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Category:Letter
MONTHYEAR05000316/LER-2024-004, AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications2024-11-11011 November 2024 AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications IR 05000315/20240032024-10-31031 October 2024 Integrated Inspection Report 05000315/2024003 05000316/2024003 07200072/2024001 and Exercise of Enforcement Discretion AEP-NRC-2024-77, U2C28 Steam Generator Tube Inspection Report2024-10-21021 October 2024 U2C28 Steam Generator Tube Inspection Report AEP-NRC-2024-80, Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask2024-10-15015 October 2024 Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask AEP-NRC-2024-79, Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask2024-09-26026 September 2024 Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask AEP-NRC-2024-78, Reply to a Notice of Violation: EA-24-0472024-09-23023 September 2024 Reply to a Notice of Violation: EA-24-047 05000316/LER-2024-002-01, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-09-12012 September 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak IR 05000315/20244022024-09-10010 September 2024 Security Baseline Inspection Report 05000315/2024402 and 05000316/2024402, Independent Spent Fuel Storage Installation Security Inspection Report 07200072/2024401 AEP-NRC-2024-69, Core Operating Limits Report2024-09-0909 September 2024 Core Operating Limits Report IR 05000315/20243012024-09-0505 September 2024 NRC Initial License Examination Report 05000315/2024301 and 05000316/2024301 ML24225A0022024-09-0303 September 2024 Issuance of Amendment Nos. 363 and 344 Revising Technical Specifications Section 3.8.1, AC Sources-Operating, for a One-Time Extension of a Completion Time IR 05000315/20240112024-08-30030 August 2024 NRC Inspection Report 05000315/2024011 and 05000316/2024011 and Notice of Violation AEP-NRC-2024-76, Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-08-28028 August 2024 Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating AEP-NRC-2024-51, Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes2024-08-28028 August 2024 Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes 05000316/LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage2024-08-22022 August 2024 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage IR 05000315/20240052024-08-21021 August 2024 Updated Inspection Plan for Donald C. 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Cook Nuclear Plant, Emergency Plan Revision 492024-05-14014 May 2024 Transmittal of Donald C. Cook Nuclear Plant, Emergency Plan Revision 49 IR 05000315/20244012024-05-14014 May 2024 – Security Baseline Inspection Report 05000315/2024401 and 05000316/2024401 ML24115A2152024-05-0707 May 2024 LTR: CNP Non-Acceptance with Opportunity TS 3-8-1 AEP-NRC-2024-24, Form OAR-1, Owners Activity Report2024-05-0707 May 2024 Form OAR-1, Owners Activity Report ML24256A1472024-05-0606 May 2024 DC Cook 2024 NRC Examination Submittal Letter: Submittal ML24116A0002024-05-0202 May 2024 – Regulatory Audit in Support of Review of the Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors AEP-NRC-2024-35, Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations2024-04-30030 April 2024 Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations AEP-NRC-2024-28, 2023 Annual Radioactive Effluent Release Report2024-04-29029 April 2024 2023 Annual Radioactive Effluent Release Report AEP-NRC-2024-31, Annual Report of Individual Monitoring2024-04-24024 April 2024 Annual Report of Individual Monitoring AEP-NRC-2024-02, Unit 2 License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-04-0303 April 2024 Unit 2 License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating 2024-09-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000316/LER-2024-004, AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications2024-11-11011 November 2024 AB Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications 05000316/LER-2024-002-01, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-09-12012 September 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak 05000316/LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage2024-08-22022 August 2024 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage 