report pursuant to Specification 6.9.2 within 30 days. On June 1, 1995, Salem Unit No. 1 experienced a valid failure of the lB diesel generator. On June 2, 1995 the diesel generator was repaired and returned to service. On June 7, 1995, Public Service Electric and Gas Company (PSE&G) identified that the failure of lB diesel generator was a potential common mode failure and reportable in accordance with 10CFR50.73.
The Special Report for a diesel failure (Technical Specification 4.8.1.1.4) will not be submitted within the required 30 days; PSE&G's decision *to combine the Special Report with the Licensee Event Report (LER) shorted the time required to complete the LER.
Because the root cause of the failure was more complex than expected, PSE&G was unable to complete the LER in the time frame required by the Special Report.                    The LER will be submitted within the 30 day (July 7, 1995) requirements of 10CFR50.73.
9507110166 950703 PDR ADOCK 05000272 S                          PDR The power is in your hand~.
95-2168 REV. 6/94


====6.9.2 within====
DOCUME~T CONTROL DESK           2                 July 3, 1995 LR-N95101 Should there be any questions with regard to this submittal, please do not hesitate to contact us.
30 days. On June 1, 1995, Salem Unit No. 1 experienced a valid failure of the lB diesel generator.
Sincere~,
On June 2, 1995 the diesel generator was repaired and returned to service. On June 7, 1995, Public Service Electric and Gas Company (PSE&G) identified that the failure of lB diesel generator was a potential common mode failure and reportable in accordance with 10CFR50.73.
J*f~~
The Special Report for a diesel failure (Technical Specification 4.8.1.1.4) will not be submitted within the required 30 days; PSE&G's decision *to combine the Special Report with the Licensee Event Report (LER) shorted the time required to complete the LER. Because the root cause of the failure was more complex than expected, PSE&G was unable to complete the LER in the time frame required by the Special Report. The LER will be submitted within the 30 day (July 7, 1995) requirements of 10CFR50.73.
General Manager -
9507110166 950703 PDR ADOCK 05000272 S PDR The power is in your 95-2168 REV. 6/94  
Salem Operations C   Mr. T. T. Martin, Administrator - Region I U. s. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. L. N. Olshan, Licensing Project Manager - Salem U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 14E21 Rockville, MD 20852 Mr. c. Marschall - Salem (S09)
 
USNRC Senior Resident Inspector Mr. K. Tosch, Manager, IV NJ Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625}}
CONTROL DESK LR-N95101 2 July 3, 1995 Should there be any questions with regard to this submittal, please do not hesitate to contact us.
General Manager -Salem Operations C Mr. T. T. Martin, Administrator  
-Region I U. s. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. L. N. Olshan, Licensing Project Manager -Salem U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 14E21 Rockville, MD 20852 Mr. c. Marschall  
-Salem (S09) USNRC Senior Resident Inspector Mr. K. Tosch, Manager, IV NJ Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625}}

Latest revision as of 09:11, 21 October 2019

Special Rept:On 950607,identified That 950601 Failure of EDG 1B Potential Common Mode Failure.Util Unable to Determine Cause at Present Time.Ler Will Be Submitted to NRC
ML18101A806
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/03/1995
From: Summers J
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LR-N95101, NUDOCS 9507110166
Download: ML18101A806 (2)


Text

e CJ* PS~G *

~*

Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit July 3, 1995 LR-N95101 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

SPECIAL REPORT EMERGENCY DIESEL GENERATORS SALEM GENERATING STATION UNIT NQ. 1 DOCKET NO. 50-272 Salem Generating Station Technical Specification 4. 8 .1.1. 4 requires that all diesel generator failures, valid or non-valid, be reported to the Commission in a Special Report pursuant to Specification 6.9.2 within 30 days. On June 1, 1995, Salem Unit No. 1 experienced a valid failure of the lB diesel generator. On June 2, 1995 the diesel generator was repaired and returned to service. On June 7, 1995, Public Service Electric and Gas Company (PSE&G) identified that the failure of lB diesel generator was a potential common mode failure and reportable in accordance with 10CFR50.73.

The Special Report for a diesel failure (Technical Specification 4.8.1.1.4) will not be submitted within the required 30 days; PSE&G's decision *to combine the Special Report with the Licensee Event Report (LER) shorted the time required to complete the LER.

Because the root cause of the failure was more complex than expected, PSE&G was unable to complete the LER in the time frame required by the Special Report. The LER will be submitted within the 30 day (July 7, 1995) requirements of 10CFR50.73.

9507110166 950703 PDR ADOCK 05000272 S PDR The power is in your hand~.

95-2168 REV. 6/94

DOCUME~T CONTROL DESK 2 July 3, 1995 LR-N95101 Should there be any questions with regard to this submittal, please do not hesitate to contact us.

Sincere~,

J*f~~

General Manager -

Salem Operations C Mr. T. T. Martin, Administrator - Region I U. s. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. L. N. Olshan, Licensing Project Manager - Salem U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 14E21 Rockville, MD 20852 Mr. c. Marschall - Salem (S09)

USNRC Senior Resident Inspector Mr. K. Tosch, Manager, IV NJ Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625