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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20082B469 + (ML20082B469)
- ML20082B476 + (ML20082B476)
- ML20082B478 + (ML20082B478)
- 05000366/LER-1983-113-03, /03L-0:on 831018,drywell B Equipment Drain Sump Pump Control Indication Showed Pump Running But No Flow Indicated.Caused by Failed Couplings.Couplings Replaced + (ML20082B479)
- ML20082B482 + (ML20082B482)
- RBG-16-326, Interim Deficiency Rept DR-128 Re Stainless Steel Tubing Supplied by Gulfalloy,Hub,Inc & Capital Pipe & Steel.Interim or Final Rept Will Be Submitted by 831228 + (ML20082B486)
- ML20082B489 + (ML20082B489)
- LIC-95-0077, Forwards Revised Radiological Emergency Response Plan & Revised Epips,Including Central Files Version of Emergency Plan Form (Epf) FC-EPF-9,Rev 4.Central Files Version of Epf FC-EPF-9,Rev 4 Withheld + (ML20082B490)
- 05000250/LER-1983-019-03, /03L-0:on 831008,RHR Flow Isolated Due to Pressure Transmitter PT-3-405 Exposure to Hydrostatic Test Pressure of 3,100 Psig.Caused by Unclear Drawing Configuration of Loop a Sample Line.Transmitter Replaced + (ML20082B492)
- GO2-83-678, Forwards Final Response to Notice of Violation from IE Insp Rept 50-397/83-14.Corrective Actions:Review of Quality Documentation & Receiving Records Performed to Assess Potential for Inadvertent Substitution of Reinforcing Steel + (ML20082B496)
- 05000335/LER-1983-028-03, /03L-0:on 831004,while Defueled,Test Connections Not Provided Spare Electrical Penetration E-4 W/Flange Cover.Caused by Design Deficiency Not Showing Flanged Connection.Design Change Performed + (ML20082B498)
- ML20082B500 + (ML20082B500)
- 05000269/LER-1983-016-03, Hydrogen Purge Unit Declared Inoperable Due to Discharge Flow Instrument FT-100 Damage.Caused by Personnel Error.Flow Instrument Repaired & Connections Will Be Relocated + (ML20082B508)
- ML20082B511 + (ML20082B511)
- ML20082B515 + (ML20082B515)
- ML20082B516 + (ML20082B516)
- ML20082B520 + (ML20082B520)
- ML20082B521 + (ML20082B521)
- PY-CEI-NRR-1353, Proposed Tech Specs 2.1.2,2.2.1,3.3.1,3.3.6,3.4.1.1,3.4.1.2 & 3.4.1.3 + (ML20082B526)
- ML20082B527 + (ML20082B527)
- ML20082B536 + (ML20082B536)
- ML20082B538 + (ML20082B538)
- ML20082B540 + (ML20082B540)
- LIC-95-0076, V 1 + (ML20082B541)
- 05000271/LER-1991-015, :on 910614,containment Isolation Valve Failed to Closed Due to Erosion/Corrosion & Displacement of screw- in Seat.Valve Repaired by Welding New Seat Into Valve Body + (ML20082B547)
- ML20082B548 + (ML20082B548)
- ML20082B549 + (ML20082B549)
- ML20082B551 + (ML20082B551)
- 05000333/LER-1983-046-03, /03L-0:on 831008,plant Entered 24 H Limiting Condition for Operation Due to Control Rod 02-23 Rod Selection Switch Inoperability.Caused by Old Age of Switch. Switch Replaced & Verified Operable + (ML20082B552)
- ML20082B558 + (ML20082B558)
- ML20082B563 + (ML20082B563)
- 05000333/LER-1983-050-03, /03L-0:on 831024,reactor Cleanup Sys Equipment Area High Temp Switch 12-TS-139B Setpoint Found Higher than Tech Spec Max.Caused by Instrument Drift.Setpoint Reset + (ML20082B565)
- U-601857, Monthly Operating Rept for June 1991 for Clinton Power Station,Unit 1 + (ML20082B568)
- ML20082B572 + (ML20082B572)
- 05000265/LER-1983-020-01, /01T-0:on 831027,test Data Revealed Six 12 & 28- Inch Welds on Reactor Recirculation Sys & One 20-inch Weld on RHR Shutdown Cooling Had Circumferential Indications. Caused by Intergranular Stress Corrosion + (ML20082B574)
- ML20082B575 + (ML20082B575)
- 05000277/LER-1983-024-01, /01T-0:on 831024,during Audit of Certain Radiographs of Class I Piping,Three Radiographs Read Improperly.Caused by Personnel Error.All Radiographs Reviewed + (ML20082B576)
- ML20082B577 + (ML20082B577)
- ML20082B587 + (ML20082B587)
- ML20082B590 + (ML20082B590)
- ML20082B591 + (ML20082B591)
- ML20082B592 + (ML20082B592)
- ML20082B593 + (ML20082B593)
- 05000333/LER-1983-048-03, /03L-0:on 831021,during Normal Operation,Plant Entered 24 H Limiting Condition Due to Control Rod Selection Switch 10-15 Being Inoperable.Caused by Switch Aging.Switch Replaced + (ML20082B595)
- 05000334/LER-1983-033-03, /03L-0:on 830922,two of Three River Water Pumps Left in pull-to-lock Position.Caused by Operator Failure to Return River Water Sys to Pretest Condition.Corrective Actions Complete or in Progress + (ML20082B599)
- 05000373/LER-1995-008-01, :on 950301,determined That TS SR to Take CR Temp Not Met Due to Deficient Procedure.Required Readings Immediately Taken & Verified & Operations Dept Sp LOS-AA-S2 Revised + (ML20082B601)
- ML20082B603 + (ML20082B603)
- ML20082B605 + (ML20082B605)
- 05000289/LER-1983-039-01, /01T-0:on 831018,waste Gas Sys Deuterium Monitor Removed from Svc W/O Sample Taken.Caused by Personnel Error. Sample Taken & Analyzed Immediately + (ML20082B608)
- 05000220/LER-1983-027-03, /03L-0:on 830923,during Normal Full Power Operations,Two of Three Feedwater Strings Tripped & Cooler Water Entered Reactor Core.Caused by Bad Fuse Holder in Reactor Trip Bus 131.Fuse Holder Replaced + (ML20082B613)
- 0CAN108311, Responds to NRC Re Violations Noted in IE Insp Repts 50-313/83-16 & 50-368/83-16.Corrective Actions:Actual Classroom Attendance Required at Requalification Lectures + (ML20082B615)