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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
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MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N4381999-10-25025 October 1999 Safety Evaluation Supporting Amend 17 to License DPR-9 ML20217P3551999-10-22022 October 1999 LER 99-S01-00:on 990922,loaded 9mm Handgun Was Discovered on Truck Cargo Area of Vehicle Inside Protected Area.Caused by Inadequate Vehicle Search.Guidance in Procedures & Security Training to Address Multiple Vehicle Searches Was Provided NRC-99-0095, Monthly Operating Rept for Sept 1999 for Fermi 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fermi 2.With NRC-99-0067, Monthly Operating Rept for Aug 1999 for Fermi 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fermi 2.With NRC-99-0065, Monthly Operating Rept for July 1999 for Fermi 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fermi 2.With NRC-99-0088, Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with1999-06-30030 June 1999 Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with NRC-99-0064, Monthly Operating Rept for June 1999 for Fermi 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fermi 2.With NRC-99-0062, Monthly Operating Rept for May 1999 for Fermi 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fermi 2.With ML20206J9301999-05-10010 May 1999 SER Concluding That Util Adequately Addressed Actions Requested in GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Powered-Operated Gate Valves ML20206G5081999-05-0505 May 1999 Safety Evaluation Approving Request for Relief PR-8,Rev 2 on Basis That Licensee Committed to Meet All Related Requirements of ASME OM-6 Std & PR-12 on Basis That Proposed Alternative Will Provide Acceptable Level of Safety NRC-99-0022, Monthly Operating Rept for Apr 1999 for Fermi 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fermi 2.With ML20205Q7141999-04-15015 April 1999 Safety Evaluation Supporting Amend 16 to License DPR-9 ML20205P9721999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fermi 2 ML20204E0371999-03-17017 March 1999 Safety Evaluation Accepting Licensee Request for NRC Approval of Alternative Rv Weld Exam,Per Provisions of 10CFR50.55a(a)(3)(i) & 10CFR50.55a(g)(6)(ii)(A)(5) for Plant,Unit 2 for 40-month Period ML20204D0361999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fermi 2 ML20198S3341999-01-0606 January 1999 Safety Evaluation Supporting Amend 15 to License DPR-9 NRC-99-0005, Monthly Operating Rept for Dec 1998 for Fermi 2.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fermi 2.With ML20207B7491998-12-31031 December 1998 1998 Annual Operating Rept for Fermi 2 ML20205Q9621998-12-31031 December 1998 Revised Monthly Operating Rept for Dec 1998 for Fermi 2 NRC-99-0021, 1998 Annual Financial Rept for Detroit Edison Co. with1998-12-31031 December 1998 1998 Annual Financial Rept for Detroit Edison Co. with NRC-98-0153, Monthly Operating Rept for Nov 1998 for Fermi 2.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fermi 2.With NRC-98-0160, Monthly Operating Rept for Oct 1998 for Fermi 2.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fermi 2.With ML20154R2331998-10-21021 October 1998 Safety Evaluation Supporting Amend 13 to License DPR-9 ML20154L1031998-10-14014 October 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode NRC-98-0139, Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With ML20154H8161998-09-30030 September 1998 Rev 0 to COLR Cycle 7 for Fermi 2 ML20153B8811998-09-18018 September 1998 Safety Evaluation Accepting Request for Relief from Certain Requirements of ASME Boiler & Pressure Vessel Code,Section Xi,For Plant,Unit 2 ML20151X0651998-09-11011 September 1998 Safety Evaluation Re Inservice Testing Program Relief Request VR-63 for Plant NRC-98-0111, Monthly Operating Rept for Aug 1998 for Fermi 2.