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{{#Wiki_filter:NRC FooM 195~U.S.NUCLEAfl BEGULATofIV COMMIS ION I7 7tfgt NRC DISTRIBUTION FOB I-T 60 DOCI(ET MATERIAL DOCKI'iT NVMf3EfI Sg-g f'LL NUM OE B Mr.Benard Rusche FROM: Indiana&Michigan Power Company New York, N~Y.John Tillinghast DATE OF DOCVIAENT 4/22/77 DATE BECEIVED 4/26/77 Hi.ETTEB O'OB(OINAL CIcopv DES C BI PT I ON Lj MOTO B I Z E D 0$NCLAS'SIFIED INPUT FOBM ENCLOSU BE NUMBER OF COPIES BECEIVED r srs~c4'tr, notorized 4/22/77~~~.trans the-following:
{{#Wiki_filter:U.S. NUCLEAfl BEGULATofIVCOMMIS ION     DOCKI'iT NVMf3EfI NRC FooM 195 I7 7tfgt
'I ll PLANT HAIIE: I gook I RJL (4-P)Consists of requested information regar'ding the chemical cleaqing'of, the.Unit No..2 Feedwatei ans Condensate Systemic+~RICINGl'M989
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Sg-g f'LL NUM OE B NRC DISTRIBUTION FOB                   I-     T 60 DOCI(ET MATERIAL FROM:                                                     DATE OF DOCVIAENT Indiana & Michigan Power                 Company                         4/22/77 Mr. Benard Rusche                                                New York, N~ Y.                                     DATE BECEIVED John       Tillinghast                                                   4/26/77 Hi.ETTEB                               LjMOTO  B IZ E D                                                  INPUT FOBM          NUMBER OF COPIES BECEIVED O'OB(OINAL CIcopv 0$ NCLAS'SIFIED r
'~RO EC~I4ANA E L C ASST~cVc.LXC ASST FOR ACTION/INFORMATION
DES C   BI PT I ON                                                                           ENCLOSU BE                               srs~c4'tr, notorized 4/22/77 ~ ~ ~ .trans the-following:                                                                                 Consists of requested information regar'ding the chemical cleaqing'of, the .Unit No..2
.NEfXII~SIGHED~f'iT~IIXEF~PROJECT I~>IMAGER IN TE R MAL D IST SYSTEMS SAFETY RI BUTJON ELAI.T SZSTEMS~M'L!~NRC PDI/X&E 2 OELD GOSSXCK 6c STAFF CASE HAHAUER HARLESS PROJECT MANAGEMENT BOYD P~COLLXHS HOUSTON PETERSON HELTZ 11 I'.LTEI IES SKOV)IOLT CFOR;S~o~t TIC!HSXC: ASJ.II: ACRS CYS X/NBC FOAM IOS I2 76I HEXIiEMAN SCHROEDER EHGXHEERXNG MACARRY 130SNAK SX1NF T.L P/n<LXC I'X REACTOR SAF~E'OSS NOVAK ROSZTOCZY CHF.CK AT&X SALTL HAH RUT131'.RC EXTERNAL DISTRIBUTION HAT, JAII REG VS IF.LA PDR CO R'ULTANTS!
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PLANT HAIIE:
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TEDESCO LhZHI'A GOSSXCK         6c   STAFF                       EHGXHEERXNG                                  XPPOL TO                  ~ENV RO~QI MACARRY                                                                   ERHST CASE                                              130SNAK                                                                   BALLARD HAHAUER                                            SX1NF T.L                                   OPERATING REACTORS          SPANGLER HARLESS                                            P/n<LXC I'X                                   STELLO SITE TFCH PROJECT MANAGEMENT                                  REACTOR                                     OPERATING TECH              GAI Pi IILL SAF~E'OSS BOYD                                                                                            EXSENIIUT                  STEPP P ~ COLLXHS                                        NOVAK                                         SU                        HULIIAN HOUSTON                                            ROSZTOCZY                               ~DE PETERSON                                            CHF.CK                                       13UTT.E                    SXTE ANALYSIS HELTZ                                                                                              IU/IES                    VOLT.IIER 11 I'.LTEIIES                                      AT&X                                                                     BUNCH SKOV) IOLT                                          SALTLHAH                                                                J ~ 'OT.LIHS RUT131'.RC                                                               KREGER EXTERNAL DISTRIBUTION                                                             CONTROL NUMBER CFOR;S        ~
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INDIANA II MICHIGAN POWER COMPANY P.O.BOX 18 BO WL IN G G R E EN STAT ION NEW YORK, N.Y.10004 April 22, 1977 Donald C.Cook Nuclear plant Unit No.1 Docket No.50-315 DPR No.58 Reggatory,P jig Cy, Mr.Benard Rusche, Director Office of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission Washington, D.C.20555 I'i/8 egg(~>~<PRZ8 pp, IT j~~
INDIANA II MICHIGAN POWER COMPANY P. O. BOX 18 BO WL IN G G R E EN STAT ION NEW YORK, N. Y. 10004 April 22,   1977 Donald C. Cook Nuclear         plant Unit       No. 1 Docket No. 50-315                                               I    'i/ 8 DPR No. 58 Reggatory,P           jig Cy,            egg(~>        ~
                                                            <PRZ8 pp, Mr. Benard Rusche, Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555                                             IT j~~


