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Issue date | Title | Topic | |
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PNO-V-93-013, on 930809,during pre-announced anti-nuclear demonstration,13 Protestors Illegally Entered Plant Access Gate & Immediately Taken Into Custody by Sheriff Deputies. Demonstration Related to CP Recapture Hearings for Plant | 9 August 1993 | PNO-V-93-013:on 930809,during pre-announced anti-nuclear demonstration,13 Protestors Illegally Entered Plant Access Gate & Immediately Taken Into Custody by Sheriff Deputies. Demonstration Related to CP Recapture Hearings for Plant | |
PNO-V-93-002, on 930113,L Marbet Held Press Conference W/ Portland,Or Media & Alleged That NRC Had Inappropriately Authorized Feb 1992 Restart of Plant.Util Announced on 930104 That Operation of Plant Would Be Permanently Ceased | 13 January 1993 | PNO-V-93-002:on 930113,L Marbet Held Press Conference W/ Portland,Or Media & Alleged That NRC Had Inappropriately Authorized Feb 1992 Restart of Plant.Util Announced on 930104 That Operation of Plant Would Be Permanently Ceased | |
PNO-V-93-001, on 930104,Licensee Notified Region V That Util Board Decided That Plant Will Not Be Restarted & Currently Shutdown for Insp & Repair of SG Tubes.Licensee Notified Media | 4 January 1993 | PNO-V-93-001:on 930104,Licensee Notified Region V That Util Board Decided That Plant Will Not Be Restarted & Currently Shutdown for Insp & Repair of SG Tubes.Licensee Notified Media | |
PNO-V-92-038, on 921209,B Roberts Plans to Notify News Media of Request of or Energy Facility Siting Council to Hold Hearing on Utility Steam Generator Safety | 8 December 1992 | PNO-V-92-038:on 921209,B Roberts Plans to Notify News Media of Request of or Energy Facility Siting Council to Hold Hearing on Utility Steam Generator Safety | |
PNO-V-92-037, on 921201,meeting Conducted at Plant to Address 921109 Steam Generator Tube Leak & Licensee Request for Emergency TS Change to Permit Restart | 1 December 1992 | PNO-V-92-037:on 921201,meeting Conducted at Plant to Address 921109 Steam Generator Tube Leak & Licensee Request for Emergency TS Change to Permit Restart | |
PNO-V-92-033, on 921019,US Geological Survey Notified California Governor Ofc of Significant Likelihood That Earthquake of Magnitude 6 Will Occur on San Andreas Fault Near Parkfield | 20 October 1992 | PNO-V-92-033:on 921019,US Geological Survey Notified California Governor Ofc of Significant Likelihood That Earthquake of Magnitude 6 Will Occur on San Andreas Fault Near Parkfield | Earthquake |
PNO-V-92-004, on 920225,Trojan Power Plant Entered Mode 2 After Extended Outage.Plant Currently Critical at Less than 1 Percent Power & Licensee Conducting Low Power Physics Testing.Tests Expected to Be Completed by 920227 | 25 February 1992 | PNO-V-92-004:on 920225,Trojan Power Plant Entered Mode 2 After Extended Outage.Plant Currently Critical at Less than 1 Percent Power & Licensee Conducting Low Power Physics Testing.Tests Expected to Be Completed by 920227 | |
PNO-V-91-003, on 910307,unit 1 Shutdown for Refueling Operations & Loss of Offsite Power.Licensee Personnel Manually Moved New Module,Still in Mast,Away from Reactor Vessel & Core | 7 March 1991 | PNO-V-91-003:on 910307,unit 1 Shutdown for Refueling Operations & Loss of Offsite Power.Licensee Personnel Manually Moved New Module,Still in Mast,Away from Reactor Vessel & Core | |
