Similar Documents at Fermi |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
[Table view] Category:RO)
MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N4381999-10-25025 October 1999 Safety Evaluation Supporting Amend 17 to License DPR-9 ML20217P3551999-10-22022 October 1999 LER 99-S01-00:on 990922,loaded 9mm Handgun Was Discovered on Truck Cargo Area of Vehicle Inside Protected Area.Caused by Inadequate Vehicle Search.Guidance in Procedures & Security Training to Address Multiple Vehicle Searches Was Provided NRC-99-0095, Monthly Operating Rept for Sept 1999 for Fermi 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fermi 2.With NRC-99-0067, Monthly Operating Rept for Aug 1999 for Fermi 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fermi 2.With NRC-99-0065, Monthly Operating Rept for July 1999 for Fermi 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fermi 2.With NRC-99-0088, Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with1999-06-30030 June 1999 Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with NRC-99-0064, Monthly Operating Rept for June 1999 for Fermi 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fermi 2.With NRC-99-0062, Monthly Operating Rept for May 1999 for Fermi 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fermi 2.With ML20206J9301999-05-10010 May 1999 SER Concluding That Util Adequately Addressed Actions Requested in GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Powered-Operated Gate Valves ML20206G5081999-05-0505 May 1999 Safety Evaluation Approving Request for Relief PR-8,Rev 2 on Basis That Licensee Committed to Meet All Related Requirements of ASME OM-6 Std & PR-12 on Basis That Proposed Alternative Will Provide Acceptable Level of Safety NRC-99-0022, Monthly Operating Rept for Apr 1999 for Fermi 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fermi 2.With ML20205Q7141999-04-15015 April 1999 Safety Evaluation Supporting Amend 16 to License DPR-9 ML20205P9721999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fermi 2 ML20204E0371999-03-17017 March 1999 Safety Evaluation Accepting Licensee Request for NRC Approval of Alternative Rv Weld Exam,Per Provisions of 10CFR50.55a(a)(3)(i) & 10CFR50.55a(g)(6)(ii)(A)(5) for Plant,Unit 2 for 40-month Period ML20204D0361999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fermi 2 ML20198S3341999-01-0606 January 1999 Safety Evaluation Supporting Amend 15 to License DPR-9 NRC-99-0005, Monthly Operating Rept for Dec 1998 for Fermi 2.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fermi 2.With ML20207B7491998-12-31031 December 1998 1998 Annual Operating Rept for Fermi 2 ML20205Q9621998-12-31031 December 1998 Revised Monthly Operating Rept for Dec 1998 for Fermi 2 NRC-99-0021, 1998 Annual Financial Rept for Detroit Edison Co. with1998-12-31031 December 1998 1998 Annual Financial Rept for Detroit Edison Co. with NRC-98-0153, Monthly Operating Rept for Nov 1998 for Fermi 2.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fermi 2.With NRC-98-0160, Monthly Operating Rept for Oct 1998 for Fermi 2.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fermi 2.With ML20154R2331998-10-21021 October 1998 Safety Evaluation Supporting Amend 13 to License DPR-9 ML20154L1031998-10-14014 October 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode NRC-98-0139, Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With ML20154H8161998-09-30030 September 1998 Rev 0 to COLR Cycle 7 for Fermi 2 ML20153B8811998-09-18018 September 1998 Safety Evaluation Accepting Request for Relief from Certain Requirements of ASME Boiler & Pressure Vessel Code,Section Xi,For Plant,Unit 2 ML20151X0651998-09-11011 September 1998 Safety Evaluation Re Inservice Testing Program Relief Request VR-63 for Plant NRC-98-0111, Monthly Operating Rept for Aug 1998 for Fermi 2.