05000316/LER-2024-002, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-07-15015 July 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak 05000316/LER-2024-001, Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip2024-05-20020 May 2024 Reactor Trip Due to Main Turbine Trip from a High-High Thrust Bearing Position Trip 05000315/LER-2023-002, Failure of Unit 1 West Auxiliary Feedwater Pump to Restart During Load Sequencer Testing2023-12-12012 December 2023 Failure of Unit 1 West Auxiliary Feedwater Pump to Restart During Load Sequencer Testing 05000315/LER-2023-001, Two Trains of Fuel Handling Area Exhaust Ventilation Inoperable2023-09-28028 September 2023 Two Trains of Fuel Handling Area Exhaust Ventilation Inoperable 05000315/LER-2022-003-01, Automatic Trip on Losss of Flow Due to Reactor Coolant Pump Trip2023-02-22022 February 2023 Automatic Trip on Losss of Flow Due to Reactor Coolant Pump Trip 05000316/LER-2022-001, Automatic Reactor Trip Due to Steam Generator High-High Level2023-01-0404 January 2023 Automatic Reactor Trip Due to Steam Generator High-High Level 05000315/LER-2022-003, Automatic Reactor Trip on Loss of Flow Due to Reactor Coolant Pump Trip2022-10-19019 October 2022 Automatic Reactor Trip on Loss of Flow Due to Reactor Coolant Pump Trip 05000315/LER-2022-002, Ice Condenser Door Inoperable Resulting in a Condition Prohibited by Technical Specifications2022-09-20020 September 2022 Ice Condenser Door Inoperable Resulting in a Condition Prohibited by Technical Specifications 05000315/LER-2022-001, Manual Reactor Trio Following Manual Turbine Trio Due to High Vibrations on Main Turbine2022-07-21021 July 2022 Manual Reactor Trio Following Manual Turbine Trio Due to High Vibrations on Main Turbine 05000316/LER-2021-002, Re Manual Reactor Trip Due to an Unisolable Steam Leak2021-08-18018 August 2021 Re Manual Reactor Trip Due to an Unisolable Steam Leak 05000315/LER-2021-001, Main Steam Safety Valve Setpoints Found Outside Technical Specifications Limits2021-06-10010 June 2021 Main Steam Safety Valve Setpoints Found Outside Technical Specifications Limits 05000316/LER-2020-004-01, Regarding Unit 2 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level2021-02-25025 February 2021 Regarding Unit 2 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level 05000316/LER-2020-004, Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level2020-12-0909 December 2020 Automatic Reactor Trip on Low-Low 24 Steam Generator Water Level 05000315/LER-2020-001, Containment Closure Requirements Not Met During Refueling Operations2020-12-0909 December 2020 Containment Closure Requirements Not Met During Refueling Operations 05000316/LER-2020-003, Manual Reactor Trip and Automatic Safety Injection Due to Failed Open Pressurizer Spray Valve2020-11-0202 November 2020 Manual Reactor Trip and Automatic Safety Injection Due to Failed Open Pressurizer Spray Valve 05000316/LER-2017-0012017-05-19019 May 2017 1 OF 5, LER 17-001-00 for Cook, Unit 2 re Containment Hydrogen Skimmer Ventilation Fan #1 Inoperable Longer than Allowed by Technical Specifications 05000316/LER-2016-0022017-02-0909 February 2017 Emergency Diesel Generators Declared Inoperable Due to a Manufacturing Design Issue, LER 16-002-00 for Donald C. Cook Nuclear Plant Unit 2 Regarding Emergency Diesel Generators Declared Inoperable Due to a Manufacturing Design Issue 05000316/LER-2016-0012016-08-31031 August 2016 Manual Reactor Trip Due To Moisture Separator Heater Expansion Joint Failure, LER 16-001-00 for Donald C. Cook Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due To Moisture Separator Heater Expansion Joint Failure ML16193A3902016-07-15015 July 2016 Donald C. Cook Nuclear Plant Unit 2 - A Loss of Main Condenser Event Occurred Due to a Storm-Induced Debris Damage of the Circulating Water System Pumps in the Forebay (LER-316-2014-003-00) 05000315/LER-2015-0022016-01-18018 January 2016 -Technical Specification Violation due to Inoperable Residual. Heat Removal Pump, LER 15-002-01 for D.C. Cook, Unit 1, Regarding Technical Specification Violation Due to Inoperable Residual Heat Removal Pump 05000316/LER-2015-0012016-01-15015 January 2016 Manual Reactor Trip Due To A Secondary Plant Transient, LER 15-001-01 for D.C. Cook, Unit 2, Regarding Manual Reactor Trip Due