PNO-V-91-002, on 910303,Trojan Declared an Unsual Event & Initiated Plant Shutdown Due to Inability to Meet Requirements of TS 3.8.2.1,which Requires That Four 120 Volts AC Preferred Instrument Busses Be Operable | 5 March 1991 | PNO-V-91-002:on 910303,Trojan Declared an Unsual Event & Initiated Plant Shutdown Due to Inability to Meet Requirements of TS 3.8.2.1,which Requires That Four 120 Volts AC Preferred Instrument Busses Be Operable | |
PNO-V-90-045, State of or Measure 4 Re Closure of Facility Defeated in 901106 Vote.Util Will Hold News Conference | 7 November 1990 | PNO-V-90-045:State of or Measure 4 Re Closure of Facility Defeated in 901106 Vote.Util Will Hold News Conference | |
PNO-V-90-038, A:on 900927,main Generator Trip Resulted in Unplanned Plant Shutdown.Transient Caused 140 MW Excursion on Grid,Tripped Off Nearby Substation & Shook Turbine Bldg Deck.Ge Contacted for Recommendations | 27 September 1990 | PNO-V-90-038-A:on 900927,main Generator Trip Resulted in Unplanned Plant Shutdown.Transient Caused 140 MW Excursion on Grid,Tripped Off Nearby Substation & Shook Turbine Bldg Deck.Ge Contacted for Recommendations | |
PNO-V-90-033, on 900726,observed Crack in Charging Pump Suction Header Piping Caused by Boric Acid Crystals on Elbow of Pump.Licensee Considers Piping Operable & to Be Repaired W/O Plant Shut Down.Inspector Monitoring Plant | 27 July 1990 | PNO-V-90-033:on 900726,observed Crack in Charging Pump Suction Header Piping Caused by Boric Acid Crystals on Elbow of Pump.Licensee Considers Piping Operable & to Be Repaired W/O Plant Shut Down.Inspector Monitoring Plant | Boric Acid |
PNO-V-90-032, on 900711,steam Dumps Did Not Automatically Open to Pick Up Load Lost from Turbine During Performance of Turbine Test.Operators Took Manual Control & Stabilized Plant.Plant Shutdown to Investigate Event | 11 July 1990 | PNO-V-90-032:on 900711,steam Dumps Did Not Automatically Open to Pick Up Load Lost from Turbine During Performance of Turbine Test.Operators Took Manual Control & Stabilized Plant.Plant Shutdown to Investigate Event | |
PNO-V-90-010, on 900320,facility Entered TS 3.0.3 After Engineering Organization Determined Main Steam Flow Trip Setpoints Were Incorrect & Nonconservative.Plant Shutdown Began IAW TSs | 20 March 1990 | PNO-V-90-010:on 900320,facility Entered TS 3.0.3 After Engineering Organization Determined Main Steam Flow Trip Setpoints Were Incorrect & Nonconservative.Plant Shutdown Began IAW TSs | |
PNO-V-90-011, on 900919,Vice President Nuclear DW Cockfield Announced Resignation After Being in Position Since March 1987.TD Walt Will Serve as Vice President-Nuclear Until Licensee Identify Replacement | 20 March 1990 | PNO-V-90-011:on 900919,Vice President Nuclear DW Cockfield Announced Resignation After Being in Position Since March 1987.TD Walt Will Serve as Vice President-Nuclear Until Licensee Identify Replacement | |
PNO-V-89-048, on 890809,plant Tripped on Overtemp Differential Temp.Caused by Spurious Trip Signal Received from Other Channel.Reactor Shutdown in Mode 3 in Order for Licensee to Attempt to Identify Source & Cause of Signal | 10 August 1989 | PNO-V-89-048:on 890809,plant Tripped on Overtemp Differential Temp.Caused by Spurious Trip Signal Received from Other Channel.Reactor Shutdown in Mode 3 in Order for Licensee to Attempt to Identify Source & Cause of Signal | |
ML20245G610 | 16 June 1989 | PNS-V-89-005:on 890615,licensee Informed NRC of Possible Onsite Use & Sale of Marijuana & Cocaine by Five Contract Employees,Employed by Northwest Energy Svcs Co.Employees Interviewed,Searched & Given Urinanalyses on 890616 | |