==Dear Mr.Rusche:==
==Dear Mr. Rusche:==
This letter provides information requested by Mr.M.H.Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning the chemical cleaning of the Unit No.2 Feedwater and Condensate Systems.His requests and our responses follow.Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.~Res onse The 300,000 gallons of flushing solution (pH approximately 11.4)will be displaced through the turbine room sump (capacity 90,000 gallons)to the absorption field.It will be continuously pumped by the sump pumps at.a rate of 2,000 to 3,000 plus gpm.The displacement rinses of demineralized water (pH about 6.5 to 7.5)will follow.These will also be continuously pumped to the field.Total rinse volume will be about 600,000 gallons.The solution and displacement rinses will mix with the approximately 2 x 10 gallons in the absorption field, with a resultant pH of around 10.5.Subsequent discharge of waste water from the turbine room sump (approximately 300,000 gallons/day, pH about 6.5 to 7.5)will further lower the pH to 9.0 or less in two 7'//7o gad W~"((r'I II'0~I, a~I F l I~-I I t IP'I F IF\'g IF g r F If I I F Fy' Mr.B.C.Rusche April 22, 1977 to four weeks.The sediment on the bottom of the pond will assist in lowering the pH.The ability of the waste water to reduce the pH to 9.0 has been confirmed by a rough titration of a sample of the flush/rinse solution with a sample of waste water now in the absorption field.This showed that, about 7 to 8 x 106 gallons of"normal" waste water would reduce the pH from about 11.4 to 9.0..Based on the above operations and characteristics of the rinse water,"normal" waste water, and the absorption field sediment, it is our considered engineering judgement that the resultant water which eventually percolates into the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with xespect to pH limitations.
2.The letter of March 16, 1977 requested that the licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper.Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation proposed, provide justification for the request.~Res onse The Peedwater and Condensate Systems in Unit 2 of the Donald C.Cook Nuclear plant are made only of carbon steel, stain-less steel and copper.The carbon steel has some rust deposits which would be removed by the cleaning operation resulting in'mall quantities of iron being discharged with the cleaning solution.Copper exhibits a very slow corrosion zate in a basic solution such as that which will be used in the subject.chemical cleaning operation.
Even the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities of copper being discharged with the cleaning solution.Stainless steel is particularly resistant to corrosion such that no rust exists on the stainless steel surfaces and no corrosion will xesult from contact with the cleaning solution.
~e Ih~'f~I~~,I I gh C.h I,'C It II C~e~I If h 1I W C I v h'e ce I e C I'Cr C~'If e.e~h C e Phh.Q gC C\e>>C h C)"
Mr.B.C.Rusche April 22, 1977 Appendix B Specification 2,.2.3.2 requires monitoring for heavy metals when spent chemical cleaning solutions are to be discharged to the absorption field.We will comply with this by monitoring for those potential candidates which could be removed by the cleaning'operation
-iron and copper.3.Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field.Include any supportive information which is available.
~Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5.5 to 9 prior to discharge.
For purposes of=this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.
A similar chemical cleaning operation for Unit 1 was performed in July 1973.Preoperational terrestrial and aquatic studies were in effect at that time and, although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected.(See Appendix D,"Terrestrial Studies" in the Environmental Operating Report (EOR)covering October through December 1974, and Benton Harbor Power Plant Limnological Studies, Special Report No.44.of the Great Lakes Research Division of the University of Michigan.In addition, the postoperational studies now in effect, have detected no changes of a long term nature which are attributable to the first cleaning.(See EOR's covering all of 1975 and.1976).Groundwater monitoring at the site, as required by Appendix B Technical Specification 4.1.1.5, was started in late 1974, slightly over one year following the first cleaning operation.
Two wells were drilled from which groundwater moving from the absorption pond to the lake can be monitored.
Sampling from these has shown that even when high discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and 9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years).
~WI g 3 1(lt-hf, I I.I~4(gjf 3 r V~4 I f(4((()'I v'e,-I(tl I$t(Ph y gh''h''I e.3(W(e'I ('f V r~glt~',f 4~, r I I Ih C~3 Phf 4 It'I'I'Vl v>>'I C'(I t(J V-V f V 3 I'~-3 C"'~~V",W~" V V', 41 Pt(It~"'.0()(('I e>f("(V~, I 433\I I h Per.B.C.Rusche April 22, 1977 The discharge of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C.Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.Very truly yours, JT:mam Vice President Sworn and subscribed to before me this 22nd day of April, 1977 in New York County, New York Notary Public KATI.H HPA DARRX NOTARY PUSt.!C, State ol New York, Yo.41-4GOG793'" Qualitied in Queens County g~tjIicate liled irt New York County.Cornnusston axpuus triarch 30, 19'Ff cc: G.Charnoff P.W.Steketee R.C.Callen R.Walsh R.J.Vollen R.W.Jurgensen-Bridgman R.S.Hunter 4~4 4 808]y l26t Clljg".ISS3ggpg llgg IlGOO 09AI3038
~--~INDIANA R MICHIGAN POWER COMPANY P O.BOX 18 BOWLING GREEN STATION HRW YORK, N.Y.1000i April 22, 1977 Donald C.Cook Nuclear Plant Unit No.1 Docket No.50-315 DPR No.58 Mr.Benard Rusche, Director Office of Nuclear Reactor Regulation U;S.Nuclear Regulatory Commission Whshington, D.C.20555