to a Secondary Plant Transient ML0528703602005-10-0505 October 2005 Special Report for D. C. Cook Unit 2 Re Unit 2 Reactor Coolant Inventory Tracking System ML0508903452005-03-22022 March 2005 LER 99-001-01 Donald C. Cook Nuclear Plant Unit 2, Regarding Supplemental LER for Degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations ML0210601432002-04-12012 April 2002 LER 02-02-00, Donald C. Cook Nuclear Plant Unit 2, Technical Specification 3.9.4.c Was Violated During Core Alteration ML0209205342002-03-15015 March 2002 LER 99-012-01 for Cook Nuclear Plant, Unit 1 Re Auxiliary Building ESF Ventilation System May Not Be Capable of Maintaining ESF Room Temperature Post-Accident ML9936300511999-12-20020 December 1999 LER 99-S004-00, Intentionally Falsifying Documentation Results in Unauthorized Unescorted Access, on 11/18/99. with Letter Dated 12/20/99 05000315/LER-1999-027, LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination1999-11-29029 November 1999 LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination ML18219B5201978-09-27027 September 1978 09/27/1978 Letter Enclosure of Licensee Event Report ML18219E1521978-09-27027 September 1978 Submit Licensee Event Report Nos. RO 78-051/03L-0 & RO 78-052/03L-0 ML18219B5211978-09-19019 September 1978 09/19/1978 Letter Enclosure of Licensee Event Report ML18219B5541978-09-18018 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report (RO 78-062/03L-0) ML18219E1531978-09-18018 September 1978 Submit Licensee Event Report No. RO 78-050/03L-0 ML18219B5551978-09-12012 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-56/03L-1 and RO 78-061/03L-0) ML18219E1541978-09-12012 September 1978 Submit Licensee Event Report No. RO 78-049/03L-0 ML18219B5561978-09-0808 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-059/03L-1 and RO 78-060/03L-0) ML18219E1551978-09-0808 September 1978 Submit Licensee Event Report No. RO 78-048/03L-0 ML18219B5571978-09-0505 September 1978 Letter from Indiana & Michigan Power Co to NRC Submitting License Event Report RO 78-059/03L-0 ML18219B5581978-08-30030 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report RO 78-058/03L-0 ML18219B5621978-08-22022 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-056/03L-0 and RO 78-057/03L-0) ML18219B5611978-08-18018 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Reports (RO 78-052/03L-0, RO 78-053/03L-0, RO 78-054-03L-0 and RO 78-055/03L-0) ML18219E1561978-08-15015 August 1978 Submit Licensee Event Report No. RO 78-047/03L-0 ML18219E1581978-08-14014 August 1978 Submit Licensee Event Report Nos. RO 78-043/03L-1 & RO 78-044/03L-1 ML18219E1571978-08-14014 August 1978 Submit Licensee Event Report Nos. RO 78-045/03L-0 & RO 78-046/03L-0 ML18219E1601978-08-11011 August 1978 Submit Licensee Event Report Nos. 1978-043-03L & 1978-044-03L ML18219B5641978-08-10010 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report (RO 78-051/03L-0) ML18219B5651978-08-0909 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report (RO 78-049/03L-1) ML18219B5661978-08-0808 August 1978 Letter from Indiana & Michigan Power Co to NRC Submitting Licensee Event Report (RO 78-050/03L-0) 2024-09-12
[Table view] |
LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage |
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Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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3162024003R00 - NRC Website |
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INDIANA MICHIGAN POWIR-An MP Company BOUNDLESS ENERGY-August 22, 2024 Docket No.: 50-316 U. S. Nuclear Regulatory Commission A TIN: Document Control Desk 11555 Rockville Pike Rockville, MD 20852 Donald C. Cook Nuclear Plant Unit 2 LICENSEE EVENT REPORT 316/2024-003-00 Indiana Michigan Power Cook Nuclear Plant One Cook Place Bridgman, Ml 49106 indianamichiganpower.com AEP-NRC-2024-66 10 CFR 50.73 Unit 2 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage In accordance with 10 CFR 50. 73, Licensee Event Report (LER) System, Indiana Michigan Power Company, the licensee for Donald C. Cook Nuclear Plant Unit 2, is submitting as an enclosure to this letter the following report:
LER 316/2024-003-00: Unit 2 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage There are no commitments contained in this submittal.