PNO-V-88-060, on 881113,turbine Trip/Reactor Trip on hi-hi Steam Generator Level Occurred.Caused by Faulty Controller for Feedwater Regulation Valve on Steam Generator B.Licensee Developing Actions to Address Problems | 15 November 1988 | PNO-V-88-060:on 881113,turbine Trip/Reactor Trip on hi-hi Steam Generator Level Occurred.Caused by Faulty Controller for Feedwater Regulation Valve on Steam Generator B.Licensee Developing Actions to Address Problems | |
PNO-V-88-057, on 880916,while Verifying Pressure Transmitter PT-458,bistables Tripped.Caused by Technician Error & Exceeding Shutdown by More than 48 H.Problems Encountered During Reactor Startup Listed | 19 September 1988 | PNO-V-88-057:on 880916,while Verifying Pressure Transmitter PT-458,bistables Tripped.Caused by Technician Error & Exceeding Shutdown by More than 48 H.Problems Encountered During Reactor Startup Listed | |
PNO-V-88-048, on 880717,unit Manually Tripped & Natural Cooldown Commenced as Result of Ground Fault in 12 Kv non- Vital Buses.Event Investigation Team Formed to Determine Location & Cause of Ground Fault | 18 July 1988 | PNO-V-88-048:on 880717,unit Manually Tripped & Natural Cooldown Commenced as Result of Ground Fault in 12 Kv non- Vital Buses.Event Investigation Team Formed to Determine Location & Cause of Ground Fault | |
PNO-V-88-031, on 880512,engineering Walkdowns of Pipe Whip Restraints Identified That Pressurizer Surge Line in Contact W/Upper Shim Pack of Pipe Whip Restraint 1.2.Possibly Caused by Difference Between Pressurizer & Hot Leg | 12 May 1988 | PNO-V-88-031:on 880512,engineering Walkdowns of Pipe Whip Restraints Identified That Pressurizer Surge Line in Contact W/Upper Shim Pack of Pipe Whip Restraint 1.2.Possibly Caused by Difference Between Pressurizer & Hot Leg | |
PNO-V-88-026, on 880418,workers Removed Flange from Pressurizer Relief Tank,Releasing Radioactive Noble Gas. Level of Activity Resulted in Containment Purge Isolation Signal.Release Caused by Inadequate Procedural Control | 19 April 1988 | PNO-V-88-026:on 880418,workers Removed Flange from Pressurizer Relief Tank,Releasing Radioactive Noble Gas. Level of Activity Resulted in Containment Purge Isolation Signal.Release Caused by Inadequate Procedural Control | |
PNO-V-88-001, on 880108,reactor Trip/Turbine Trip Occurred & Plant Shutdown for Greater than 48 H.Caused by Dirty Contact in Cable Connection to pre-amplifier.Containment Leakage Also Discovered.Manway Cover Bolts Torqued | 12 January 1988 | PNO-V-88-001:on 880108,reactor Trip/Turbine Trip Occurred & Plant Shutdown for Greater than 48 H.Caused by Dirty Contact in Cable Connection to pre-amplifier.Containment Leakage Also Discovered.Manway Cover Bolts Torqued | |
PNO-V-87-083, on 871213,reactor Tripped.Caused by Loss of Feed Water Pump 1-1.Cause of Trip Under Investigation. Variety of Maint Activities to Be Performed Before Restart | 14 December 1987 | PNO-V-87-083:on 871213,reactor Tripped.Caused by Loss of Feed Water Pump 1-1.Cause of Trip Under Investigation. Variety of Maint Activities to Be Performed Before Restart | |
PNO-V-87-081, on 871209,indication of Increased Leakage in Containment Identified.Caused by Leakage from Charging Sys Valve & Steam Generator Tubesheet Drain Valve Due to Abnormal Seal Performance.Seals Examined & Valves Repaired | 10 December 1987 | PNO-V-87-081:on 871209,indication of Increased Leakage in Containment Identified.Caused by Leakage from Charging Sys Valve & Steam Generator Tubesheet Drain Valve Due to Abnormal Seal Performance.Seals Examined & Valves Repaired | |
PNO-V-87-082, on 871210,fire Occurred in Temporary Tool Storage Trailer in Vicinity of Unit 2 Main Generator Transformers.Caused by 120 Volt Junction Box,Possibly Overloaded from Portable Space Heater.Fire Put Out | 10 December 1987 | PNO-V-87-082:on 871210,fire Occurred in Temporary Tool Storage Trailer in Vicinity of Unit 2 Main Generator Transformers.Caused by 120 Volt Junction Box,Possibly Overloaded from Portable Space Heater.Fire Put Out | |