==Dear Mr.Rusche:==
This letter provides information requested by Mr. M. H. Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning the chemical cleaning of the Unit No. 2 Feedwater and Condensate Systems.       His requests and our responses follow.
This letter provides information requested by Mr.M.H.Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning'the chemical cleaning of the Unit No.2 Feedwater and Condensate Systems.His requests and our responses follow.1.Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.Res onse The 300,000 gallons of flushing solution (pH approximately
Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.
'1.4)will be displaced through the turbine room sump (capacity 90,000 gallons)to the absorption field..It will be continuously pumped by the sump'pumps at a rate of 2,000 to 3,000 plus gpm.The displacement rinses of demineralized water (pH about 6.5 to'.5)will follow.These will also be continuously pumped to the field.Total.rinse volume will be about 600,000 gallons.~va ra The solution and displacement rinses will mix with the approximately 2 x 10 gallons in the absorption field, with a resultant pH of around 10.5.Subsequent discharge of waste water from the turbine room sump (approximately
    ~Res onse The 300,000       gallons of flushing solution (pH approximately 11.4) will be displaced through the turbine room sump (capacity 90,000 gallons) to the absorption field. It will be continuously pumped by the sump pumps at. a rate of 2,000 to 3,000 plus gpm.
'300,000 gallons/day, pH about 6.5 to 7.5)will further lower the pH to 9.0 or less in two  
The displacement rinses of demineralized water (pH about 6.5 to 7.5) will follow. These will also be continuously pumped to the field. Total rinse volume will be about 600,000 gallons.
The solution     and displacement rinses will mix with the approximately 2 x   10     gallons in the absorption field, with a resultant pH of around 10.5.             Subsequent discharge of waste water from the turbine room sump (approximately 300,000 gallons/day, pH about 6.5 to 7.5) will further lower the pH to 9.0 or less in two 7'//7o gad


