ML20084A972

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Ro:On 741008,Westinghouse Informed Util That Safety Injection Sys Delivery Curve Employed for Steam Line Break Accident Analysis Inconsistent W/Analyses Used for Recent Loca.Util to Maintain Shutdown Margin of at Least 2.45%
ML20084A972
Person / Time
Site: Ginna Constellation icon.png
Issue date: 11/07/1974
From: White L
ROCHESTER GAS & ELECTRIC CORP.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20084A958 List:
References
NUDOCS 8304060047
Download: ML20084A972 (1)


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g ROCHESTER CAS U D ELE &ic CORPORATION e 89 EAST AVEN ROCliES TER, ll.y.

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tion u wuait. JR inter o e uc t rae siot eer sera coot ns 5 4 b.2 700 November 7,1974 Mr. James P. O'Reilly 7

r Director U.S. Atomic Energy Commission

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b Directorate of Regulatory Operations

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Region I N

G31 Park Avenue l'ing of Prussia, Pennsylvania 19406 m

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Subject:

Unusual Event - R.E. Ginna Nuclear Power Plant Unit No.1 Docket No. 50-244 ek 7

Dear Mr. O'Reilly:

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Rochester Cas and Electric Corporatiori was informed at a meeting on October 8,1974 by Westinghouse Electric Co' peration that the Safety Injection r

h System delivery curve employed for the Steam LUu Preak Accident Analysia (SLilA Analysis) was inconsistent with that used for recent Loss of. Coolant

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y Accident Analyses. The delivery curve had been revised subsequent to the most recent SLBA Analycis, rcrferr'od by Westinghousc in I cbrusrv 1971 to cccount for the as-built piping configuration and operatio +] characteristics and to p_

include a provision for system degradation over'the life of the plant. Those revisions resulted in a lowrsing of the delivery curve.

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Preliminary analyses performed by Westinghouse with conservativo reactivity 3

a pLrameters demonstrate that a shutdown margin of 2.45%Ak/k will insure that all f

design criteria are met. The calculated shutdown margin for the present fuci a

cycle, Cycle 4, which includes provision for the most reactive contrei rod being stuck out of the core and includas a 10% design allowance,'2s 2.48%$k/k at E

the end of the cycle ( 0 ppta boron) with equilibrium ::enon and is 0.25G Ak/k

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ilt the haginning of the cycle with equilibrium xenon. The shutdown m:rgir 7

required by the Technical Snecifications is 1.9% Ak/k at the end of the cycle.

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Roc 60 ster Gat and Electric CorporMioil has asked Westinghouse to perform' h

g additional analyses in order to minimize the shutdown margin required to meet L

all design objectives. In the interim, P.G&E will maiittain a chutdown marcin E

at least 2.45% Ah/k.

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Very truly youri,

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