PNO-V-87-074, on 871110,county Inadvertently Actuated Emergency Notification Sys(Sirens).Caused by Wrong Sequence Being Entered Into Sys While Performing Weekly Silent Test. Corrective Action Under Investigation | 10 November 1987 | PNO-V-87-074:on 871110,county Inadvertently Actuated Emergency Notification Sys(Sirens).Caused by Wrong Sequence Being Entered Into Sys While Performing Weekly Silent Test. Corrective Action Under Investigation | |
PNO-V-87-073, on 871107,unit Trip Manually Initiated.Caused by Failure of motor-operated Disconnect in Main Generator 25 Kv Isophase Bus C.Repair & Unit Outage Will Take Between 2 Wks & 2 Months,Depending on Availability of Parts | 9 November 1987 | PNO-V-87-073:on 871107,unit Trip Manually Initiated.Caused by Failure of motor-operated Disconnect in Main Generator 25 Kv Isophase Bus C.Repair & Unit Outage Will Take Between 2 Wks & 2 Months,Depending on Availability of Parts | Fire Watch |
PNO-V-87-066, on 871006,while Performing Periodic Surveillance Testing of Control Rods at 100% Power,Rod Control Urgent Failure Alarm Received on Shutdown Bank A. Caused by Blown Fuses.Fuses Replaced & Alarm Cleared | 6 October 1987 | PNO-V-87-066:on 871006,while Performing Periodic Surveillance Testing of Control Rods at 100% Power,Rod Control Urgent Failure Alarm Received on Shutdown Bank A. Caused by Blown Fuses.Fuses Replaced & Alarm Cleared | |
PNO-V-87-062, on 870928,unit Shut Down to Repair Boron Injection Tank Leaking Pressure Relief Valve Psv 8852. Leaking Relief Valve Removed & Blank Flange Put Over Line. Plant Remains in Shutdown Status | 29 September 1987 | PNO-V-87-062:on 870928,unit Shut Down to Repair Boron Injection Tank Leaking Pressure Relief Valve Psv 8852. Leaking Relief Valve Removed & Blank Flange Put Over Line. Plant Remains in Shutdown Status | |
PNO-V-87-057, on 870824,Oregon State Agreement Program Director,R Paris,Informed NRC That State Employee Union Voted to Strike on 870913.If Settlement Not Reached Prior to Walk Out,Managers Will Handle Radioactive Matls Program | 24 August 1987 | PNO-V-87-057:on 870824,Oregon State Agreement Program Director,R Paris,Informed NRC That State Employee Union Voted to Strike on 870913.If Settlement Not Reached Prior to Walk Out,Managers Will Handle Radioactive Matls Program | |
PNO-V-87-053, on 870723,high Radiation Alarm Automatically Diverted Liquid Radwaste Flow to Storage Tank.Licensee Determining Root Cause.Chemical Drain Tank Properly Recirculated & Sampled Prior to Discharge Per Procedure | 24 July 1987 | PNO-V-87-053:on 870723,high Radiation Alarm Automatically Diverted Liquid Radwaste Flow to Storage Tank.Licensee Determining Root Cause.Chemical Drain Tank Properly Recirculated & Sampled Prior to Discharge Per Procedure | |
PNO-V-87-051, on 870714,reactor Trip & Safety Injection from 12% Power Occurred.Caused by turbine-generator Trip Due to High Steam Generator Water Level & Flickering High Steam Flow Bistables,Respectively.Root Causes Under Investigation | 14 July 1987 | PNO-V-87-051:on 870714,reactor Trip & Safety Injection from 12% Power Occurred.Caused by turbine-generator Trip Due to High Steam Generator Water Level & Flickering High Steam Flow Bistables,Respectively.Root Causes Under Investigation | |