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fermi 2.With ML20153B7921998-08-31031 August 1998 Rev 0 to Fermi 1 Sar ML20237E1171998-08-25025 August 1998 Safety Evaluation Accepting Licensee Relief Requests for First 10-yr Interval Inservice Insp Nondestructive Exam Program ML20236X8611998-08-0505 August 1998 SER Related to Revised Feedwater Nozzle Analysis to Facility Operating License NPF-43,Enrico Fermi Nuclear Power Plant, Unit 2 NRC-98-0109, Monthly Operating Rept for July 1998 for Fermi 21998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Fermi 2 ML20236K3261998-07-0101 July 1998 SER Accepting Licensee Response Related to Revised Feedwater Nozzle Analysis to License NPF-43 for Enrico Fermi Nuclear Power Plant,Unit 2 NRC-98-0097, Monthly Operating Rept for June 1998 for Fermi,Unit 21998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Fermi,Unit 2 NRC-98-0127, Annual Rept for Period 970701-9806301998-06-30030 June 1998 Annual Rept for Period 970701-980630 NRC-98-0079, Monthly Operating Rept for May 1998 for Fermi 21998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Fermi 2 NRC-98-0076, Monthly Operating Rept for Apr 1998 for Fermi 21998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Fermi 2 NRC-98-0072, Monthly Operating Rept for Mar 1998 for Fermi 21998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Fermi 2 NRC-98-0050, Monthly Operating Rept for Feb 1998 for Fermi 21998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Fermi 2 NRC-98-0019, Monthly Operating Rept for Jan 1998 for Fermi 21998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Fermi 2 ML20198L4241998-01-0808 January 1998 Safety Evaluation Accepting Proposed Rev 2 to Relief Request VR-51 Under Fermi 2 Pump & Valve Inservice Testing Program Per 10CFR50.55a(f)(6)(i) for First 10-yr Interval NRC-98-0015, Monthly Operating Rept for Dec 1997 for Fermi 21997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Fermi 2 ML20217N3821997-12-31031 December 1997 Annual Operating Rept for 970101-1231 NRC-98-0053, 1997 Annual Financial Rept for Detroit Edison Company1997-12-31031 December 1997 1997 Annual Financial Rept for Detroit Edison Company ML20205Q9601997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Fermi 2 NRC-97-0141, Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility1997-12-23023 December 1997 Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility ML20197A9921997-12-15015 December 1997 Rev 0 to Efp,Unit 1 Fermi 1 Sar NRC-97-0131, Monthly Operating Rept for Nov 1997 for Fermi 21997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Fermi 2 ML20248H1151997-10-31031 October 1997 Rev 1 to Colr,Cycle 6 for Fermi 2 1999-09-30
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EC ISOn '~." 10CrR30.73 Hay 24, 1991 NRC-91-0069 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555
Reference:
Fermi 2 NRC Docket No. 50-341 NRC License No. NPF-43
Subject:
Licensee Event Report (LER) No. 90-012-01 Please find enclosed LER No. 90-012-01, dated May 24, 1991, for a reportable event that occurred on October 16, 1990. A copy of this LER is also being sent to the Regional Administrator, USNRC Region Ill.
If you have any questions, please contact Barbara Siemasz, Compliance Engineer, at (313) 586-1683 Sincerely, 7
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Enclosure:
NRC Forms 366, 366A cc: A. B. Davis J. R. Eckert R. W. DeFayette W. G. Rogers J. F. Stang Wayne County Emergency Management Division l
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y33 On October 16, 1990, at 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br />, the High Pressure Coolant Injection System (HPCI) was found to have a failed channel for HPCI Steam Line Differential Pressure High, Division 1 (Lcgic A). The system was in st,andby at the time of discovery of the channel failure. In compliance with Technical Specification action statement requirements, the channel was declared inoperable. The HPCI System was subsequently declared inoperable and the appropriate Limiting Condition for Operation was entered.
Initial investigation revealed that one or both internal circuit boards on differential pressure transmitter, E41-N057A, had failed. <
The failed circuit. boards were sent to Rosemount Inc., for failure I analysis to aid in deternining the root cause of the channel failure.1 Besults of this analysis indicated a capacitor on the amplifier I circuit board failed due to a short circuit across the capacitor i pl a te.> . I The transmitter was repaired. Post maintenance surveillance testing demonstrated the effectiveness of the repair wcrk and the channel was declared operable. Subsequently, HPCI was declared operable.
