Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick: Difference between revisions

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{{#Wiki_filter:UNITED STATESNUCLEAR REGULATORY COMMISSIONOFFICE OF NUCLEAR REACTOR REGULATIONWASHINGTON, D.C. 20555-0001May 5, 1999NRC INFORMATION NOTICE 99-14: UNANTICIPATED REACTOR WATER DRAINDOWNAT QUAD CITIES UNIT 2, ARKANSAS NUCLEAR ONEUNIT 2, AND FITZPATRICK
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY
 
COMMISSION
 
===OFFICE OF NUCLEAR REACTOR REGULATION===
WASHINGTON, D.C. 20555-0001 May 5, 1999 NRC INFORMATION
 
NOTICE 99-14: UNANTICIPATED
 
REACTOR WATER DRAINDOWN AT QUAD CITIES UNIT 2, ARKANSAS NUCLEAR ONE UNIT 2, AND FITZPATRICK


==Addressees==
==Addressees==
Line 20: Line 29:


==Purpose==
==Purpose==
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alertaddressees to the potential for personnel errors during infrequently performed evolutions thatresult in, or contribute to, events such as the inadvertent draining of water from the reactorvessel during shutdown operations. It is expected that recipients will review the information forapplicability to their facilities and consider actions, as appropriate, to prevent a similaroccurrence. However, suggestions contained in this information notice are not NRCrequirements; therefore, no specific action or written response to this notice is required.DescriDtion of CircumstancesQuad Cities Unit 2On February 24, 1999, Quad Cities Unit 2 was in cold shutdown with reactor water temperatureat 131 'F and reactor water level at 80 inches indicated level (normal level during operations is30 inches indicated or 173 inches above the top of active fuel [TAF]). Core cooling was beingmaintained in a band of 120 'F to 170 OF by the OA" loop of the shutdown cooling mode of theresidual heat removal (RHR) system after being switched from the nB" loop at 12:32 a.m.During the switch over the licensee inadvertently failed to close the OA RHR minimum flowvalve as required by the procedure. Sometime later operators noted a decreasing reactor waterlevel and at about 1:02 a.m. secured the *2A RHR pump and isolated shutdown cooling. At1:55 a.m. operators restored the *2A' loop of shutdown cooling to the proper lineup and startedthe *2A RHR pump. Water level had decreased to a minimum of about 45 inches indicated,and reactor water temperature had risen to a maximum of about 163 OF. Forced circulation ofreactor vessel water using a reactor recirculation pump remained in effect throughout the event.On the basis of post event reviews, It appears that the minimum flow valve in the OA loop wasleft open because the nuclear station operator failed to ensure that the tasks were performed inthe sequence specified in the operating procedures. The nuclear station operator who was(7008 PD(L H ort<<4qj-Oiif qqos(J5C7FfcjANW\\b
The U.S. Nuclear Regulatory
 
Commission (NRC) is issuing this information
 
notice to alert addressees
 
to the potential
 
for personnel
 
errors during infrequently
 
performed
 
evolutions
 
that result in, or contribute
 
to, events such as the inadvertent
 
draining of water from the reactor vessel during shutdown operations.
 
It is expected that recipients
 
will review the information
 
for applicability
 
to their facilities
 
and consider actions, as appropriate, to prevent a similar occurrence.
 
However, suggestions
 
contained
 
in this information
 
notice are not NRC requirements;  
therefore, no specific action or written response to this notice is required.DescriDtion
 
of Circumstances
 
Quad Cities Unit 2 On February 24, 1999, Quad Cities Unit 2 was in cold shutdown with reactor water temperature
 
at 131 'F and reactor water level at 80 inches indicated
 
level (normal level during operations
 
is 30 inches indicated
 
or 173 inches above the top of active fuel [TAF]). Core cooling was being maintained
 
in a band of 120 'F to 170 OF by the OA" loop of the shutdown cooling mode of the residual heat removal (RHR) system after being switched from the nB" loop at 12:32 a.m.During the switch over the licensee inadvertently
 
failed to close the OA RHR minimum flow valve as required by the procedure.
 
Sometime later operators
 
noted a decreasing
 
reactor water level and at about 1:02 a.m. secured the *2A RHR pump and isolated shutdown cooling. At 1:55 a.m. operators
 
restored the *2A' loop of shutdown cooling to the proper lineup and started the *2A RHR pump. Water level had decreased
 
to a minimum of about 45 inches indicated, and reactor water temperature
 
had risen to a maximum of about 163 OF. Forced circulation
 
of reactor vessel water using a reactor recirculation
 
pump remained in effect throughout
 
the event.On the basis of post event reviews, It appears that the minimum flow valve in the OA loop was left open because the nuclear station operator failed to ensure that the tasks were performed
 
in the sequence specified
 
in the operating
 
procedures.
 
The nuclear station operator who was (7008 PD(L H ort<<4qj-Oiif
 
qqos(J5 C7Ffcj ANW\\b
 
IN 99-14 May 5, 1999 directing
 
the evolution
 
from the control room gave the non-licensed
 
operator permission
 
to de-energize the breaker for the WA RHR minimum flow valve operator before the valve was taken to the required closed position.
 
De-energizing
 
the breaker also removed power to the valve position indicator
 
lights in the control room. Thus, when the nuclear station operator tried to verify that the valve was closed, there was no position indication
 
in the control room to make that verification.
 
The nuclear station operator made the incorrect
 
assumption
 
that the valve was already closed and moved to the next step in the procedure.
 
This failure to close the WAX RHR minimum flow valve opened a drain path from the reactor to the suppression
 
pool. To further complicate
 
the event, the operating
 
crew did not recognize
 
that there was any problem until approximately
 
10 minutes had passed and the water level had decreased
 
about 13 inches because of a misinterpretation
 
of causes of the level decrease.
 
After detecting
 
the decrease, the operating
 
crew was slow to react, which allowed the level to decrease another 20 inches before the operators
 
isolated shutdown cooling which terminated
 
the draindown.
 
