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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20138P730 + (ML20138P730)
- ML20138P732 + (ML20138P732)
- 05000373/LER-1985-063-01, :on 851008,control Room HVAC Chlorine Detector B Tripped & Would Not Reset.Caused by Lower than Normal Electrolyte Drip Rate.Proper Drip Rate & Local & Control Room Alarms Restored + (ML20138P733)
- 05000267/LER-1984-012, :on 841105,only Half of Reserve Shutdown Matl Discharged from Reserve Shutdown Hopper Assembly of Control Drive During Testing.Caused by Reaction of Water Vapor Entering Assembly.Absorber Matl Replaced + (ML20138P735)
- ML20138P736 + (ML20138P736)
- 05000458/LER-1985-011, :on 850930,both Divs of Secondary & Primary Containment Isolation Spuriously Actuated.Caused by Testing Which Generated Div II MSIV Isolation Signal.Testing Reperformed & No Isolations Occurred + (ML20138P737)
- 05000259/LER-1985-050, :on 851003,during Review of Surveillance Requirements,Determined Several Instrument Surveillances Not Performed Per Tech Specs.Caused by Failure to Implement Plant Procedures + (ML20138P738)
- 05000260/LER-1985-013-03, :on 851002,during Performance of Plant Surveillance Instruction,Inadvertent Secondary Containment Isolation Occurred When Alternate Feeder Breaker to Shutdown Board Tripped.Caused by Binding Trip Button + (ML20138P742)
- 05000295/LER-1985-032, :on 850909,six Containment Isolation Phase a Valves Stroked Closed During Periodic Test PT-10, Safeguards Actuation Unit 1. Caused by Personnel Error. Test Operators Cautioned + (ML20138P744)
- 05000266/LER-1985-009, :on 851009,turbine Runback Occurred Due to Rod Drop Signal on Power Range Nuclear Instrumentation Sys. Caused by Technician Introducing Signal During Calibr of Negative Rate Runback Setpoint + (ML20138P746)
- 05000317/LER-1985-014, :on 851120,discovered One Isolation Damper in Each of Two Control Room HVAC Inlet Ducts Inoperable.Caused by Improper Adjustment of Damper Linkages.Blade Brackets Replaced & Procedure Changed + (ML20138P747)
- ML20138P748 + (ML20138P748)
- 05000282/LER-1985-014, :on 851001,breaker 12M Accidentally Tripped Making Safeguards Bus 120 Inoperable.Caused by Contractor Workman Bumping Manual Trip Device & Mgt Deficiency.Breaker Reclosed.Administrative Controls Tightened + (ML20138P749)
- ML20138P750 + (ML20138P750)
- 05000237/LER-1985-036-03, :on 851002,reactor Bldg Ventilation Sys Trip Occurred from Fuel Pool Monitor Downscale Trip.Caused by Loose Channel a Connector & Low Channel B Setpoint.Anomalies Corrected.Bldg Sys Reset + (ML20138P751)
- ML20138P752 + (ML20138P752)
- 05000312/LER-1985-019, :on 851002,reactor Trip Occurred & RCS Temp Decreased to Approx 70 F.Caused by Excessive Steam Loads Due to Two Open Relief Valves on Feedwater Heater 4A.HPI Flow Manually Initiated to Maintain Pressure + (ML20138P753)
- ML20138P754 + (ML20138P754)
- 05000289/LER-1981-013-01, /01X-1:on 811125,bubble Leakage Test Indicated Leaking Tubes in once-through Steam Generators (OTSG) a & B. Caused by Inadvertent Introduction of Sulfur Into Rcs. Chemical Agent Removed & OTSGs Repaired + (ML20138P756)
- 05000458/LER-1985-037, :on 851117,while in Startup,Erroneous RWCU Isolation Occurred.Caused by Defective Trip Unit.Trip Condition Reset + (ML20138P757)
- ML20138P758 + (ML20138P758)
- ML20138P759 + (ML20138P759)
- ML20138P760 + (ML20138P760)
- 05000366/LER-1985-032-01, :on 851005,while Placing Reactor Water Cleanup (RWCU) Sys in Svc,Personnel Noted That RWCU Pump Inboard Suction Isolation Valve Isolated on High Sys Differential Flow.Caused by Valves Leaking Past Seats + (ML20138P761)
- ML20138P763 + (ML20138P763)
- ML20138P766 + (ML20138P766)
- ML20138P767 + (ML20138P767)
- 05000293/LER-1985-032, :on 851125,5 of 16 Main Steam Line High Flow Switches Found Outside of Required Setpoint During Routine Primary Containment Isolation Sys Surveillance.Caused by Improper Alignment of Switch Linkage + (ML20138P768)
- IR 05000456/1985052 + (ML20138P770)
- 05000331/LER-1985-040, :on 851010,unintentional Momentary Violation of Secondary Containment Occurred When Both Airlock Doors Simultaneously Opened.Caused by Loose Wire on Solenoid.Wire Repaired.Amend to Tech Specs Requested + (ML20138P773)
- ML20138P774 + (ML20138P774)
- ML20138P775 + (ML20138P775)
- IR 05000219/1985033 + (ML20138P776)
- ML20138P777 + (ML20138P777)
- ML20138P778 + (ML20138P778)
- ML20138P779 + (ML20138P779)
- ML20138P780 + (ML20138P780)
- ML20138P781 + (ML20138P781)
- ML20138P782 + (ML20138P782)
- ML20138P784 + (ML20138P784)
- ML20138P785 + (ML20138P785)
- ML20138P787 + (ML20138P787)
- ML20138P788 + (ML20138P788)
- ML20138P790 + (ML20138P790)
- ML20138P792 + (ML20138P792)
- U-600357, Final Deficiency Rept 55-85-09 Re Inadequate Implementation of Design Change Documents by Baldwin Assoc & Improper Use of Field Interference Notice by Zack Co.Initially Reported on 850816.Condition Not Reportable Under 10CFR50.55(e) + (ML20138P796)
- ML20138P798 + (ML20138P798)
- ML20138P800 + (ML20138P800)
- ML20138P801 + (ML20138P801)
- 05000260/LER-1985-016-02, :on 850606,excessive Setpoint Drift Discovered During Bench Testing.On 850722,factory Testing by Automatic Switch Co Confirmed TVA Test Data.Four Switches Returned to Factory + (ML20138P802)
- 05000245/LER-1985-028, :on 851122,possible IGSCC Identified in Several Welds on Both Jet Pump Instrumentation Assemblies.Cause Not Stated.Indications Repaired Using Weld Overlay Technique.W/ + (ML20138P804)