Should you have any questions, please contact Mr. Michael K. Scarpello, Regulatory Affairs Director, at (269) 466-2649.
Sincerely,
~t~
Kelly J. Ferneau Site Vice President MPH/kmh Enclosure:
Licensee Event Report 316/2024-003-00: Unit 2 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage
U.S. Nuclear Regulatory Commission Page 2 c:
EGLE - RMD/RPS J. B. Giessner -- NRC Region Ill NRC Resident Inspector N. Quilico -- MPSC R. M. Sistevaris -- AEP Ft. Wayne S. P. Wall, NRC Washington D.C.
A. J. Williamson -- AEP Ft. Wayne AEP-NRC-2024-66
Enclosure to AEP-NRC-2024-66 Licensee Event Report 316/2024-003-00: Unit 2 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage
Abstract
On June 27, 2024, at 0803 hours0.00929 days <br />0.223 hours <br />0.00133 weeks <br />3.055415e-4 months <br /> EDT, a Unit 2 shutdown was completed in accordance with Technical Specification (TS) 3.4.13, Reactor Coolant System (RCS) Operational Leakage, Condition C. On June 26, 2024, at 2303 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.762915e-4 months <br />, a packing leak developed on 2-QRV-251,
Chemical Volume & Control System (CVCS) Charging Pumps Discharge Flow Control Valve, which was determined to be greater than the 10 gallons per minute (gpm) limit per TS. The packing for 2-QRV-251 was replaced and the valve was returned to service.
Following the manual Unit 2 Reactor Trip, per normal plant shutdown operating procedures, at approximately 17 percent(%) power, the Unit 2 Turbine Driven Auxiliary Feedwater Pump (TDAFP) automatically started when two steam generator levels reached less than the low-low setpoint.
)
The completion of the plant shutdown required by TS is reportable as a License~ Event Report (LER) in accordance with 10CFR 50.73(a)(2 (i)
(A) and the Unit 2 TDAFP Auto Start is reportable in accordance with 10CFR 50.73(a)(2)(iv)(A).
I EVENT DESCRIPTION
- 2. DOCKET NUMBER
- 3. LER NUMBER I
00316 NUMBER NO.
I YEAR SEQUENTIAL REV
~-,
003 1-0 On June 27, 2024, at 0803 hours0.00929 days <br />0.223 hours <br />0.00133 weeks <br />3.055415e-4 months <br /> EDT, a Unit 2 shutdown was completed in accordance with Technical Specification (TS) 3.4.13, Reactor Coolant System (RCS) [AB] Operational Leakage, Condition C. On June 26, 2024, at 2302 hours0.0266 days <br />0.639 hours <br />0.00381 weeks <br />8.75911e-4 months <br /> EDT, with Unit 2 operating in Mode 1 at 100 percent (%) power, a packing leak developed on 2-QRV-251, Chemical Volume & Control System (CVCS) [CB] Charging Pumps Discharge Flow Control Valve [FCV]. The leak rate was determined, through monitoring by Control Room operators, to be approximately 11.8 gallons per minute (gpm) and not repairable at power.