The licensee estimated
 
that a total of 6000 to 7000 gallons was drained from the reactor to the suppression
 
pool.Operations
 
staff practices
 
including
 
poor communications, poor activity briefings
 
for high-risk activities, lack of effective
 
pre-shift
 
briefings, inadequate
 
supervision
 
of important
 
control room activities, inadequate
 
monitoring
 
of control room panels, and slow event response may have contributed
 
to the event. Although the unintended
 
loss of inventory
 
to the suppression
 
pool highlighted
 
significant
 
weaknesses
 
in plant operations, the safety significance
 
was minimized
 
by two features.
 
First, a reactor recirculation
 
pump remained in service throughout
 
the event which served to distribute
 
decay heat. Second, an automatic
 
isolation
 
of shutdown cooling would have occurred at 8 inches indicated
 
level which would have stopped the draining event.An indicated
 
water level of 8 inches corresponds
 
to approximately
 
151 inches of water level above the TAF in the reactor core.Arkansas Nuclear One Unit 2 On February 2, 1999, at Arkansas Nuclear One Unit 2, the operators
 
were draining the refueling
 
canal in preparation
 
for installing
 
the reactor vessel head. Refueling
 
was complete and steam generator
 
nozzle dams were installed.
 
The operators
 
were using the two low pressure safety injection (LPSI) pumps to drain the canal to the refueling
 
water storage tank;one pump also served as the shutdown cooling pump. The rate of draindown
 
was approximately
 
3.3 Inches per minute. When the water level reached 105 inches, the reactor operator noted that level started to lower rapidly. Operators
 
stopped one of the LPSI pumps and instructed
 
a local operator to close the isolation
 
valve to the refueling
 
water tank. This manually operated valve required 55 turns of the handwheel
 
to fully close. Within approximately
 
1.5 minutes, the reactor vessel level had dropped below the 65 inch level (where reduced inventory
 
begins) and continued
 
down to 56 inches before the valve could be fully closed. (Reference
 
zero on these level instruments
 
is the bottom of the hot leg, with mid-loop being defined at approximately
 
24 inches.) The average rate of level decrease between 105 IN 99-14 May 5, 1999 inches and 56 inches was approximately
 
33 inches per minute. At its lowest level, 56 inches indicated, there were still 93 inches of water above the TAF. Using the high pressure safety injection (HPSI) pump the operators
 
brought the level back up to 90 inches. The plant was in reduced inventory
 
operations (below 65 inches) for approximately
 
7 minutes. During the event the level remained well above the point where LPSI pump cavitation
 
would be expected.
 
The licensee concluded
 
that the safety significance
 
of the event was minimal because multiple sources of makeup water were available, redundant
 
mitigation
 
equipment
 
was available, and the operators
 
were quick to recognize
 
and respond to the event.On the basis of post event reviews, it was determined
 
that the procedure
 
used for draining down the refueling
 
canal was inadequate
 
in that it incorrectly
 
stated that the draindown
 
should be secured at the 90-inch level. The procedure
 
should have directed that the rate of draining be secured at the 106-inch level so that appropriate
 
precautions
 
could be taken before resuming the draindown.
 
These precautions
 
should have Included reminders
 
to the operating crew that below the 106-inch level the level will drop much more quickly due to the transition
 
of pumping from a large volume in the refueling
 
canal to a small volume In the reactor vessel.Therefore, in order to maintain control of the water level, the draindown
 
rate should be decreased
 
and an operator should be stationed
 
to directly monitor the level.Additional
 
factors that contributed
 
to this event include: the operators
 
received little specific training on this evolution;
the crew was inexperienced
 
in performing
 
this task; the task should have been classified
 
as an infrequent
 
task requiring
 
a more thorough briefing;
and, operators failed to station an operator in a position where he could directly monitor the water level in the refueling
 
canal. Instead they monitored
 
it remotely using a video camera that did not provide a clear picture of the water level.FitzPatrick
 
On December 2, 1998, at the James A. FitzPatrick
 
Nuclear Power Plant, the operators
 
were in the process of reassembling
 
the reactor following
 
refueling.
 
Operators
 
were controlling
 
the reactor vessel water level at 357 inches above TAF by adjusting
 
the water discharge
 
rate to compensate
 
for the constant input from the control rod drive cooling water system. While in this condition, the licensees
 
risk analysis requires that reactor vessel water level be monitored
 
using two independent
 
level indicators.
 
To meet this requirement, the licensee designated
 
a wide range indicator
 
which provided Indication
 
up to the top of the reactor vessel and an RHR interlock
 
level indicator
 
which provided indication
 
in the range from -150 inches to +200 Inches as the instruments
 
to be used during this evaluation.
 
In order for the wide-range
 
level Indicator
 
to remain available
 
with the reactor head removed, a temporary
 
standpipe
 
and fill funnel were used to replace a portion of the reference
 
leg. At the time of the event, the licensee was in the process of removing this temporary
 
standpipe
 
and reinstalling
 
the original reference
 
leg components.
 
As the water drained from the standpipe, it caused the wide-range
 
level indicator
 
to erroneously
 
show an increasing
 
water level. For a period of approximately
 
one hour the operators
 
in the control room, unaware that the ongoing maintenance
 
would cause an error in the indicated
 
water level, compensated
 
for the apparent increasing
 
level by increasing
 
the discharge
 
rate. This action had the effect of reducing the
 
IN 99-14 May 5, 1999 actual water level from 357 inches to 255 inches. During the same time period, the operators were also in the process of filling and venting the reactor feedwater
 
piping, which could have affected the reactor water level. Once the normal reference
 
leg piping had been reinstalled
 
and the reference
 
leg began to refill, the indicated
 
level decreased
 
from 357 inches to the actual level of 255 inches. The second level instrument, which does not come on-scale until the level goes below 200 inches, remained off-scale
 
high.When operators
 
discovered
 
the level discrepancy, they used a temporary
 
pressure gauge connected
 
to the reactor vessel low-point
 
tap to confirm the actual water level. After confirming
 
the accuracy of the wide-range
 
indicator, they restored the reactor vessel water level to 357 inches. The 100-inch error represented
 