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fermi 2.With ML20153B7921998-08-31031 August 1998 Rev 0 to Fermi 1 Sar ML20237E1171998-08-25025 August 1998 Safety Evaluation Accepting Licensee Relief Requests for First 10-yr Interval Inservice Insp Nondestructive Exam Program ML20236X8611998-08-0505 August 1998 SER Related to Revised Feedwater Nozzle Analysis to Facility Operating License NPF-43,Enrico Fermi Nuclear Power Plant, Unit 2 NRC-98-0109, Monthly Operating Rept for July 1998 for Fermi 21998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Fermi 2 ML20236K3261998-07-0101 July 1998 SER Accepting Licensee Response Related to Revised Feedwater Nozzle Analysis to License NPF-43 for Enrico Fermi Nuclear Power Plant,Unit 2 NRC-98-0097, Monthly Operating Rept for June 1998 for Fermi,Unit 21998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Fermi,Unit 2 NRC-98-0127, Annual Rept for Period 970701-9806301998-06-30030 June 1998 Annual Rept for Period 970701-980630 NRC-98-0079, Monthly Operating Rept for May 1998 for Fermi 21998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Fermi 2 NRC-98-0076, Monthly Operating Rept for Apr 1998 for Fermi 21998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Fermi 2 NRC-98-0072, Monthly Operating Rept for Mar 1998 for Fermi 21998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Fermi 2 NRC-98-0050, Monthly Operating Rept for Feb 1998 for Fermi 21998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Fermi 2 NRC-98-0019, Monthly Operating Rept for Jan 1998 for Fermi 21998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Fermi 2 ML20198L4241998-01-0808 January 1998 Safety Evaluation Accepting Proposed Rev 2 to Relief Request VR-51 Under Fermi 2 Pump & Valve Inservice Testing Program Per 10CFR50.55a(f)(6)(i) for First 10-yr Interval NRC-98-0015, Monthly Operating Rept for Dec 1997 for Fermi 21997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Fermi 2 ML20217N3821997-12-31031 December 1997 Annual Operating Rept for 970101-1231 NRC-98-0053, 1997 Annual Financial Rept for Detroit Edison Company1997-12-31031 December 1997 1997 Annual Financial Rept for Detroit Edison Company ML20205Q9601997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Fermi 2 NRC-97-0141, Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility1997-12-23023 December 1997 Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility ML20197A9921997-12-15015 December 1997 Rev 0 to Efp,Unit 1 Fermi 1 Sar NRC-97-0131, Monthly Operating Rept for Nov 1997 for Fermi 21997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Fermi 2 ML20248H1151997-10-31031 October 1997 Rev 1 to Colr,Cycle 6 for Fermi 2 1999-09-30
[Table view] |
Text
_. . _ .. . . _ ___.___ _ . . . _
~
1 c:
D
WHh m B.orser 250i'#4b.
10CrR50.73 ,, H 7"., .
u Detroi.t
== i
..rmie 64JO North Dem Highwal Nuclear IQAn 8vv3 I Newport cAcnio.n (3'31686 4
l l
December 21 1989 -j NRC-89-0260 1 I
U. S. Nuclear Regulatory Commission ;
Attention: ~ Document Control Desk
. Washington, D.C. 20555
Reference:
(1) Fermi 2 NRC Docket No. 50-341 Facility Operating License No.-NPF-43 (2) Transmittal of Licensee Event Report. r
. 89-021-00, dated October 6.-1909.
NRC-89-0185
Subject:
-Licensee Event-Report (LER) No. 89-021-01 ;
Please find' enclosed LER No. 89-021-01.. dated. December .
- 21. 1989, for a reportable event that occurred on' l September 6. 1989. . A supplement is being submitted to-7 report final results of Type A. B. and C testing and the corrective actions for Type B E C testing failures as reported in the original LER. A copy of this LER is.also being sent to the Regional Administrator. USNRC Region III.
If you have any questions, please. contact Gordon Nader at (313) 586-4513.
I Sincerely, y ~ <
b
Enclosure:
NRC Forms 366. 366A l cc: A. B. Davis l
J. R. Eckert l
R. W. Defayette/W. L. Axelson W. G. Rogers J. F. Stang Wayne County Emergency -
Management Division 8912280116 PDR 891221 S
ADOCK 05000341 72 > >
PDC i g L ._ ,__. - . . . . _ . . _ _ _ . _ . , . . ~ . .
-i N C to, mate U.S touCLEMt 1.51ULAToRY COMMISSfoN a
APPRovto OMS No 3106 4104 LICENSEE EVENT REPORT (LER) '"a'*8"
- ACILITv hAME til oOCKET NUMSSR Qi FAGE 2 Fermi 2 elTLt der o is I o io I o i 314 l 1 1IOFl015 Local / Integrated Leak Rate Testing Results I_ event oATstai ttR NvMaaR isi RaPoRT OAT: m ovuaR r Acittfits INVoLVio (St MoNT w Day vsAR vaaR $*g ;*' Of,3 MowTu oav vaAR *aciutv aMes pocasT hvMetR:si 11/A oisioiogo, , i 0l9 l0l6 89 8l 9 -l0l @ 1
- i Q1 1l2 2l1 8l9 N/A oisioio,o, i ,
,,,,,,,,, THi4 REPORT 68 SUDMITTEo PURSUANT To TM4 REoulREMENTS of 10 CFR i IC.s.r. o=. or #ao'. of **. foMpwas, (1 H "oo'
n .i y .on an i m ai g n ei.imm no mi.im uni.imn., n.,u.i noi 0 i Oi 0 ,
n .==im m so mi.im un.immi
_ gag;s7g,; gg,e,, ,
n .a.i.imiMi son.imm uni.iun..nAi mA, 20.oSt.il1Ht.i 734.H3Hul St. fan.lGH Hsi N , m.., .m...., ,
m,,,.i.s.,
tlCENSEE CONT ACT FoR TMit LeR 113!