Mr.B.C.Rusche~.April 22, 1977 to four weeks.The sediment.on the bottom of the pond will assist in lowering the pH.The ability of the waste water to reduce the pH to 9.0 has been confirmed by a rough titration of a sample of the flush/rinse solution with a sample of waste water now in the absorption field.This showed that about 7 to 8 x 106 gallons of"normal" waste water would reduce the pH from about 11.4'to 9.0.Based on the above operations and characteristics of the rinse water,"normal" waste water, and the absorption field sediment, it is our considered engineering judgement that the'resultant water which eventually percolates into"the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with respect to pH limitations.
W
2.The letter of March 16, 1977 requested that the.licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper.Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation proposed, provide justification for the request.II~Res ense The Feedwater and Condensate Systems in Unit 2 of the.Donald C.Cook, Nuc3.ear Plant are made only of carbon steel, stain-less steel and copper.-The carbon steel has some rust deposits which would be removed by the cleaning operation resulting in small quantities of iron being discharged with the cle'aning solution.Copper exhibits a very slow corrosion rate in a basic.solution such as that which will be used, in the subject chemical cleaning operation.
                                                          ~ "(      (
rien the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities=
r 'I II
of copper being discharged with the cleaning solution.,Stainless steel is particularly resistant to corrosion such that no rust exists on the stainless steel surfaces and no corrosion will result from contact with the cleaning solution.
                          '
gr.B.c.Rusche~ApM1.22, 1977 Appendix B Specification 2.2.3.2 requires monitoring for heavy metals when spent chemical cleaning solutions are to be discharged to the absorption field.We will comply with this by monitoring for those potential candidates which could be removed by the cleaning operation-iron and copper.3.Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field.Xnclude any supportive information which is available..Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5;5 to 9 prior to discharge.
I, 0  ~
For purposes of this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.
a
A similar chemical cleaning operation for Unit 1 was performed in July 1973.Preoperational terrestrial and aquatic studies were in effect at that time and,,although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected.(See Appendix D,"Terrestrial Studies" in the Environmental Operating Report (EOR)covering October'hrough December 1974, and Benton Harbor Power Plant Limnological
                                ~ I                            F l
~Studies, Special Report No.44 of the Great Lakes Research Division of the University of Michigan.Xn addition, the postoperational studies now in effect have detected no changes of a long term nature which are attributable to the first cleaning.(See EOR's covering all of 1975 and 1976).Groundwater monitoring at the site, as required by Appendix B Technical Specification 4.1.1.5,'was started.in late 1974, slightly over one year following the first cleaning operation.
I ~-
Two wells were drilled from.which groundwater moving from the absorption pond to the lake can.be, monitored.
I I
Sampling from these has show'n that.even when high.discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and.9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years).
t IP          'I    F                        IF
S.C.Rusche April 22, 1977 The discharge of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C.'Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.Very truly yours, JT imam Vice President Sworn and subscribed to before me this 22nd day of April, 1977 in New York County, New York Notary Public KATEILEC".4 BARRY HOTARY irUitt.tC, Stets ot thew York No.41-iGOG i&2 Qualified in Queens County Certificete filed in Hew'lark~Cornnussran tkprres lnerah 30'97 I cc: G.Charnoff P N.Steketee R.C.Callen R.Nalsh R., J.Vollen , R.N.Jurgensen-Bridgman R.S.Hunter
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Mr. B. C. Rusche                                  April 22, 1977 to four    weeks. The sediment on the bottom of the pond   will assist in lowering the     pH.
The ability of the waste water to reduce the pH to 9.0 has been confirmed by a rough titration of a sample of the flush/
rinse solution with a sample of waste water now in the absorption field. This showed that, about 7 to 8 x 106 gallons of "normal" waste water would reduce the pH from about 11.4 to 9.0..
Based on the above operations and characteristics of the rinse water, "normal" waste water, and the absorption field sediment,   it is our considered engineering judgement that the resultant water which eventually percolates into the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with xespect to pH limitations.
: 2. The letter of March 16, 1977 requested that the licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper. Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation proposed, provide justification for the request.
      ~Res onse The Peedwater  and Condensate   Systems in Unit 2 of the Donald C. Cook Nuclear    plant are made only of carbon steel, stain-less steel and copper.     The carbon steel has some rust deposits which would be removed by the cleaning operation resulting quantities of iron being discharged with the cleaning      in'mall solution. Copper exhibits a very slow corrosion zate in a basic solution such as that which will be used in the subject. chemical cleaning operation. Even the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities of copper being discharged with the cleaning solution.
Stainless steel is particularly resistant to corrosion such that no rust exists on the stainless steel surfaces and no corrosion will xesult from contact with the cleaning solution.
 
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Mr. B. C. Rusche                                  April 22,  1977 Appendix B Specification 2,.2.3.2 requires monitoring for heavy metals when spent chemical cleaning solutions are to be discharged to the absorption field. We will comply with this by monitoring for those potential candidates which could be removed by the cleaning 'operation - iron and copper.
: 3. Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field. Include any supportive information which is available.
      ~Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5.5 to 9 prior to discharge. For purposes of
=this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.
A similar chemical cleaning operation for Unit   1 was performed in July 1973.       Preoperational terrestrial and aquatic studies were in effect at that time and, although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected.       (See Appendix D, "Terrestrial Studies" in the Environmental Operating Report (EOR) covering October through December 1974, and Benton Harbor Power Plant Limnological Studies, Special Report No. 44 .of the Great Lakes Research Division of the University of Michigan. In addition, the postoperational studies now in effect, have detected no changes of a long term nature which are attributable to the first cleaning.       (See EOR's covering all of 1975 and. 1976).
Groundwater monitoring   at the site, as required by Appendix   B Technical Specification 4.1.1.5, was started in late 1974,   slightly over one year following the first cleaning operation. Two wells were drilled from which groundwater moving from the absorption pond to the lake can be monitored. Sampling from these has shown that even when high discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and 9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years).
 