approximately
 
14,000 gallons of water. The licensee determined
 
that the safety significance
 
of this event was low since the reactor was in cold shutdown with low decay heat and the reactor water level remained well above the TAF. In addition, the drain-down
 
would have been limited by an automatic
 
Isolation
 
of the draindown path, which would have occurred prior to vessel level reaching 177 Inches above the TAF.The licensee's
 
post event review identified:
weaknesses
 
in the operator's
 
knowledge
 
of the reactor assembly process; lack of explicit detail in the reactor assembly procedure;
and, weaknesses
 
in the plant risk assessment
 
process. Contrary to the assumption
 
that two designated
 
reactor water level indicators
 
were available, only one indicator, the wide-range
 
instrument, was available
 
in the range above 200 inches. When the reference
 
leg on the wide-range instrument
 
was disassembled
 
and drained, the one usable indicator
 
was rendered unavailable.
 
The second instrument
 
was pegged off-scale
 
high and remained that way throughout
 
the event because the level never dropped below 200 inches. A post event review by the licensee indicated
 
that other reactor water level instruments, remained operable during the event but, apparently
 
the operators
 
did not rely on these other instruments
 
or notice the discrepancy
 
between them and the wide range Indicator.
 
Proposed corrective
 
actions included procedural
 
enhancements
 
to ensure that reactor level instrumentation
 
credited by the outage risk assessment
 
remains available
 
during reactor disassembly
 
and reassembly.
 
Discussion
 
Personnel
 
errors appear to have caused, or contributed
 
to, these three inadvertent
 
reactor vessel draindown
 
events. The likelihood
 
of personnel
 
errors is dependent
 
upon the operators knowledge
 
of the task gained through previous experience
 
and training.
 
It is also dependent upon the quality of the procedures
 
used to perform the task, the level of supervision, the adequacy of pre-job briefings, fatigue, and distractions
 
resulting
 
from multiple tasks. In each of the events, the plant staff made errors during a seldom-performed
 
evolution.
 
Because it was a seldom-performed
 
evolution, more training, better pre-job briefings, closer supervision, and procedures
 
that contain more details than those for frequently
 
performed
 
activities
 
might have prevented
 
these events.
 
IN 99-14 May 5, 1999 This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact the technical
 
contact listed below, the appropriate
 
regional office, or the appropriate
 
Office of Nuclear Reactor Regulation (NRR)project manager.Ledyard B. Marsh, Chief Events Assessment, Generic Communications
 
And Non-Power
 
Reactors Branch Division of Regulatory
 
Improvement
 
===Programs Office of Nuclear Reactor Regulation===
Technical
 
contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdDRenrc.aov
 
REFERENCES:
NRC Integrated
 
Inspection
 
Report No. 50-333/98-08, issued February 10, 1999 (Accession
 
No.9902170348)
for the James A. FitzPatrick
 
Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachment:
List of Recently Issued NRC Information
 
Notices
 
~~ Attachment
 
1 IN 99-14 May 5, 1999 Page 1 of I LIST OF RECENTLY ISSUED NRC INFORMATION
 
NOTICES Information
 
Date of Notice No. Subject Issuance Issued to 99-13 Insiahts from NRR Inspections
 
4129199 All holders of operatina
 
licenses of Low-and Medium-Voltage
 
===Circuit Breaker Maintenance===
Programs for nuclear power reactors 99-12 Year 2000 Computer Systems Readiness
 
Audits Incidents
 
Involving
 
the Use of Radioactive
 
Iodine-131
4/28/99 4/23/99 All holders of operating
 
licenses or construction
 
permits for nuclear power plants All medical use licensees 99-11 97-15, Sup 1 Reporting
 
of Errors and 4/16/99 Changes in Large-Break/Small- Break Loss-of-Coolant
 
Evaluation
 
Models of Fuel Vendors and Compliance
 
with 10 CFR 50.46(a)(3)
All holders of operating
 
licenses for nuclear power reactors, except those who have permanently
 
cease operations
 
and have certified
 
that fuel has been permanently
 
removed from the reactor 99-10 99-09 Degradation
 
of Prestressing
 
4/13/99 Tendon Systems in Prestressed
 
===Concrete Containments===
Problems Encountered
 
When 3/24/99 Manually Editing Treatment
 
Data on The Nucletron
 
Microselectron-HDR (New) Model 105.999 Urine Specimen Adulteration
 
4/1/99 All holders of operating
 
licenses for nuclear power reactors All medical licensees
 
authorized
 
to conduct high-dose-rate (HDR)remote after loading brachytherapy
 
treatments
 
All holders of operating
 
licensees for nuclear power reactors and licensees
 
authorized
 
to possess or use formula quantities
 
of strategic
 
special nuclear material 99-08 OL = Operating
 
License CP = Construction
 
Permit
 
IN 99-xx April xx, 1999 Page 5of 5 This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact the technical
 
contact listed below, the appropriate
 
regional office, or the appropriate
 
office of Nuclear Reactor Regulation (NRR)Project Manager.Ledyard B. Marsh, Chief Events Assessment, Generic Communications
 
And Non-Power
 
Reactors Branch Division of Regulatory
 
Improvement
 
===Programs Office of Nuclear Reactor Regulation===
Technical
 
contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdRDanrc.aov
 
REFERENCES:
NRC Integrated
 
Inspection
 
Report No. 50-333198-08, issued February 10, 1999 (Accession
 
No.9902170348)
for the James A. FitzPatrick
 
Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachments:
1. List of Recently Issued NMSS Information
 
Notices 2. List of Recently Issued NRC Information
 
Notices DOCUMENT NAME: G:ICDPDRAININ\DRAIN.0B.WPD
 
To receive a copy of this document, Indicate In the box C=Copy w/o attachmentlenclosure
 
E=Copy with attachment/enclosure
 
N = No copy OFFICE PECB:DRIP
 
I Tech Editor l DRCH I PDIV-1 I NAME CPetrone I_ RGallo 1 MNolangfarP.
 
