ML18102A281: Difference between revisions

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{{#Wiki_filter:e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit JUL 2 9 1996 LR-N96215 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
{{#Wiki_filter:e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit JUL 2 9 1996 LR-N96215 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
LER 311/96-002-00 SALEM GENERATING STATION -UNIT 2 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report entitled "Waste Gas Decay Tank Oxygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (i) (B). Attachment SORC Mtg. 96-101 DVH/tcp C Distribution LER File 3.7 David F. Garchow General Manager -Salem Operations 9608050186 960729 PDR ADOCK 05000311 S PDR --,---,-/ ,. . / J-t __ ..,,, d I 1 95-2168 REV. 6/94 Document Control Desk LR-N96215 JUL 2 9 1996 Attachment A The following item represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-00).
LER 311/96-002-00 SALEM GENERATING STATION - UNIT 2 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report entitled "Waste Gas Decay Tank Oxygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (i) (B).
The commitments are as follows: 1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2. 2. Oxygen concentration levels expeditiously in accordance currently being developed.
                                                &F~
oxygen levels are restored.
David F. Garchow General Manager -
will be restored at Unit 1 with the maintenance schedule This LER will be supplemented when 3. The problems with this Technical Specification have been communicated to the operating crews. Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building.
Salem Operations Attachment SORC Mtg. 96-101 DVH/tcp C       Distribution LER File 3.7 9608050186 960729                                                                           --,--- ,- /   ,.   . /
PDR ADOCK 05000311                                                                          J- t __ ..,,, d I     1 S                        PDR 95-2168 REV. 6/94
 
Document Control Desk LR-N96215                                             JUL 2 9 1996 Attachment A The following item represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-00). The commitments are as follows:
: 1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2.
: 2. Oxygen concentration levels will be restored at Unit 1 expeditiously in accordance with the maintenance schedule currently being developed. This LER will be supplemented when oxygen levels are restored.
: 3. The problems with this Technical Specification have been communicated to the operating crews. Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building.
If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR. If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.
If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR. If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.
: 4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.
: 4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.
: 5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems will be submitted by August 15, 1996.}}
: 5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems will be submitted by August 15, 1996.}}

Latest revision as of 09:41, 21 October 2019

Lists Commitments Relative to LER 311/96-002-00.LER Encl
ML18102A281
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/29/1996
From: Garchow D
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A282 List:
References
LR-N96215, NUDOCS 9608050186
Download: ML18102A281 (2)


Text

e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge. New Jersey 08038-0236 Nuclear Business Unit JUL 2 9 1996 LR-N96215 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

LER 311/96-002-00 SALEM GENERATING STATION - UNIT 2 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report entitled "Waste Gas Decay Tank Oxygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (i) (B).

&F~

David F. Garchow General Manager -

Salem Operations Attachment SORC Mtg.96-101 DVH/tcp C Distribution LER File 3.7 9608050186 960729 --,--- ,- / ,. . /

PDR ADOCK 05000311 J- t __ ..,,, d I 1 S PDR 95-2168 REV. 6/94

Document Control Desk LR-N96215 JUL 2 9 1996 Attachment A The following item represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-00). The commitments are as follows:

1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2.
2. Oxygen concentration levels will be restored at Unit 1 expeditiously in accordance with the maintenance schedule currently being developed. This LER will be supplemented when oxygen levels are restored.
3. The problems with this Technical Specification have been communicated to the operating crews. Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building.

If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR. If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.

4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.
5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems will be submitted by August 15, 1996.