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Per. B. C. Rusche                                          April 22,  1977 The    discharge of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C. Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.
Very truly yours, Vice President JT:mam Sworn and subscribed to before me this 22nd day of April, 1977 in New    York County,              New  York Notary Public KATI.HHPA DARRX NOTARY PUSt.!C, State ol New York, Yo. 41-4GOG793'"
Qualitied in Queens County County.
g~tjIicate liled irt New York 19'Ff Cornnusston axpuus triarch 30, cc:      G. Charnoff P. W. Steketee R. C. Callen R. Walsh R. J. Vollen R. W. Jurgensen                Bridgman R. S. Hunter
 
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INDIANA      R  MICHIGAN POWER COMPANY P  O. BOX 18 BOWLING GREEN STATION HRW YORK, N. Y. 1000i April 22,  1977 Donald C. Cook Nuclear Plant        Unit No. 1 Docket No. 50-315 DPR  No. 58 Mr. Benard Rusche, Director Office of Nuclear Reactor Regulation U;S. Nuclear Regulatory Commission Whshington, D.C. 20555
 
==Dear Mr. Rusche:==
 
This letter provides information requested by Mr. M. H. Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning 'the chemical cleaning of the Unit No. 2 Feedwater and Condensate Systems.      His requests and our responses follow.
: 1. Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.
Res onse The 300,000    gallons of flushing solution (pH approximately
'1.4) will be      displaced through the turbine room sump (capacity 90,000 gallons) to the absorption field..        It    will be continuously pumped by the sump'pumps at a rate of 2,000 to 3,000 plus gpm.
The displacement rinses of demineralized water (pH about 6.5 to
'.5) will follow. These will also be continuously              pumped to the field. Total. rinse volume    will be  about 600,000 gallons.
va  ra and displacement rinses will mix with the
                                                    ~
The  solution approximately    2 x  10    gallons in the absorption field, with a resultant pH of around 10.5. Subsequent discharge of waste water from the turbine room sump (approximately '300,000 gallons/day, pH about 6.5 to 7.5) will further lower the pH to 9.0 or less in two
 
                              ~  .
Mr. B. C. Rusche                                    April 22,  1977 to four    weeks.      The sediment. on  the bottom of the pond  will assist in  lowering      the pH.
The  ability of  the waste water to reduce the  pH  to 9.0 has been confirmed by a rough titration of a sample of the flush/
rinse solution with a sample of waste water now in the absorption field. This showed that about 7 to 8 x 106 gallons of "normal" waste water would reduce the pH from about 11.4'to 9.0.
Based on the above operations and characteristics of the  rinse    water,    "normal" waste water, and the absorption field sediment,      it  is our considered engineering judgement that the
  'resultant water which eventually percolates into "the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with respect to pH limitations.
: 2.      The  letter of March 16, 1977 requested that the
                  .licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper. Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation II proposed, provide justification for the request.
          ~Res    ense The Feedwater and Condensate Systems in Unit 2 of the
. Donald C. Cook, Nuc3.ear Plant are made only of carbon steel, stain-less steel and copper. The carbon steel has some rust deposits
                                    -
which would be removed by the cleaning operation resulting in small quantities of iron being discharged with the cle'aning solution. Copper exhibits a very slow corrosion rate in a basic
. solution such as that which will be used, in the subject chemical cleaning operation. rien the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities= of copper being discharged with the cleaning solution.
                  ,Stainless steel    is particularly resistant to corrosion such  that      no  rust exists  on the stainless steel surfaces and no corrosion      will result    from contact with the cleaning solution.
 