DATE V /0199 [3 /1/99 4 /4I9 1' /0g99 F .V. ...OFFICE PDI-1 IA .I PDIII-2 I C:PECB:DRIP
 
I NAME 2 Jiiam RPulsjier
 
LMarsh DATE lf/499 I1'/t 99 I /99 OFFICIAL RECORD COPY
 
IN 99-14 May 5, 1999 This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact the technical
 
contact listed below, the appropriate
 
regional office, or the appropriate
 
Office of Nuclear Reactor Regulation (NRR)project manager.[arig sjid by]Ledyard B. Marsh, Chief Events Assessment, Generic Communications
 
And Non-Power
 
Reactors Branch Division of Regulatory
 
Improvement
 
===Programs Office of Nuclear Reactor Regulation===
Technical
 
contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdr)ODnrc.gov
 
REFERENCES:
NRC Integrated
 
Inspection
 
Report No. 50-333/98-08, issued February 10, 1999 (Accession
 
No.9902170348)
for the James A. FitzPatrick
 
Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachment:
List of Recently Issued NRC Information
 
Notices DOCUMENT NAME: S:XDRPMSEC\99-14.IN
 
*See previous concurrence


IN 99-14May 5, 1999 directing the evolution from the control room gave the non-licensed operator permission to de-energize the breaker for the WA RHR minimum flow valve operator before the valve was takento the required closed position. De-energizing the breaker also removed power to the valveposition indicator lights in the control room. Thus, when the nuclear station operator tried toverify that the valve was closed, there was no position indication in the control room to makethat verification. The nuclear station operator made the incorrect assumption that the valve wasalready closed and moved to the next step in the procedure. This failure to close the WAX RHRminimum flow valve opened a drain path from the reactor to the suppression pool. To furthercomplicate the event, the operating crew did not recognize that there was any problem untilapproximately 10 minutes had passed and the water level had decreased about 13 inchesbecause of a misinterpretation of causes of the level decrease. After detecting the decrease,the operating crew was slow to react, which allowed the level to decrease another 20 inchesbefore the operators isolated shutdown cooling which terminated the draindown. The licenseeestimated that a total of 6000 to 7000 gallons was drained from the reactor to the suppressionpool.Operations staff practices including poor communications, poor activity briefings for high-riskactivities, lack of effective pre-shift briefings, inadequate supervision of important control roomactivities, inadequate monitoring of control room panels, and slow event response may havecontributed to the event. Although the unintended loss of inventory to the suppression poolhighlighted significant weaknesses in plant operations, the safety significance was minimized bytwo features. First, a reactor recirculation pump remained in service throughout the eventwhich served to distribute decay heat. Second, an automatic isolation of shutdown coolingwould have occurred at 8 inches indicated level which would have stopped the draining event.An indicated water level of 8 inches corresponds to approximately 151 inches of water levelabove the TAF in the reactor core.Arkansas Nuclear One Unit 2On February 2, 1999, at Arkansas Nuclear One Unit 2, the operators were draining therefueling canal in preparation for installing the reactor vessel head. Refueling was completeand steam generator nozzle dams were installed. The operators were using the two lowpressure safety injection (LPSI) pumps to drain the canal to the refueling water storage tank;one pump also served as the shutdown cooling pump. The rate of draindown wasapproximately 3.3 Inches per minute. When the water level reached 105 inches, the reactoroperator noted that level started to lower rapidly. Operators stopped one of the LPSI pumpsand instructed a local operator to close the isolation valve to the refueling water tank. Thismanually operated valve required 55 turns of the handwheel to fully close. Withinapproximately 1.5 minutes, the reactor vessel level had dropped below the 65 inch level (wherereduced inventory begins) and continued down to 56 inches before the valve could be fullyclosed. (Reference zero on these level instruments is the bottom of the hot leg, with mid-loopbeing defined at approximately 24 inches.) The average rate of level decrease between 105 IN 99-14May 5, 1999 inches and 56 inches was approximately 33 inches per minute. At its lowest level, 56 inchesindicated, there were still 93 inches of water above the TAF. Using the high pressure safetyinjection (HPSI) pump the operators brought the level back up to 90 inches. The plant was inreduced inventory operations (below 65 inches) for approximately 7 minutes. During the eventthe level remained well above the point where LPSI pump cavitation would be expected. Thelicensee concluded that the safety significance of the event was minimal because multiplesources of makeup water were available, redundant mitigation equipment was available, andthe operators were quick to recognize and respond to the event.On the basis of post event reviews, it was determined that the procedure used for drainingdown the refueling canal was inadequate in that it incorrectly stated that the draindown shouldbe secured at the 90-inch level. The procedure should have directed that the rate of drainingbe secured at the 106-inch level so that appropriate precautions could be taken beforeresuming the draindown. These precautions should have Included reminders to the operatingcrew that below the 106-inch level the level will drop much more quickly due to the transition ofpumping from a large volume in the refueling canal to a small volume In the reactor vessel.Therefore, in order to maintain control of the water level, the draindown rate should bedecreased and an operator should be stationed to directly monitor the level.Additional factors that contributed to this event include: the operators received little specifictraining on this evolution; the crew was inexperienced in performing this task; the task shouldhave been classified as an infrequent task requiring a more thorough briefing; and, operatorsfailed to station an operator in a position where he could directly monitor the water level in therefueling canal. Instead they monitored it remotely using a video camera that did not provide aclear picture of the water level.FitzPatrickOn December 2, 1998, at the James A. FitzPatrick Nuclear Power Plant, the operators were inthe process of reassembling the reactor following refueling. Operators were controlling thereactor vessel water level at 357 inches above TAF by adjusting the water discharge rate tocompensate for the constant input from the control rod drive cooling water system. While in thiscondition, the licensees risk analysis requires that reactor vessel water level be monitored usingtwo independent level indicators. To meet this requirement, the licensee designated a widerange indicator which provided Indication up to the top of the reactor vessel and an RHRinterlock level indicator which provided indication in the range from -150 inches to +200 Inchesas the instruments to be used during this evaluation.In order for the wide-range level Indicator to remain available with the reactor head removed, atemporary standpipe and fill funnel were used to replace a portion of the reference leg. At thetime of the event, the licensee was in the process of removing this temporary standpipe andreinstalling the original reference leg components. As the water drained from the standpipe, itcaused the wide-range level indicator to erroneously show an increasing water level. For aperiod of approximately one hour the operators in the control room, unaware that the ongoingmaintenance would cause an error in the indicated water level, compensated for the apparentincreasing level by increasing the discharge rate. This action had the effect of reducing the
To receive a copy of this document.