Since this leak rate was greater than the 10 gpm limit allowed per TS 3.4.13 for identified leakage, TS 3.4.13, Condition B, was entered, which requires RCS Operational Leakage to be reduced to within limits in four (4) hours or less. Subsequently, on June 27, 2024, at 0302 hours0.0035 days <br />0.0839 hours <br />4.993386e-4 weeks <br />1.14911e-4 months <br />, TS 3.4.13, Condition C, was entered when the required action of Condition B, could not be met. Condition C requires Unit 2 to be shutdown to MODE 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and MODE 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
At 0159 hours0.00184 days <br />0.0442 hours <br />2.628968e-4 weeks <br />6.04995e-5 months <br />, Operators commenced a shutdown of Unit 2 in accordance with the Power Reduction Procedure due to the identified RCS leak. At 0803 hours0.00929 days <br />0.223 hours <br />0.00133 weeks <br />3.055415e-4 months <br />, Unit 2 was manually tripped from 17% power, in accordance with normal operating procedures. All required equipment operated as expected following the reactor trip.
Following the manual Unit 2 Reactor Trip, the Unit 2 Turbine Driven Auxiliary Feedwater Pump (TDAFP) automatically started when two steam generator levels reached less than the low-low setpoint, The completion of the plant shutdown required by TS is reportable as a Licensee Event Report (LER) in accordance with 1 0CFR 50. 73(a)(2)(i)(A) and the Unit 2 TDAFP Auto Start is reportable as an LER in accordance with 1 0CFR 50. 73(a)(2)(iv)
(A).
COMPONENT 2-QRV-251, eves CHARGING PUMPS DISCHARGE FLOW CONTROL VALVE with Chesterton 5800 packing.
CAUSE OF THE EVENT The direct cause of the leak was determined to be a packing failure, within 2-QRV-251, that resulted in a leak rate of approximately 11.8 gpm. An Apparant Cause Evaluation (ACE) is in progress at the time of the writing of this LER. If the ACE reveals further insights or causes different than described in this LER, a supplement will be provided.
CORRECTIVE ACTIONS 2-QRV-251 was repacked with a replacement Chesterton 5800 packing set and returned to service.
ASSESSMENT OF SAFETY CONSEQUENCES NUCLEAR SAFETY
- 2. DOCKET NUMBER
- 3. LER NUMBER I
00316 NUMBER NO.
I YEAR SEQUENTIAL REV
~-I 003 1-0 The approximately 11.8 gpm leak rate from 2-QRV-251 was significantly less than the makeup capacity of the CVCS Charging Pump and there was no actual or potential nuclear safety hazard resulting from the 2-QRV-251 packing failure.
INDUSTRIAL SAFETY There was no actual or potential industrial safety hazard resulting from the 2-QRV-251 packing failure.
RADIOLOGICAL SAFETY There was no actual or potential radiological safety hazard resulting from the 2-QRV-251 packing failure. This event was of minimal significance to the health and safety of the public.
PROBABILISTIC RISK ASSESSMENT A Probabilistic Risk Assessment risk evaluation was performed to determine the safety significance of the leak and ensuing shutdown. The automatic start of the Unit 2 TDAFP did not adversely affect the shutdown and was not factored into the evaluation.
The safety significance can be estimated by calculating the Conditional Core Damage Probability (CCDP) and the Conditional Large Early Release Probability (CLE RP) of the transient initiating event. A comparison of the calculated CCDP and CLERP estimates to regulatory guidance resulted in the conclusion that this event was of very low safety significance.
PREVIOUS SIMILAR EVENTS A review of LERs for the past five years found one similar event. On May 1, 2020, at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br />, a Unit 2 shutdown, due to exceeding TS 3.4.13 RCS Operational Leakage limits, was completed and reported under LER 316/2020-002-00. The cause of that leak was determined to be a bellows failure within 2-NRV-163, Reactor Coolant Loop #3 to Pressurizer Spray Control Valve, that resulted in a failure of the 0.5 inch welded telltale line for 2-NRV-163. This event is similar in that both events involved RCS Operational Leakage limits being exceeded. The event was different in that the leak on 2-QRV-251 was due to the packing failure. Page 3
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