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Issue date | Title | Topic | |
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ML23241A002 | 25 August 2023 | Paragon Final Part 21 Report on Defect with Eaton/Cutler Hammer Size 4 and 5 Freedom Series Contactors Modified by Paragon with Special Coils And/Or with RTV to Improve the Securing of Shading Coils | |
ML23221A370 | 3 August 2023 | Paragon Energy Solutions, 10CFR Part 21 Initial Notification: P21-08032023-IN, Rev. 0 | |
ML23038A019 | 6 February 2023 | Curtiss-Wright Part 21 Notification for Qualtech Np Supplied Eaton TMR5 Timing Relays | |
ML22341A032 | 30 November 2022 | 10 CFR Part 21 Notification from Curtiss-Wright Nuclear Division for Qualtech Np Supplied Eaton TRM5 Timing Relays | |
ML21168A217 | 17 June 2021 | GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | Operability Determination Fuel cladding |
M210077, GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | 17 June 2021 | GE Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Fuel Support Side Entry Orifice Meta-Stable Flow for 2 Beam Locations in the BWR/6 Reactors | Operability Determination Fuel cladding |
ML20366A048 | 7 December 2020 | 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10 CFR21-0114, Rev. 1 | Safe Shutdown |
ML20366A047 | 18 November 2020 | Curtiss-Wright 10 CFR Part 21 Notification for SF-1154 Hydraulic Fluid Batch 17BLVS293 | |
M200087, GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | 24 June 2020 | GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | Operability Determination Fuel cladding |
ML20176A432 | 24 June 2020 | GE-Hitachi Nuclear Energy Americas, LLC - 10 CFR Part 21.21(d)-Reportable Condition: Non-Conservative BWR/6 Side Entry Orifice (SEO) Loss Coefficients | Operability Determination Fuel cladding |
ML20049A075 | 11 February 2020 | C&D Technologies, Inc. -10 CFR Part 21 Evaluation Regarding Container Failure in KCR-07 Batteries | |
ML19121A155 | 15 April 2019 | Curtiss-Wright Nuclear Division, Enertech - 10 CFR Part 21 Notification for SF-1154 Hydraulic Fluid | |
ML17194A825 | 11 July 2017 | Part 21 Report Re Wedge Pin Failure in Anchor Darling Motor Operated Double Disc Gate Valves with Threaded Stem to Upper Wedge Connections | Anchor Darling |
ML17090A398 | 27 March 2017 | Engine Systems, Inc. - Part 21 Report Regarding Identification of Failed Diode Surge Suppressor with Internal Manufacturing Defect | |
ML17081A453 | 20 March 2017 | Part 21 - Plastic Jar Dedication Sampling | |
ML17055C177 | 9 February 2017 | 10 CFR 21 Evaluation Regarding Design Basis Calculation Error Using FL0-2D Software | |
ML17026A414 | 20 January 2017 | C&D Technologies, Inc. - Part 21 - Plastic Jar Dedication Sampling | |
ML17032A080 | 30 December 2016 | Engine Systems, Inc., 10CFR21 Reporting of Defects and Non-Compliance, Report No. 10CFR21-0114, Rev. 0 | Safe Shutdown |
ML17006A010 | 29 December 2016 | Engine Systems, Inc. - Part 21 Issues Identified with the Enterprise Diesel Engine Subcover | Safe Shutdown |
ML17006A014 | 13 December 2016 | Enercon - Part 21 - Notification-Design Basis Errors Using Flo-2D Software | |
ML16342A981 | 23 November 2016 | Enercon - Part 21 Notification - Design Basis Errors Using FLO-2D Software | |
ML16251A098 | 2 September 2016 | Part 21 - Potential Failure of Battery System Connections | |
ML16252A274 | 29 August 2016 | Azz/Nli - Part 21 Report - Potential Allen Bradley Timing Relay | Commercial Grade |
ML16243A474 | 26 August 2016 | Potential Part 21 Unqualified Component in Certain Allen Bradley Timing Relays | Commercial Grade |