IN 99-14May 5, 1999 actual water level from 357 inches to 255 inches. During the same time period, the operatorswere also in the process of filling and venting the reactor feedwater piping, which could haveaffected the reactor water level. Once the normal reference leg piping had been reinstalled andthe reference leg began to refill, the indicated level decreased from 357 inches to the actuallevel of 255 inches. The second level instrument, which does not come on-scale until the levelgoes below 200 inches, remained off-scale high.When operators discovered the level discrepancy, they used a temporary pressure gaugeconnected to the reactor vessel low-point tap to confirm the actual water level. After confirmingthe accuracy of the wide-range indicator, they restored the reactor vessel water level to 357inches. The 100-inch error represented approximately 14,000 gallons of water. The licenseedetermined that the safety significance of this event was low since the reactor was in coldshutdown with low decay heat and the reactor water level remained well above the TAF. Inaddition, the drain-down would have been limited by an automatic Isolation of the draindownpath, which would have occurred prior to vessel level reaching 177 Inches above the TAF.The licensee's post event review identified: weaknesses in the operator's knowledge of thereactor assembly process; lack of explicit detail in the reactor assembly procedure; and,weaknesses in the plant risk assessment process. Contrary to the assumption that twodesignated reactor water level indicators were available, only one indicator, the wide-rangeinstrument, was available in the range above 200 inches. When the reference leg on the wide-range instrument was disassembled and drained, the one usable indicator was renderedunavailable. The second instrument was pegged off-scale high and remained that waythroughout the event because the level never dropped below 200 inches. A post event review bythe licensee indicated that other reactor water level instruments, remained operable during theevent but, apparently the operators did not rely on these other instruments or notice thediscrepancy between them and the wide range Indicator. Proposed corrective actions includedprocedural enhancements to ensure that reactor level instrumentation credited by the outagerisk assessment remains available during reactor disassembly and reassembly.DiscussionPersonnel errors appear to have caused, or contributed to, these three inadvertent reactorvessel draindown events. The likelihood of personnel errors is dependent upon the operatorsknowledge of the task gained through previous experience and training. It is also dependentupon the quality of the procedures used to perform the task, the level of supervision, theadequacy of pre-job briefings, fatigue, and distractions resulting from multiple tasks. In each ofthe events, the plant staff made errors during a seldom-performed evolution. Because it was aseldom-performed evolution, more training, better pre-job briefings, closer supervision, andprocedures that contain more details than those for frequently performed activities might haveprevented these events.
indicate in the box C=CoDv w/o attachment/enclosure


IN 99-14May 5, 1999 This information notice requires no specific action or written response. If you have anyquestions about the information in this notice, please contact the technical contact listed below,the appropriate regional office, or the appropriate Office of Nuclear Reactor Regulation (NRR)project manager.Ledyard B. Marsh, ChiefEvents Assessment, Generic CommunicationsAnd Non-Power Reactors BranchDivision of Regulatory Improvement ProgramsOffice of Nuclear Reactor RegulationTechnical contact: Chuck Petrone, NRR301-415-1027E-mail: cdDRenrc.aovREFERENCES:NRC Integrated Inspection Report No. 50-333/98-08, issued February 10, 1999 (Accession No.9902170348) for the James A. FitzPatrick Nuclear Power Plant for the period November 22,1998, through January 10, 1999.Attachment: List of Recently Issued NRC Information Notices
E=CoDv with attachment/enclosure


~~ Attachment 1IN 99-14May 5, 1999Page 1 of ILIST OF RECENTLY ISSUEDNRC INFORMATION NOTICESInformation Date ofNotice No. Subject Issuance Issued to99-13 Insiahts from NRR Inspections 4129199 All holders of operatina licensesof Low-and Medium-VoltageCircuit Breaker MaintenanceProgramsfor nuclear power reactors99-12Year 2000 Computer SystemsReadiness AuditsIncidents Involving the Use ofRadioactive Iodine-1314/28/994/23/99All holders of operating licensesor construction permits for nuclearpower plantsAll medical use licensees99-1197-15, Sup 1Reporting of Errors and 4/16/99Changes in Large-Break/Small-Break Loss-of-Coolant EvaluationModels of Fuel Vendors andCompliance with 10 CFR 50.46(a)(3)All holders of operating licensesfor nuclear power reactors, exceptthose who have permanentlycease operations and havecertified that fuel has beenpermanently removed from thereactor99-1099-09Degradation of Prestressing 4/13/99Tendon Systems in PrestressedConcrete ContainmentsProblems Encountered When 3/24/99Manually Editing Treatment Dataon The Nucletron Microselectron-HDR(New) Model 105.999Urine Specimen Adulteration 4/1/99All holders of operating licensesfor nuclear power reactorsAll medical licensees authorizedto conduct high-dose-rate (HDR)remote after loadingbrachytherapy treatmentsAll holders of operating licenseesfor nuclear power reactors andlicensees authorized to possessor use formula quantities ofstrategic special nuclear material99-08OL = Operating LicenseCP = Construction Permit
N = No coov OFFICE PECB:DRlIP