PNO-V-87-048A, on 870702,significant Unexpected Erosion on Straight Sections of safety-related Feed Sys Piping Identified.Licensee Plans to Replace Piping Prior to Restart.Inpo Requested to Distribute Findings Via Network | 7 July 1987 | PNO-V-87-048A:on 870702,significant Unexpected Erosion on Straight Sections of safety-related Feed Sys Piping Identified.Licensee Plans to Replace Piping Prior to Restart.Inpo Requested to Distribute Findings Via Network | |
PNO-V-87-048, during Insp of Main Feedwater Sys in June 1987, Licensee Found Some Indications of Pipe Wall Thinning.Caused by Flow Transition & Turbulence.Licensee Replacing All Piping W/Below Min Wall Thickness Indications | 30 June 1987 | PNO-V-87-048:during Insp of Main Feedwater Sys in June 1987, Licensee Found Some Indications of Pipe Wall Thinning.Caused by Flow Transition & Turbulence.Licensee Replacing All Piping W/Below Min Wall Thickness Indications | Nondestructive Examination |
ML20215F900 | 17 June 1987 | PNS-V-87-005:on 870617,American Protective Svc Notified Util That Security Personnel on Strike Over Monetary Benefits. Licensee Capable to Meet Security Staffing Requirements Through Use of Proprietary Security Personnel | |
PNO-V-87-045, licensee Discovered Seperation Between Base Plate Grout & Concrete on Support SS-81 on Main Steam Line B.On 870616,dynamic Analysis Reperformed for Main Steam Supports.Supports Reinstalled W/Proper Design Loads | 16 June 1987 | PNO-V-87-045:licensee Discovered Seperation Between Base Plate Grout & Concrete on Support SS-81 on Main Steam Line B.On 870616,dynamic Analysis Reperformed for Main Steam Supports.Supports Reinstalled W/Proper Design Loads | |
PNO-V-87-041, on 870602,engineer in Containment Noted Weepage from RHR Sys Line While RHR in Svc.Cause of Effect Undetermined.Licensee Preparing Work Orders to Isolate, Examine & Repair Weld | 3 June 1987 | PNO-V-87-041:on 870602,engineer in Containment Noted Weepage from RHR Sys Line While RHR in Svc.Cause of Effect Undetermined.Licensee Preparing Work Orders to Isolate, Examine & Repair Weld | Boric Acid |
PNO-V-87-040, on 870523,360 Degrees Circumferential Break of SI Accumulator a Fill Line Occurred While Transferring Water from SI Accumulator a to D.Caused by Low Cycle,High Fatigue. Util Conducting Analyses to Determine Force & Fatigue Cycl | 26 May 1987 | PNO-V-87-040:on 870523,360 Degrees Circumferential Break of SI Accumulator a Fill Line Occurred While Transferring Water from SI Accumulator a to D.Caused by Low Cycle,High Fatigue. Util Conducting Analyses to Determine Force & Fatigue Cycl | Hydrostatic |
PNO-V-87-037, on 870512,fatigue Fracture Occurred on 1-inch Safety Injection Fill Line on Accumulator Tank a & 2,000 Gallons of 2,000 Ppm Borated Water Drained Onto Containment Floor.By 870514,two Addl Accumulator Tanks Found W/Cracks | 14 May 1987 | PNO-V-87-037:on 870512,fatigue Fracture Occurred on 1-inch Safety Injection Fill Line on Accumulator Tank a & 2,000 Gallons of 2,000 Ppm Borated Water Drained Onto Containment Floor.By 870514,two Addl Accumulator Tanks Found W/Cracks | |
PNO-V-87-038, on 870513,female Air Lock Operator Received Injury to Neck While Opening Air Lock Door to Transfer Matl from Containment.Operator Transported Offsite for Medical Attention.No Serious Injuries or Contamination Found | 14 May 1987 | PNO-V-87-038:on 870513,female Air Lock Operator Received Injury to Neck While Opening Air Lock Door to Transfer Matl from Containment.Operator Transported Offsite for Medical Attention.No Serious Injuries or Contamination Found | |