NWE YtttPMoNE NvM5tm Gordon Nader, Licensing Engineer * * " ' '
_ 3 l 113 5i8l6i-l 4 2:113 1 4
cowLeTe oN tm som aAcu cowoNaNT e AituR onchiese in T.us R PORT mi o
cAvis svin M cowoNa NT ** g ^ c- 'yo"l,"!!' [ cAun ev T M coM,oi,eNT w ^ ag* *c- gogagge i I I I I I I I I i i i I i i i I I I I I I I I I I I I I !
$UPPLEMENTA6 REPORT (iKPECTED (14i MONTH DAY vtAR s'de'MMiom
~] vis m ... .oy. surerro surwssioN oAre, ^"""
tu T R A c T u ,-, ,= i . .,,,s.,~
"T] No i i ;
, ,. . . .<. ,,, . . ., n . ,
Periodic leakage rate testing of Containment-Isolation valves and penetrations in accordance with the requirements contained in Technical Specification 3.6.1.2 and 10 CPR 50 Appendix J. has'been completed. During the performance of this testing, several valves have exceeded their administrative allowable leakage ratec and their combined leakage exceeded the limits as defined in the i
subject Technical Specification Limiting Ccadition for Operation.
Thirty-five out of the 237 containment isolation valves l exceeded their administrative individual allowable leakage rate. l-They were disassembled. cleaned. repaired or reworked, and l ,
retested as appropriate. An Integrated Leakage Rate Tect was l !
successfully completed on November 21, 1989. l l
Nu,Ce... u.~
NRC term seu
- U.S. l'UCLEAR 5.tEULATORY COMh408 0N
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION - exovf o oMe wo. 3ino-oioi EXPtRES: 8/31/W '
9 ACMf y knut til DOCKET NUMBER (2)
LtR WUMBER lel PA06 (3)
"aa "WWP Mr*J o
Fermi 2 TEXT f# mere apose 4 015101010 l 3 l 411 819 -
01211 -
01 1 01 2 0F 015
_;, ess .dpooner Nag Asse asAw (th Initial Conditions:
t operational Condition: 5 (Ref ueling)
Reactor Power 0%
reactor Pressure O psig Reactor Temperature: 97 degrees Fahrenheit Description of Event:
On November 21, 1989, the Integrated Leak. Rate-Test (ILRT) was l
-completed following earlier performance of'the Local Leak Rate l Testing (LLRT) of Primary Containment Isolation Valves (ISV) l-and Penetrations'in accordance with Technical: Specifications l (TS) 3/4.6.1.2. " Primary Containment Leakage" and 10CFR50 l Appendix J. " Primary Reactor Containment Leakage Testing for -
l Water Cooled Power Reactors". Of the 237 valves tested. 35 .l. .
contributed significantly to the total combined leakage of the -l primary containment boundary. Included in thi's total are the- l Main Steam Isolation Valves (MSIVs). l TS 3.6.1.2.a requires that the allowed primary containment l 1eakage-rate (La) be limited to 0.5 percent by weight of the l-containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> (wt%/ day) at 36.5 psig. After l rework of the 35 valves the measured Type A test result was l 0.318 wt%/ day which is within the acceptance criteria-of 0.375 l wt%/ day (0.75 La). l' Surveillance Requirement 4.6.1.2.a.2 requires that if Type B.& l C tests are conducted prior to the Type A test. then the Type. l' A test result shall have added to'it the difference between the l "as_found" vs. "as lefr" leakages for all penetrations. The _l "as found" vs. "as left" difference, including the MSIV's and l MSIV Leakage Control System, was 0.640 wt%/ day. Adding the' l-difference to'the measured Type A test results of 0.318 wt%/ day 1 results in an "as found" conteinment leakage rate of 0.958 I wt%/ day. l TS 3.6.1.2.b requires that the-combined leakage rate of Type B l and Type C tests, except f or leakage . tests on the MSIVs and l
-vcives which are hydrostatically tested, shall-be less than or l-equal to 0.60 La. Exclusion of MSIV leakage in the combined l
. total (0.60 La) is an approved exemption from 10 CFR 50 l Appendix J. Based on initici testing..two~ Type B tests andr35 l.