IN 99-xxApril xx, 1999Page 5of 5This information notice requires no specific action or written response. If you have anyquestions about the information in this notice, please contact the technical contact listed below,the appropriate regional office, or the appropriate office of Nuclear Reactor Regulation (NRR)Project Manager.Ledyard B. Marsh, ChiefEvents Assessment, Generic CommunicationsAnd Non-Power Reactors BranchDivision of Regulatory Improvement ProgramsOffice of Nuclear Reactor RegulationTechnical contact:Chuck Petrone, NRR301-415-1027E-mail: cdRDanrc.aovREFERENCES:NRC Integrated Inspection Report No. 50-333198-08, issued February 10, 1999 (Accession No.9902170348) for the James A. FitzPatrick Nuclear Power Plant for the period November 22,1998, through January 10, 1999.Attachments:1. List of Recently Issued NMSS Information Notices2. List of Recently Issued NRC Information NoticesDOCUMENT NAME: G:ICDPDRAININ\DRAIN.0B.WPDTo receive a copy of this document, Indicate In the box C=Copy w/o attachmentlenclosure E=Copy with attachment/enclosure N = No copyOFFICE PECB:DRIP I Tech Editor l DRCH I PDIV-1 INAME CPetrone I_ RGallo 1 MNolangfarP.DATE V /0199 [3 /1/99 4 /4I9 1' /0g99F .V. ...OFFICEPDI-1 IA .IPDIII-2IC:PECB:DRIPINAME 2Jiiam RPulsjier LMarshDATE lf/499 I1'/t 99 I /99OFFICIAL RECORD COPY
I Tech Editor l DRCH l-ii PDIV-1 lI NAME CPetrone*
BCalure* RGallo* MNolan*DATE 04/27/99 .3/15/99 _________04128199
= 04/27/99 1 ...OFFICE PDI-1 I PD111-2 C:PECB:DJRIP


IN 99-14May 5, 1999 
I NAME JWilliams*
}}
RPulsifer'
I-Marsh _ _ __ _DATE 04/27/9 .04/27/99 k,-u99 OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Revision as of 14:13, 31 August 2018

Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick
ML031040444
Person / Time
Site: Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant  Entergy icon.png
Issue date: 05/05/1999
From: Marsh L B
Division of Regulatory Improvement Programs
To:
References
IN-99-014, NUDOCS 9905070080
Download: ML031040444 (8)


UNITED STATES NUCLEAR REGULATORY

COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001 May 5, 1999 NRC INFORMATION

NOTICE 99-14: UNANTICIPATED

REACTOR WATER DRAINDOWN AT QUAD CITIES UNIT 2, ARKANSAS NUCLEAR ONE UNIT 2, AND FITZPATRICK

Addressees

All holders of licenses for nuclear power, test, and research reactors.

Purpose

The U.S. Nuclear Regulatory

Commission (NRC) is issuing this information

notice to alert addressees

to the potential

for personnel

errors during infrequently

performed

evolutions

that result in, or contribute

to, events such as the inadvertent

draining of water from the reactor vessel during shutdown operations.

It is expected that recipients

will review the information

for applicability

to their facilities

and consider actions, as appropriate, to prevent a similar occurrence.

However, suggestions

contained

in this information

notice are not NRC requirements;

therefore, no specific action or written response to this notice is required.DescriDtion

of Circumstances

Quad Cities Unit 2 On February 24, 1999, Quad Cities Unit 2 was in cold shutdown with reactor water temperature

at 131 'F and reactor water level at 80 inches indicated

level (normal level during operations

is 30 inches indicated

or 173 inches above the top of active fuel [TAF]). Core cooling was being maintained

in a band of 120 'F to 170 OF by the OA" loop of the shutdown cooling mode of the residual heat removal (RHR) system after being switched from the nB" loop at 12:32 a.m.During the switch over the licensee inadvertently

failed to close the OA RHR minimum flow valve as required by the procedure.

Sometime later operators

noted a decreasing

reactor water level and at about 1:02 a.m. secured the *2A RHR pump and isolated shutdown cooling. At 1:55 a.m. operators

restored the *2A' loop of shutdown cooling to the proper lineup and started the *2A RHR pump. Water level had decreased

to a minimum of about 45 inches indicated, and reactor water temperature

had risen to a maximum of about 163 OF. Forced circulation

of reactor vessel water using a reactor recirculation

pump remained in effect throughout

the event.On the basis of post event reviews, It appears that the minimum flow valve in the OA loop was left open because the nuclear station operator failed to ensure that the tasks were performed

in the sequence specified

in the operating

procedures.

The nuclear station operator who was (7008 PD(L H ort<<4qj-Oiif

qqos(J5 C7Ffcj ANW\\b

IN 99-14 May 5, 1999 directing

the evolution

from the control room gave the non-licensed

operator permission

to de-energize the breaker for the WA RHR minimum flow valve operator before the valve was taken to the required closed position.

De-energizing

the breaker also removed power to the valve position indicator

lights in the control room. Thus, when the nuclear station operator tried to verify that the valve was closed, there was no position indication

in the control room to make that verification.

The nuclear station operator made the incorrect

assumption

that the valve was already closed and moved to the next step in the procedure.

This failure to close the WAX RHR minimum flow valve opened a drain path from the reactor to the suppression

pool. To further complicate

the event, the operating

crew did not recognize

that there was any problem until approximately

10 minutes had passed and the water level had decreased

about 13 inches because of a misinterpretation

of causes of the level decrease.

After detecting

the decrease, the operating

crew was slow to react, which allowed the level to decrease another 20 inches before the operators

isolated shutdown cooling which terminated

the draindown.

The licensee estimated

that a total of 6000 to 7000 gallons was drained from the reactor to the suppression

pool.Operations

staff practices

including

poor communications, poor activity briefings

for high-risk activities, lack of effective

pre-shift

briefings, inadequate

supervision

of important

control room activities, inadequate

monitoring

of control room panels, and slow event response may have contributed

to the event. Although the unintended

loss of inventory

to the suppression

pool highlighted

significant

weaknesses

in plant operations, the safety significance

was minimized

by two features.

First, a reactor recirculation

pump remained in service throughout

the event which served to distribute

decay heat. Second, an automatic

isolation

of shutdown cooling would have occurred at 8 inches indicated

level which would have stopped the draining event.An indicated

water level of 8 inches corresponds

to approximately

151 inches of water level above the TAF in the reactor core.Arkansas Nuclear One Unit 2 On February 2, 1999, at Arkansas Nuclear One Unit 2, the operators

were draining the refueling

canal in preparation

for installing

the reactor vessel head. Refueling

was complete and steam generator

nozzle dams were installed.

The operators

were using the two low pressure safety injection (LPSI) pumps to drain the canal to the refueling

water storage tank;one pump also served as the shutdown cooling pump. The rate of draindown

was approximately

3.3 Inches per minute. When the water level reached 105 inches, the reactor operator noted that level started to lower rapidly. Operators

stopped one of the LPSI pumps and instructed

a local operator to close the isolation

valve to the refueling

water tank. This manually operated valve required 55 turns of the handwheel

to fully close. Within approximately

1.5 minutes, the reactor vessel level had dropped below the 65 inch level (where reduced inventory

begins) and continued

down to 56 inches before the valve could be fully closed. (Reference

zero on these level instruments

is the bottom of the hot leg, with mid-loop being defined at approximately

24 inches.) The average rate of level decrease between 105 IN 99-14 May 5, 1999 inches and 56 inches was approximately

33 inches per minute. At its lowest level, 56 inches indicated, there were still 93 inches of water above the TAF. Using the high pressure safety injection (HPSI) pump the operators

brought the level back up to 90 inches. The plant was in reduced inventory

operations (below 65 inches) for approximately

7 minutes. During the event the level remained well above the point where LPSI pump cavitation

would be expected.

The licensee concluded

that the safety significance

of the event was minimal because multiple sources of makeup water were available, redundant

mitigation

equipment

was available, and the operators

were quick to recognize

and respond to the event.On the basis of post event reviews, it was determined

that the procedure

used for draining down the refueling

canal was inadequate

in that it incorrectly

stated that the draindown

should be secured at the 90-inch level. The procedure

should have directed that the rate of draining be secured at the 106-inch level so that appropriate

precautions

could be taken before resuming the draindown.

These precautions

should have Included reminders

to the operating crew that below the 106-inch level the level will drop much more quickly due to the transition

of pumping from a large volume in the refueling

canal to a small volume In the reactor vessel.Therefore, in order to maintain control of the water level, the draindown

rate should be decreased

and an operator should be stationed

to directly monitor the level.Additional

factors that contributed

to this event include: the operators

received little specific training on this evolution;

the crew was inexperienced

in performing

this task; the task should have been classified

as an infrequent

task requiring

a more thorough briefing;

and, operators failed to station an operator in a position where he could directly monitor the water level in the refueling

canal. Instead they monitored

it remotely using a video camera that did not provide a clear picture of the water level.FitzPatrick

On December 2, 1998, at the James A. FitzPatrick

Nuclear Power Plant, the operators

were in the process of reassembling

the reactor following

refueling.

Operators

were controlling

the reactor vessel water level at 357 inches above TAF by adjusting

the water discharge

rate to compensate

for the constant input from the control rod drive cooling water system. While in this condition, the licensees

risk analysis requires that reactor vessel water level be monitored

using two independent

level indicators.

To meet this requirement, the licensee designated

a wide range indicator

which provided Indication

up to the top of the reactor vessel and an RHR interlock

level indicator

which provided indication

in the range from -150 inches to +200 Inches as the instruments

to be used during this evaluation.

In order for the wide-range

level Indicator

to remain available

with the reactor head removed, a temporary

standpipe

and fill funnel were used to replace a portion of the reference

leg. At the time of the event, the licensee was in the process of removing this temporary

standpipe

and reinstalling

the original reference

leg components.

As the water drained from the standpipe, it caused the wide-range

level indicator

to erroneously

show an increasing

water level. For a period of approximately

one hour the operators

in the control room, unaware that the ongoing maintenance

would cause an error in the indicated

water level, compensated

for the apparent increasing

level by increasing

the discharge

rate. This action had the effect of reducing the

IN 99-14 May 5, 1999 actual water level from 357 inches to 255 inches. During the same time period, the operators were also in the process of filling and venting the reactor feedwater

piping, which could have affected the reactor water level. Once the normal reference

leg piping had been reinstalled

and the reference

leg began to refill, the indicated

level decreased

from 357 inches to the actual level of 255 inches. The second level instrument, which does not come on-scale until the level goes below 200 inches, remained off-scale

high.When operators

discovered

the level discrepancy, they used a temporary

pressure gauge connected

to the reactor vessel low-point

tap to confirm the actual water level. After confirming

the accuracy of the wide-range

indicator, they restored the reactor vessel water level to 357 inches. The 100-inch error represented

approximately

14,000 gallons of water. The licensee determined

that the safety significance

of this event was low since the reactor was in cold shutdown with low decay heat and the reactor water level remained well above the TAF. In addition, the drain-down

would have been limited by an automatic

Isolation

of the draindown path, which would have occurred prior to vessel level reaching 177 Inches above the TAF.The licensee's

post event review identified:

weaknesses

in the operator's

knowledge

of the reactor assembly process; lack of explicit detail in the reactor assembly procedure;

and, weaknesses

in the plant risk assessment

process. Contrary to the assumption

that two designated

reactor water level indicators

were available, only one indicator, the wide-range

instrument, was available

in the range above 200 inches. When the reference

leg on the wide-range instrument

was disassembled

and drained, the one usable indicator

was rendered unavailable.

The second instrument

was pegged off-scale

high and remained that way throughout

the event because the level never dropped below 200 inches. A post event review by the licensee indicated

that other reactor water level instruments, remained operable during the event but, apparently

the operators

did not rely on these other instruments

or notice the discrepancy

between them and the wide range Indicator.

Proposed corrective

actions included procedural

enhancements

to ensure that reactor level instrumentation

credited by the outage risk assessment

remains available

during reactor disassembly

and reassembly.

Discussion

Personnel

errors appear to have caused, or contributed

to, these three inadvertent

reactor vessel draindown

events. The likelihood

of personnel

errors is dependent

upon the operators knowledge

of the task gained through previous experience

and training.