ML16232A604 | 15 August 2016 | Potentially Unqualified Component in Certain Allen Bradley Timing Relays | Commercial Grade |
ML16238A186 | 15 August 2016 | Update - Report of Potential l0CFR Part 21, Allen Bradley Timing Relay Model 700RTC-NRC Event Number 51030, Accession Number ML15134A016 | Commercial Grade |
ML16188A374 | 30 June 2016 | Part 21 - Inadequate Swaging and Adherence of Silicone O-Ring and Silicone PAD Soft Seat Main Disc and Pilot Disc Assemblies | |
ML16154A207 | 26 May 2016 | Part 21, Azz/Nli Nuclear Logistics, Inc., Potentially Unqualified Component in Certain Allen Bradley Timing Relays Model 700RTC | Commercial Grade |
ML16111A420 | 8 April 2016 | Part 21 Report No. P21-04302015, Rev. 1 Regarding Potentially Unqualified Component in Certain Allen Bradley Timing Relays, Per Browns Ferry, Ginna, Millstone, Nine Mile Point, North Anna, Ft. Calhoun, Perry, River Bend, South Texas Project | Commercial Grade |
ML16098A446 | 22 March 2016 | United Controls International - Part 21 Report Regarding Defective Fuses, Per Perry Nuclear Power Plant | |
ML15217A303 | 4 August 2015 | Notification of Part 21 - Report - Ferraz Shawmut/Mersen Fuses P/N: AJT25 and AJT60 | |
ML15140A218 | 11 May 2015 | Part 21 Report Regarding Defect Identified 6 Inch Gear Operated Ball Valves (Part Number GBV-B2-60-0020 & GBV-B2-60-0112), Notification No. 15-1 | |
ML15134A016 | 1 May 2015 | Part 21 Report Regarding Potentially Unqualified Component in Certain Allen Bradley Timing Relays | Commercial Grade |
ML15159A568 | 30 April 2015 | Report of Potential 10CFR Part 21, Allen Bradley Timing Relay Model 700RTC | Commercial Grade |
ML15022A650 | 20 January 2015 | Letter from Steven R. Eisenberg USNRC 10CFR Part 21 Notification | |
ML14274A052 | 22 September 2014 | Final Report 10CFR Part 21 Evaluation Regarding Misaligned Separators in LCR-25 Standby Batteries, Revision 1 - Original Letter Did Not Include the List of Affected Utilities | |
ML14210A010 | 23 July 2014 | Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve | Safe Shutdown Shutdown Margin Scram Discharge Volume Failure to Scram Affidavit |
ML14204A707 | 23 July 2014 | Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV | Affidavit |
ML14204A708 | 23 July 2014 | Enclosure 2, Description of Closure Evaluation, Non-Proprietary Information - Class I (Public) | Safe Shutdown Shutdown Margin Scram Discharge Volume Failure to Scram |
ML14134A079 | 8 May 2014 | Part 21 - Potential Defect in NUS-710DU Trip Unit to Produce a Valid Trip Output Signal | |
ML14139A259 | 8 May 2014 | 10 CFR Part 21 Report Notification, NUS710DU Trip Units | |
ML13324A391 | 8 November 2013 | Part 21 - Machining Error Identified in Geared Limit Switches | |
ML13284A084 | 3 October 2013 | Deficiency Report from Baldor Electric Co., on Nuclear Nonconformance Event No. 49302 | |
ML13165A342 | 12 June 2013 | 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers | |
ML13064A012 | 25 February 2013 | Notification of Potential Part 21 Report Re Wedge Pin Failure of an Anchor/Darling Double-Disc Gate Valve | Anchor Darling |
ML13044A075 | 8 February 2013 | Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology | Power Uprate |
ML13042A096 | 8 February 2013 | Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Error in Main Steam Line High Flow Calculational Methodology | Power Uprate |
ML12348A136 | 13 December 2012 | Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers | |
ML12352A123 | 13 December 2012 | 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers | |
ML12347A308 | 12 December 2012 | Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology |