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 Issue dateTitleTopic
ML20207R7529 March 1987Ro:On 870207,MSIV Failed to Close During Plant Shutdown. Caused by Binding of Valve Disc on Partially Removed Valve Stop.Disc Stop Matl Removed & Valve Tested.Sketch of Valve & Stop EnclUnanalyzed Condition
Nondestructive Examination
ML20207C81422 December 1986Ro:On 861023 & 1128,RCS High Pressure Transient Occurred. Caused by Lifted Pressurizer PORV Due to Internal Event.More Specific Info Re Events Can Be Found in LERs 86-008 & 86-011
ML20215D62311 December 1986Followup Ro:On 861128,operator Inadvertently Closed Main Steam Line Isolation Valves 3516 & 3517 Instead of Containment Vessel Depressurization Valves,Causing Pressurizer High Pressure Reactor Trip
ML20204F92229 July 1986Ro:On 860729,manual Reactor Trip Initiated When Large Quantity of Steam Found Rising Over Turbine Bay Area.Caused by Leak from Moisture Separator Reheater Drain Line 2A to High Pressure Feedwater Heater 5B.Drain Lines RepairedNondestructive Examination
ML20138Q8757 November 1985Followup Summary:On 851106,alarm & Deluge of Fire Sys S-05 Received in Control Room.Caused by Spurious Signal Spike on Second Alarm Module.Investigation on Failure Mode of Fire Sys Continuing.Cable Tunnel Dried OutContinuous fire watch
ML20128L91812 July 1985Ro:On 850701,containment Vessel Sump Pump Actuation Interval Decreased Significantly from Normal.Caused by Svc Water Leak.Fan Cooler Inspected & Repaired
ML20083P81420 March 1984Ro:On 840307,during Drainage of RCS to Holdup Tanks,Rhr Containment Sump B Suction Valves MOV 851 a & B Opened Before Valve 850 a Closed,Causing Drainage of RCS Into Sump B
ML20087P73321 February 1984Ro:Providing Sequence Summary of Closeout or Class Reduction Condition for Unusual Event on 840219 Re out-of-svc Accumulators.Accumulators Returned to Svc & Declared Operable
ML20087P97127 January 1984Ro:On 831228,turbine Driven Auxiliary Feedwater Pump Steam Stop Valve Found in Tripped Position,Although Control Room Indication Indicated Valve Open.Caused by Contractor Stepping on Valve Trip Mechanism
ML20077N59031 August 1983Ro:On 830303,diesel Fuel Oil for Fire Pump Found Below Viscosity Limit.Caused by Delays in Transporting Sample to Lab for Analysis.Procedures to Expedite Resampling & Analysis Being ReviewedBoric Acid
ML20072N5898 July 1983Ro:On 830609,during Safety Injection Functional Test,When Safety Injection Signal Initiated by Simulating High Containment Pressure,Charging Pump 1C Did Not Trip, Causing Operation of Reactor Overpressure Protection Sys
ML20072U59431 March 1983Ro:On 830331,health Physics Technician Fell 40 Ft to Floor of Reactor Cavity.Individual Removed from Area & Taken to Hosp to Be Treated for Serious Injuries & DecontaminatedFire Watch
ML20083P10221 January 1983RO 83-006/01:on 830120,alarm Received in Control Room Indicating Low Screenhouse Water Level of 20 Ft,Rendering Fire Suppression Water Sys Inoperable.Addl Info Will Be Presented in 14-day Written ReptFrazil ice
05000244/LER-1982-003, RO 82-007/01T:on 820125,unit Experienced Event Described in LER 82-003 Leading to RCS Cooldown Rate Greater than 100 F/H.Further Info Will Be Submitted w/14-day Written Rept24 February 1982RO 82-007/01T:on 820125,unit Experienced Event Described in LER 82-003 Leading to RCS Cooldown Rate Greater than 100 F/H.Further Info Will Be Submitted w/14-day Written Rept
ML20084D94115 July 1977Supplemental RO-77-010:four Addl Supports (SW-69,73,78 & 83) Found W/Stresses Under DBE Conditions in Excess of Allowable Values.Corrective Actions Underway
ML20084D93814 July 1977RO-77-010:on 770713,design Error Found in Redundant Svc Water Discharge Line Support.Overstress Condition Could Exist W/Line Not Yet Charged or in Svc.Line in Hold ConditionBackfit