gr. B. c. Rusche  ~                          ApM1. 22, 1977 Appendix B Specification 2.2.3.2 requires monitoring for  heavy  metals when spent chemical cleaning solutions are to be discharged to the absorption field. We will comply with this by monitoring for those potential candidates which could be removed by the cleaning operation - iron and copper.
: 3. Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field. Xnclude any supportive information which is available.
        .Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5;5 to 9 prior to discharge. For purposes of this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.
A similar chemical cleaning operation for Unit 1 was performed in July 1973. Preoperational terrestrial and aquatic studies were in effect at that time and,,although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected.      (See Appendix D, "Terrestrial Studies" in the Environmental Operating Report (EOR) covering October
  'hrough December 1974, and Benton Harbor Power Plant Limnological
~
Studies, Special Report No. 44 of the Great Lakes Research Division of the University of Michigan. Xn addition, the postoperational studies now in effect have detected no changes of a long term nature which are attributable to the first cleaning.      (See EOR's covering all of 1975 and 1976).
Groundwater monitoring at the site, as required by Appendix B Technical Specification 4.1.1.5, 'was started. in late 1974, slightly over one year following the first cleaning operation. Two wells were drilled from. which groundwater moving from the absorption pond to the lake can. be, monitored. Sampling from these has show'n that. even when high. discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and .9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years) .
 
S. C. Rusche                                      April 22,  1977 The discharge    of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C.'Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.
Very truly yours, Vice President JT imam Sworn and subscribed to before me this 22nd day of April, 1977 in New      York County,            New York Notary Public KATEILEC".4 BARRY HOTARY irUitt.tC, Stets ot thew York No. 41-iGOG i&2 Qualified in Queens County Certificete filed in Hew 'lark Cornnussran tkprres lnerah 30'97
                                ~ I cc:        G. Charnoff P N. Steketee R. C. Callen R. Nalsh R., J. Vollen
        ,  R. N. Jurgensen            - Bridgman R. S. Hunter
 
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Revision as of 18:41, 20 October 2019

04/22/1977 Response to Request for Additional Information Chemical Cleaning of the Unit No. 2 Feedwater and Condensate Systems
ML18219D954
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/22/1977
From: Tillinghast J
Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co)
To: Rusche B
Office of Nuclear Reactor Regulation
References
Download: ML18219D954 (16)


Text

U.S. NUCLEAfl BEGULATofIVCOMMIS ION DOCKI'iT NVMf3EfI NRC FooM 195 I7 7tfgt

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Sg-g f'LL NUM OE B NRC DISTRIBUTION FOB I- T 60 DOCI(ET MATERIAL FROM: DATE OF DOCVIAENT Indiana & Michigan Power Company 4/22/77 Mr. Benard Rusche New York, N~ Y. DATE BECEIVED John Tillinghast 4/26/77 Hi.ETTEB LjMOTO B IZ E D INPUT FOBM NUMBER OF COPIES BECEIVED O'OB(OINAL CIcopv 0$ NCLAS'SIFIED r

DES C BI PT I ON ENCLOSU BE srs~c4'tr, notorized 4/22/77 ~ ~ ~ .trans the-following: Consists of requested information regar'ding the chemical cleaqing'of, the .Unit No..2

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INDIANA II MICHIGAN POWER COMPANY P. O. BOX 18 BO WL IN G G R E EN STAT ION NEW YORK, N. Y. 10004 April 22, 1977 Donald C. Cook Nuclear plant Unit No. 1 Docket No. 50-315 I 'i/ 8 DPR No. 58 Reggatory,P jig Cy, egg(~> ~

<PRZ8 pp, Mr. Benard Rusche, Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 IT j~~

Dear Mr. Rusche:

This letter provides information requested by Mr. M. H. Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning the chemical cleaning of the Unit No. 2 Feedwater and Condensate Systems. His requests and our responses follow.

Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.

~Res onse The 300,000 gallons of flushing solution (pH approximately 11.4) will be displaced through the turbine room sump (capacity 90,000 gallons) to the absorption field. It will be continuously pumped by the sump pumps at. a rate of 2,000 to 3,000 plus gpm.

The displacement rinses of demineralized water (pH about 6.5 to 7.5) will follow. These will also be continuously pumped to the field. Total rinse volume will be about 600,000 gallons.

The solution and displacement rinses will mix with the approximately 2 x 10 gallons in the absorption field, with a resultant pH of around 10.5. Subsequent discharge of waste water from the turbine room sump (approximately 300,000 gallons/day, pH about 6.5 to 7.5) will further lower the pH to 9.0 or less in two 7'//7o gad

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Mr. B. C. Rusche April 22, 1977 to four weeks. The sediment on the bottom of the pond will assist in lowering the pH.

The ability of the waste water to reduce the pH to 9.0 has been confirmed by a rough titration of a sample of the flush/

rinse solution with a sample of waste water now in the absorption field. This showed that, about 7 to 8 x 106 gallons of "normal" waste water would reduce the pH from about 11.4 to 9.0..