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Initial Plant Conditions:
Operational Condition: 1 (Power Operation)
Reactor Power: 96.1%
Reactor Pressure: 999 psig Reactor Temperatures 535 F Description of Event:
At 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br /> on October 16, 1990, the High Pressure Coolant Injection System ((HPCI)(BJ)] was found to have a failed channel for HPCI Steam Line Differential High Pressure, Division I (Logic A). The failed channel was found during the performance of a channel check in accordance with surveillance 24.000.02, "Shiftly, Daily, Weekly and Situation Required Surveillances." 'the failed Division I channel was immediately declared inoperable and the 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> action statement for Technical Specification (TS) 3 3 2.b was entered. Tne 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> action statement subsequently expired, and Action 23 or TS 3 3 2-1 was entered. This requires the isolation valves (ISV) for HPCI to be closed within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and the system to be declared inoperable. Prior to reaching the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> Technical Specification time limit, troubleshooting of the failed Division I channel was conducted by performing surveillance 44.020.203, "NSSSS-HPCI Steam Line Flow Division I, Calibration." At this time, all other Emergency Core i Cooling Systems (ECCS) and th 'cactor Core Isolation Coo.ing l
((RCIC)(BN)] system were verirled operable as required by TS l 3 5.1.c.1, Action c.1. Data gathered during the performance of l
44.020,203 showed that differential pressure transmitt(r (PT) ,
l E41-N057A, was malfunctionir,g and had caused the failed channel check. At 1957 hours0.0227 days <br />0.544 hours <br />0.00324 weeks <br />7.446385e-4 months <br />, HPCI was declared inoperable and HPCI isolation valves, E41-F002 and E41-F042, were de-energized in the closed position in accordance with TS 3 3 2-1. Action 23 A Deviation 0:'ent l
Report (DER .3-0611) was written to investigate and evaluate the Division I channel failure.
At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on October 17, 1990, after repair and successful testing of differential pressure transmitter E41-N057A, the HPCI system was declared operable.
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initial tuvestigation of the failed Division i channel revealed that l one or both circuit boards internal to differential pressure I transmitter E41-N057A had failed. The suspect circuit boards were I sent to the manufacturer, Rosemount Inc., for failure analysis to I aid in determining the root cause of the channel failure. The I results of this analysis indicate a capacitor on the amplifier l circuit board failed due to a short circuit. The likely cause of I the capacitor short circuit was metal migration bet. ween the I capacitor plates. Along with the failure analysis, Hosemount Inc. I reviewed data relating to similar transmitter failures and concluded I that this capacitor failure was random. 1 Analysis of. Event:
The Division I channel failure rendered inoperable the capability to detect a HPCI steam line break, therefore HPCI, as required by Technical Specifications, was isolated and declared inoperable. The ,
appropriate Technical Specification actions were met, following this event. While HPCI was inoperable, the Automatic Depressurization System (part of ECCS) would have been available to reduce reactor pressure to the point where Low Pressure Coolant Injection (BO) and Core Spray (BH) could have been used. RCIC was available to provide 1 l reactor water inventory control. If an event had occurred which I would have challenged HPCI, the other ECCS systems and RCIC would have fulfilled this safet.y function.
Based upon the availability of adequate ECCS and RCIC, this event did not impact the safe operation of the plant, or the health and safety of the public.
Corrective Actions:
Initial investigation of t.he failed Division I channel revealed that one or both circuit boards internal to different.ial pressure transmitter E41-N057A had failed. The suspect circuit boards were replaced. The effectiveness of the repair work was verified by post maintenance surveillance testing. Along with the failure analysis, I Rosemount Inc. reviewed data relating to similar transmitter I failures and concluded that this capacitor failure was randon. I hRC f me 365A 44t0
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Previous Similar Events:
This is the only reportable event due to a failed circuit twaard on a i differential pressure transmitter. 1 Failed Component Data:
E41-N057A, Rosemount Inc. Differential Pr essure Transnitter, Model No.
1153DB6Rc serial No. 413862.
hkC f oem M6A 164W
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