PNO-V-87-035, on 870507,individual W/Contamination Level of 160,000 Dpm/Square Centimeters on Knees Became Ill While Removing Protective Clothing Worn for Decontaminating Equipment.Individual Transported to Hosp & Decontaminated | 8 May 1987 | PNO-V-87-035:on 870507,individual W/Contamination Level of 160,000 Dpm/Square Centimeters on Knees Became Ill While Removing Protective Clothing Worn for Decontaminating Equipment.Individual Transported to Hosp & Decontaminated | |
PNO-V-87-031A, on 870417,licensee Reported Potential Foot Exposure of Plant Worker Exceeding 18.75 Rem Limit.Staff Retrained in Precautions to Minimize Exposure from Radioactive Matl & Appropriate Radiological Control Started | 29 April 1987 | PNO-V-87-031A:on 870417,licensee Reported Potential Foot Exposure of Plant Worker Exceeding 18.75 Rem Limit.Staff Retrained in Precautions to Minimize Exposure from Radioactive Matl & Appropriate Radiological Control Started | |
ML20209D513 | 23 April 1987 | Updated PNO-V-87-030B:on 870421,onsite Phase of AIT Team Special Insp Into 870410 Loss of Suction to RHR Sys While in half-loop Concluded W/Meeting at Site | |
PNO-V-87-030A, on 870415,Region V Augmented Insp Team Commenced Insp Activities Re 870410 Loss of Suction to RHR While at Half Loop.Team Expects to Stay Onsite Through 870421.Summary of Sequence of Event Encl | 20 April 1987 | PNO-V-87-030A:on 870415,Region V Augmented Insp Team Commenced Insp Activities Re 870410 Loss of Suction to RHR While at Half Loop.Team Expects to Stay Onsite Through 870421.Summary of Sequence of Event Encl | Boric Acid |
PNO-V-87-031, on 870417,licensee Reported Potential Foot Exposure of Plant Worker Exceeding 18.75 Rem Limit.Caused by Dispersal of Irradiated Fuel Fragments.Work Stopped in Containment Bldg.Investigation Initiated | 17 April 1987 | PNO-V-87-031:on 870417,licensee Reported Potential Foot Exposure of Plant Worker Exceeding 18.75 Rem Limit.Caused by Dispersal of Irradiated Fuel Fragments.Work Stopped in Containment Bldg.Investigation Initiated | |
PNO-V-87-029A, on 870414,licensee Reported That Degraded Pellet Between Reactor Vessel & Head Flange Source of Radioactive Contamination of Area & Personnel Inside Containment Bldg on 870409.Decontamination Efforts Ongoing | 14 April 1987 | PNO-V-87-029A:on 870414,licensee Reported That Degraded Pellet Between Reactor Vessel & Head Flange Source of Radioactive Contamination of Area & Personnel Inside Containment Bldg on 870409.Decontamination Efforts Ongoing | |
PNO-V-87-030, on 870410,RHR Sys Capability Lost for Approx 90 Minutes.Caused by Entrainment of Air within RHR Pumps When RCS Water Level Dropped Due to Water Leakage Through Two Valves.Augmented Insp Team Dispatched | 13 April 1987 | PNO-V-87-030:on 870410,RHR Sys Capability Lost for Approx 90 Minutes.Caused by Entrainment of Air within RHR Pumps When RCS Water Level Dropped Due to Water Leakage Through Two Valves.Augmented Insp Team Dispatched | |
PNO-V-87-029, on 870409,while Installing Reactor Stud Plugs, Release of Radioactivity Occurred Resulting in 21 Workers Experiencing Personal Contamination.Work in Reactor Cavity Stopped Until Source of Problem Identified | 10 April 1987 | PNO-V-87-029:on 870409,while Installing Reactor Stud Plugs, Release of Radioactivity Occurred Resulting in 21 Workers Experiencing Personal Contamination.Work in Reactor Cavity Stopped Until Source of Problem Identified | |
PNO-V-87-028, on 870403,reactor Tripped from 12% Power During Shut Down for First Refueling Outage.Caused by Flicker of High Steam Flow Bistables Coincident w/lo-lo T Average.Investigation Continuing | 6 April 1987 | PNO-V-87-028:on 870403,reactor Tripped from 12% Power During Shut Down for First Refueling Outage.Caused by Flicker of High Steam Flow Bistables Coincident w/lo-lo T Average.Investigation Continuing |