ML20084B85510 February 1977Supplemental RO 76-24:on 761008,leaks Found in 8-inch Schedule 10 Boric Acid Piping.Cause of Cracks Probably Due to Stress Corrosion AttackBoric Acid
Hydrostatic
Nondestructive Examination
Liquid penetrant
ML20084C15121 December 1976Supplemental RO-76-21:on 760819,two Control Rods Dropped. Westinghouse Recommendations for Cause Later Determined Not to Be Actual Cause.New Recommendations to Be Carried Out During Next Refueling Outage
ML20084C31521 June 1976Supplemental RO 76-10:on 760228,excessive Leakage Observed from Valve Inside Purge Supply Control Valve.Results of Vendor Insp of Assembly Submitted
ML20084C29025 May 1976Supplemental RO-76-12:on 760331,during Testing,Excessive Leakage Found in Containment Personnel Airlock Handwheel Shaft Seal.Corrective Action Include Placing Seal on Packing Gland Nuts to Prevent Rotation W/Shaft
ML20084A09712 May 1976Supplemental RO 76-07 Re Train a Containment Isolation & Ventilation Isolation Failure to Latch.Fourteen Relays Checked for Clearance Between Electromagnet Pole Face & Raised Section of Armature
ML20083R8889 March 1976RO 76-11:on 760308,control Room Charcoal Filter Damper Discovered Improperly Positioned.Trouble Card Issued & Work Initiated to Correct Problem
ML20084A01223 February 1976RO 76-08:on 760227,39 Steam Generator Tubes Explosively Plugged in Steam Generator a & 2 in Steam Generator B.Tubes Exhibited Tube Wall Deterioration in Excess of 40%
ML20084A1358 February 1976RO 76-05:on 760208,excessive Leakage Observed Through Several Containment Penetrations.Cause Not Stated.Repairs to Valves Underway
ML20084A9727 November 1974Ro:On 741008,Westinghouse Informed Util That Safety Injection Sys Delivery Curve Employed for Steam Line Break Accident Analysis Inconsistent W/Analyses Used for Recent Loca.Util to Maintain Shutdown Margin of at Least 2.45%Shutdown Margin
ML20084E2257 June 1974Ro:On 740509,during Surveillence Procedure PT 16,little Flow Reduction Occurred Following Opening of Motor Driven Auxiliary Feedwater Pump a & B Discharge Valve.Cause Unapparent.Frequency of Surveillance Test Increased
ML20084H09625 February 1974RO: Overexposure of Individual to Radiation Occurred During First Quarter of 1974.Correction to Reporting Similar Occurrence Encl
ML20084H09920 February 1974RO: Individuals Overexposed to Radiation During First Quarter 1974.Investigation Underway
ML20084E33421 June 1973Ro:On 730523,thirty Minutes After Boric Acid Transfer Pumps Started Recirculation,Control Rods Noted as Stepping Out. Caused by Malfunction of Blend Sys Valve FCV-110B.Repair Instituted & Completed on 730524Boric Acid
ML20084E4368 June 1973Ro:On 730529,during Performance of Monthly Surveillance Undervoltage & Underfrequency Protection,Device Armature of Knife Switches for Solenoid Coil Discovered Not Dropping to Assume Deenergized Condition.Caused by Scale Accumulation
ML20084E3657 June 1973Ro:On 730606,high Bistable Setting Approx 2.1% Higher than Specified Value Set Forth in Plant Procedure.Caused by Personnel Error in Transposing Desired Calculated Current Level from Work Sheet.Setting to Correspond W/Steam Flow
ML20084E35431 May 1973Ro:On 730502,Bank D Control Rod Sys Observed Stepping Out of Core.Caused by Loose Solder Joint in QM-401.Automatic Rod Control Immediately Switched to Manual W/No Indication of Any Change in Reactor Power.Averaging Unit Repaired
ML20084E45630 May 1973Ro:On 730529,upon Opening Knife for Solenoid Coil of Primary Undervoltage Device 273/IIA,device Armature Discovered Not Dropping Down to Assume Deenergized Condition.Caused by Scale Accumulation on Device.Investigation Continuing