Based on the above operations and characteristics of the rinse water, "normal" waste water, and the absorption field sediment, it is our considered engineering judgement that the resultant water which eventually percolates into the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with xespect to pH limitations.

2. The letter of March 16, 1977 requested that the licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper. Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation proposed, provide justification for the request.

~Res onse The Peedwater and Condensate Systems in Unit 2 of the Donald C. Cook Nuclear plant are made only of carbon steel, stain-less steel and copper. The carbon steel has some rust deposits which would be removed by the cleaning operation resulting quantities of iron being discharged with the cleaning in'mall solution. Copper exhibits a very slow corrosion zate in a basic solution such as that which will be used in the subject. chemical cleaning operation. Even the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities of copper being discharged with the cleaning solution.

Stainless steel is particularly resistant to corrosion such that no rust exists on the stainless steel surfaces and no corrosion will xesult from contact with the cleaning solution.

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Mr. B. C. Rusche April 22, 1977 Appendix B Specification 2,.2.3.2 requires monitoring for heavy metals when spent chemical cleaning solutions are to be discharged to the absorption field. We will comply with this by monitoring for those potential candidates which could be removed by the cleaning 'operation - iron and copper.

3. Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field. Include any supportive information which is available.

~Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5.5 to 9 prior to discharge. For purposes of

=this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.

A similar chemical cleaning operation for Unit 1 was performed in July 1973. Preoperational terrestrial and aquatic studies were in effect at that time and, although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected. (See Appendix D, "Terrestrial Studies" in the Environmental Operating Report (EOR) covering October through December 1974, and Benton Harbor Power Plant Limnological Studies, Special Report No. 44 .of the Great Lakes Research Division of the University of Michigan. In addition, the postoperational studies now in effect, have detected no changes of a long term nature which are attributable to the first cleaning. (See EOR's covering all of 1975 and. 1976).

Groundwater monitoring at the site, as required by Appendix B Technical Specification 4.1.1.5, was started in late 1974, slightly over one year following the first cleaning operation. Two wells were drilled from which groundwater moving from the absorption pond to the lake can be monitored. Sampling from these has shown that even when high discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and 9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years).

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Per. B. C. Rusche April 22, 1977 The discharge of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C. Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.

Very truly yours, Vice President JT:mam Sworn and subscribed to before me this 22nd day of April, 1977 in New York County, New York Notary Public KATI.HHPA DARRX NOTARY PUSt.!C, State ol New York, Yo. 41-4GOG793'"

Qualitied in Queens County County.

g~tjIicate liled irt New York 19'Ff Cornnusston axpuus triarch 30, cc: G. Charnoff P. W. Steketee R. C. Callen R. Walsh R. J. Vollen R. W. Jurgensen Bridgman R. S. Hunter

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INDIANA R MICHIGAN POWER COMPANY P O. BOX 18 BOWLING GREEN STATION HRW YORK, N. Y. 1000i April 22, 1977 Donald C. Cook Nuclear Plant Unit No. 1 Docket No. 50-315 DPR No. 58 Mr. Benard Rusche, Director Office of Nuclear Reactor Regulation U;S. Nuclear Regulatory Commission Whshington, D.C. 20555

Dear Mr. Rusche:

This letter provides information requested by Mr. M. H. Fletcher, of the NRC Division of Operating Reactors, in connection with our letter of March 16, 1977 to you con-cerning 'the chemical cleaning of the Unit No. 2 Feedwater and Condensate Systems. His requests and our responses follow.

1. Provide a detailed description of the chemical cleaning operation which indicates how a ph of 9.0 is expected in the absorption field following the discharge of the cleaning solution.

Res onse The 300,000 gallons of flushing solution (pH approximately

'1.4) will be displaced through the turbine room sump (capacity 90,000 gallons) to the absorption field.. It will be continuously pumped by the sump'pumps at a rate of 2,000 to 3,000 plus gpm.

The displacement rinses of demineralized water (pH about 6.5 to

'.5) will follow. These will also be continuously pumped to the field. Total. rinse volume will be about 600,000 gallons.

va ra and displacement rinses will mix with the

~

The solution approximately 2 x 10 gallons in the absorption field, with a resultant pH of around 10.5. Subsequent discharge of waste water from the turbine room sump (approximately '300,000 gallons/day, pH about 6.5 to 7.5) will further lower the pH to 9.0 or less in two

~ .

Mr. B. C. Rusche April 22, 1977 to four weeks. The sediment. on the bottom of the pond will assist in lowering the pH.