It is also dependent upon the quality of the procedures

used to perform the task, the level of supervision, the adequacy of pre-job briefings, fatigue, and distractions

resulting

from multiple tasks. In each of the events, the plant staff made errors during a seldom-performed

evolution.

Because it was a seldom-performed

evolution, more training, better pre-job briefings, closer supervision, and procedures

that contain more details than those for frequently

performed

activities

might have prevented

these events.

IN 99-14 May 5, 1999 This information

notice requires no specific action or written response.

If you have any questions

about the information

in this notice, please contact the technical

contact listed below, the appropriate

regional office, or the appropriate

Office of Nuclear Reactor Regulation (NRR)project manager.Ledyard B. Marsh, Chief Events Assessment, Generic Communications

And Non-Power

Reactors Branch Division of Regulatory

Improvement

Programs Office of Nuclear Reactor Regulation

Technical

contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdDRenrc.aov

REFERENCES:

NRC Integrated

Inspection

Report No. 50-333/98-08, issued February 10, 1999 (Accession

No.9902170348)

for the James A. FitzPatrick

Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachment:

List of Recently Issued NRC Information

Notices

~~ Attachment

1 IN 99-14 May 5, 1999 Page 1 of I LIST OF RECENTLY ISSUED NRC INFORMATION

NOTICES Information

Date of Notice No. Subject Issuance Issued to 99-13 Insiahts from NRR Inspections

4129199 All holders of operatina

licenses of Low-and Medium-Voltage

Circuit Breaker Maintenance

Programs for nuclear power reactors 99-12 Year 2000 Computer Systems Readiness

Audits Incidents

Involving

the Use of Radioactive

Iodine-131

4/28/99 4/23/99 All holders of operating

licenses or construction

permits for nuclear power plants All medical use licensees 99-11 97-15, Sup 1 Reporting

of Errors and 4/16/99 Changes in Large-Break/Small- Break Loss-of-Coolant

Evaluation

Models of Fuel Vendors and Compliance

with 10 CFR 50.46(a)(3)

All holders of operating

licenses for nuclear power reactors, except those who have permanently

cease operations

and have certified

that fuel has been permanently

removed from the reactor 99-10 99-09 Degradation

of Prestressing

4/13/99 Tendon Systems in Prestressed

Concrete Containments

Problems Encountered

When 3/24/99 Manually Editing Treatment

Data on The Nucletron

Microselectron-HDR (New) Model 105.999 Urine Specimen Adulteration

4/1/99 All holders of operating

licenses for nuclear power reactors All medical licensees

authorized

to conduct high-dose-rate (HDR)remote after loading brachytherapy

treatments

All holders of operating

licensees for nuclear power reactors and licensees

authorized

to possess or use formula quantities

of strategic

special nuclear material 99-08 OL = Operating

License CP = Construction

Permit

IN 99-xx April xx, 1999 Page 5of 5 This information

notice requires no specific action or written response.

If you have any questions

about the information

in this notice, please contact the technical

contact listed below, the appropriate

regional office, or the appropriate

office of Nuclear Reactor Regulation (NRR)Project Manager.Ledyard B. Marsh, Chief Events Assessment, Generic Communications

And Non-Power

Reactors Branch Division of Regulatory

Improvement

Programs Office of Nuclear Reactor Regulation

Technical

contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdRDanrc.aov

REFERENCES:

NRC Integrated

Inspection

Report No. 50-333198-08, issued February 10, 1999 (Accession

No.9902170348)

for the James A. FitzPatrick

Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachments:

1. List of Recently Issued NMSS Information

Notices 2. List of Recently Issued NRC Information

Notices DOCUMENT NAME: G:ICDPDRAININ\DRAIN.0B.WPD

To receive a copy of this document, Indicate In the box C=Copy w/o attachmentlenclosure

E=Copy with attachment/enclosure

N = No copy OFFICE PECB:DRIP

I Tech Editor l DRCH I PDIV-1 I NAME CPetrone I_ RGallo 1 MNolangfarP.

DATE V /0199 [3 /1/99 4 /4I9 1' /0g99 F .V. ...OFFICE PDI-1 IA .I PDIII-2 I C:PECB:DRIP

I NAME 2 Jiiam RPulsjier

LMarsh DATE lf/499 I1'/t 99 I /99 OFFICIAL RECORD COPY

IN 99-14 May 5, 1999 This information

notice requires no specific action or written response.

If you have any questions

about the information

in this notice, please contact the technical

contact listed below, the appropriate

regional office, or the appropriate

Office of Nuclear Reactor Regulation (NRR)project manager.[arig sjid by]Ledyard B. Marsh, Chief Events Assessment, Generic Communications

And Non-Power

Reactors Branch Division of Regulatory

Improvement

Programs Office of Nuclear Reactor Regulation

Technical

contact: Chuck Petrone, NRR 301-415-1027 E-mail: cdr)ODnrc.gov

REFERENCES:

NRC Integrated

Inspection

Report No. 50-333/98-08, issued February 10, 1999 (Accession

No.9902170348)

for the James A. FitzPatrick

Nuclear Power Plant for the period November 22, 1998, through January 10, 1999.Attachment:

List of Recently Issued NRC Information

Notices DOCUMENT NAME: S:XDRPMSEC\99-14.IN

  • See previous concurrence

To receive a copy of this document.

indicate in the box C=CoDv w/o attachment/enclosure

E=CoDv with attachment/enclosure

N = No coov OFFICE PECB:DRlIP

I Tech Editor l DRCH l-ii PDIV-1 lI NAME CPetrone*

BCalure* RGallo* MNolan*DATE 04/27/99 .3/15/99 _________04128199

= 04/27/99 1 ...OFFICE PDI-1 I PD111-2 C:PECB:DJRIP

I NAME JWilliams*

RPulsifer'

I-Marsh _ _ __ _DATE 04/27/9 .04/27/99 k,-u99 OFFICIAL RECORD COPY