ML20084E61628 December 1972RO:720831 & 0901 Unplanned Release of Radioactive Passes Occurred During Removal of Spent Resins from Spent Resin Tanks.Cause Not Stated.Written Procedure for Handling Resin Revised & Precaution Included Re Vent Header Pressure
ML20084E96430 June 1972Ro:On 720623,w/reactor at 5% Thermal Power,Control Board Received Alarms of Rod Bottom Rod Stop & Rod Control Urgent Failure Rod Stop.Caused by Water from Swagelok Fitting on Tubing Dropping on Rod Control Cabinets.Fitting Repaired
ML20084E97331 May 1972Ro:On 720503,upon Entering Steam Generator & Starting Grit Blasting Equipment,Workman Discovered Face Mask Not Functioning & Exited Area.Caused by Failure to Tighten Threaded Connection of Air Hose to Mask.Exams Performed
ML20084E46828 April 1972Ro:On 720420,while Plant Being Cooled Down in Preparation for Refueling,Release Rate of Airborne I-131 from Plant Vent Exceeded Tech Spec Limits.Cause Unknown.Charcoal Filters from Plant Vent Iodine Monitor Being ReplacedBoric Acid
ML20084E65930 March 1972Ro:On 720320,while Reactor in Hot Shutdown,Msivs Tested for Closure & MSIV-1B Valve Found Closed Only Half Way.Cause Unknown.Valve Mfg Contacted for Recommendations to Prevent Recurrence
ML20084F0807 February 1972Ro:On 720131,while Conducting Monthly Surveillance Test, Underfrequency Relay on 4160-kV Bus 11B Failed to Transmit Signal to Logic Racks.Caused by Faulty Capacitor.Spare Relay Installed & Tested Satisfactorily
ML20084F12114 December 1971Ro:On 711205,safety Injection Pump Motor C Tripped Automatically When Nearly Up to Speed.Caused by Motor Tripping Out on Starting Current Due to Leakage in Time Delay Dashpot.Replacement Overcurrent Device Installed
ML20084E5679 July 1971Ro:On 710630,MSIV Failed to Close on Signal.Solenoid Operators on MSIV 1A Removed & Inspected and All Parts
ML20084E61011 June 1971Ro:Between 710601-05,calculations Indicated Gaseous Effluent Release Limits Exceeded.Caused by Gasket Leak on Vol Control Tank Pressure Control Regulator Valve PCV141.Continuous Recording Iodine Monitor Installed on Stack Vent
ML20084E63729 April 1971Ro:On 710422,during Diesel Generator Load & Safeguard Sequence Test,Valves 826 A,B,C & D Failed to Open.Caused by Momentary Loss of Voltage on 480-volt Safeguard Busses.Power Supply Transfer RecommendedBoric Acid
ML20084E83621 December 1970Ro:During 700930-1015 Shutdown,Broken Stud Found on One Support for Primary Sys Component.W/O Stated Encl
ML20084E85614 October 1970Ro:On 701004,core Deluge Valve 852B Malfunctioned.Caused by Seizure of Stem Nut to Valve Stem.New Stem Nut Installed
ML20084E55015 July 1970Ro:On 700706,boron Dilution Performed W/Reactor Critical & No Reactor Coolant Pump on RHR Pump in Operation.Orders Issued That Maint Work Performed Only W/Authorized Procedures AvailableBoric Acid
Power change
ML20084E72122 May 1970Ro:On 700514,during Reactor Cooldown Procedure,Msiv 1B Failed to Close.Caused by Malfunction of Valve Mechanism. Packing Gland Loosened
ML20084E78213 March 1970Ro:On 700306,during Surveillance Test,Excessive Air Leakage Around Lower Handwheel Shafts That Penetrate to Outside Handwheels Noted.Ring of Packing to Lower Handwheel Shaft Added
ML20084E77727 February 1970Ro:On 700130,motor Operated Svc Water Valves 4013,4300 & 4028 on Emergency Suction Line to Auxiliary Feedwater Pumps Reported to Operate Improperly.Caused by Operating Personnel Misunderstanding
ML20084E41619 January 1970RO:700108,during Draining Required to Permit Replacement of Coolant Temp detectors,in-core Thermocouple Reading Indicated Temp Exceeded Tech Spec Limit.Caused by Failure to Monitor Temp by Alternate Means