The ability of the waste water to reduce the pH to 9.0 has been confirmed by a rough titration of a sample of the flush/

rinse solution with a sample of waste water now in the absorption field. This showed that about 7 to 8 x 106 gallons of "normal" waste water would reduce the pH from about 11.4'to 9.0.

Based on the above operations and characteristics of the rinse water, "normal" waste water, and the absorption field sediment, it is our considered engineering judgement that the

'resultant water which eventually percolates into "the ground will have a pH of 9.0 or less and would therefore meet the intent of the technical specifications with respect to pH limitations.

2. The letter of March 16, 1977 requested that the

.licensee not be required to monitor the discharge to the absorption pond for heavy metals other than iron and copper since the systems being chemically cleaned are made up almost entirely of iron and copper. Since Appendix B Section 2.2.3.2, which requires the monitoring of heavy metals, is intended specifically for the type chemical cleaning operation II proposed, provide justification for the request.

~Res ense The Feedwater and Condensate Systems in Unit 2 of the

. Donald C. Cook, Nuc3.ear Plant are made only of carbon steel, stain-less steel and copper. The carbon steel has some rust deposits

-

which would be removed by the cleaning operation resulting in small quantities of iron being discharged with the cle'aning solution. Copper exhibits a very slow corrosion rate in a basic

. solution such as that which will be used, in the subject chemical cleaning operation. rien the very large surface area represented by the copper tubing in the condensers should, when cleaned, result in just barely measurable quantities= of copper being discharged with the cleaning solution.

,Stainless steel is particularly resistant to corrosion such that no rust exists on the stainless steel surfaces and no corrosion will result from contact with the cleaning solution.

gr. B. c. Rusche ~ ApM1. 22, 1977 Appendix B Specification 2.2.3.2 requires monitoring for heavy metals when spent chemical cleaning solutions are to be discharged to the absorption field. We will comply with this by monitoring for those potential candidates which could be removed by the cleaning operation - iron and copper.

3. Provide an appraisal of the environmental impact resulting from the discharge of the chemical cleaning solution and flush waters to the absorption field. Xnclude any supportive information which is available.

.Res onse The Technical Specifications require that all chemical discharges to the absorption field be neutralized to give a pH in the range of 5;5 to 9 prior to discharge. For purposes of this one-time chemical cleaning operation our request amounts to neutralization of the discharge in the pond water after discharge, rather than neutralization in the plant prior to discharge.

A similar chemical cleaning operation for Unit 1 was performed in July 1973. Preoperational terrestrial and aquatic studies were in effect at that time and,,although no separate observations were made specifically for this event, no damage to the flora and fauna around the absorption field or to the aquatic life was detected. (See Appendix D, "Terrestrial Studies" in the Environmental Operating Report (EOR) covering October

'hrough December 1974, and Benton Harbor Power Plant Limnological

~

Studies, Special Report No. 44 of the Great Lakes Research Division of the University of Michigan. Xn addition, the postoperational studies now in effect have detected no changes of a long term nature which are attributable to the first cleaning. (See EOR's covering all of 1975 and 1976).

Groundwater monitoring at the site, as required by Appendix B Technical Specification 4.1.1.5, 'was started. in late 1974, slightly over one year following the first cleaning operation. Two wells were drilled from. which groundwater moving from the absorption pond to the lake can. be, monitored. Sampling from these has show'n that. even when high. discharge quantities are sent to the absorption, pond, (averaging 300,000 gallons/day with pH varying between 5.5 and .9.0 since restart of construction activities in Unit 2 in 1975), the pH of the groundwater does not vary to any significant degree (7.0 to 7.8 in the last two years) .

S. C. Rusche April 22, 1977 The discharge of the chemical cleaning solution and flush waters to the absorption field resulting from the cleaning of the Unit 2 Feedwater and Condensate Systems at the Donald C.'Cook Nuclear Plant will have a negligible environmental impact in and around the vicinity of the absorption field.

Very truly yours, Vice President JT imam Sworn and subscribed to before me this 22nd day of April, 1977 in New York County, New York Notary Public KATEILEC".4 BARRY HOTARY irUitt.tC, Stets ot thew York No. 41-iGOG i&2 Qualified in Queens County Certificete filed in Hew 'lark Cornnussran tkprres lnerah 30'97

~ I cc: G. Charnoff P N. Steketee R. C. Callen R. Nalsh R., J. Vollen

, R. N. Jurgensen - Bridgman R. S. Hunter

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