Type C.. tested valves exceeded their individual' administrative l limits. . Administrative limits are established for Type B and C l Jageoau mea .u.s. cro, a...- m e m. m a
. l ofRC Feem aSaa' U S. NUCLE A3 3 47ULATORv COMMitalON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION snRoveo ous Nown-cio4 I EXPIRES: $!91/N F ACILITV $ FAME (1) 00CKLT NUMatR (36 Lin NUMBER 16) PA05 (3)
Nm ItYnN e ' Fermi 2 tw a mm ee s om< n, newac re mennm o is lo lo lo l3 l 4l1 49 -
0l 2 l1 -l0l1 Q3 OF 0l .5 l
l
}
tests in accordance with the Inservice Test. Program to provide 'l~
' individual valve and penetration acceptance criteria. The l combined leakage from Type B and~C Tests exceeded-0.60 La after 1 initial testing. l TS 3.6.1.2.c requires that the leakage rates for all four main i steam lines..when tested at 25.0 psig, be less than or equal to l .
100 Standard Cubic Feet per Hour (SCFH). LLRTs of the HSIVs l resulted in these valves exceeding their TS limit of 100 SCFH. l- ;
TS 3.6.1.2.d requires.that a combined leakage ~ rate.for all l' l containment isolation valves in hydrostatically tested lines be. l 1ess than or equal to 5 gallons per-minutes (gpm) when tested at 'l 1.10 Pa. The combined _ local leakage rates of-hydrostatically- l tested valves exceeded the 5 gpm TSLlimit.. l Additionally. TS 3. 6.1. 2. e requi'res that the water leakage.be l-
- less than or equal to lgpm times the number of valves per l penetration not to' exceed 3 gallons per minute (gpm) per: l penetration for any line penetrating containment when l hydrostatically tested at 1.10 Pa. One valve in a' penetration l l
leaked in excess of the 3 gpm TS limit. l .
The post ILRT Report (required by 10CFR50, Appendix J) will l-specify the as found and as left individual-leakege rates for 1 all valves / penetrations. l Cause of the Events t The basis for the associated TS-survelliance requirement is to 1 detect valve leakage due to normal wear and-degradation during a l specified. time interval.- l The observed containment isolation valve leakage was generally .l caused by normal degradation of valve components and/or l l contaminants on the valve seating surfaces._ One exception was -l L identified where an MSIV Leekage Control Valve, B21-F434, I l
1eaked 155 SCFH (0.52 La). This valve failed to fully close l due to binding of the valves' internals. l Analysis of the Event:
I ' Type A test leakage.is to a large degree a measure of the 'l individual penetration leak tightness. The MSIVs and MSIV l Leakage-Control System valve leakage was a maj or contributor l to~ the "as-found" Type A test results. I i
,,,,, c,o, 3,,,,33,,,,,,,,,,,
, Q*ou asea
4 NaC tem aneA' UL NUCLEAR LETULATORY COMMtIDION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION' =>Psovto oMe No 3ino-om -
, fxPtRES: 8/31/0B -
F ACILtTY Naut til DOCRE1 NVMSER G) PAOS (3l
, LER NUMBER (6)
V$AM -
"Na[nN '
nan TExi w ow. e a o. eau, m. .m.w mc em ammm o is 1o lo lo l3 l 4[1 8!9 -
0l2l 1 - 0l 1, 44 OF 0l 5 The Fermi MSIV Leakage Control System (MSIVLC) eliminates l~
leakage through the MSIVs by pressurizing the space between 'l the inboard-and outboard MSIVs and the outboard and third MSIV l to slightly above containment post-LOCA accident pressure. The l Design Basis LOCA is_ the most limiting accident with respect to l containment pressurization and off-site dose consequences. l This system meets the guidelines of Regulatory Guide l'.96 and l therefore, meets the requirement of General Design Criterion 54 l as it relates to leak detection, isolation, containment' I capabilities and suitable redundancy. l Since operations personnel are directed.to initiate the MSIV l Leakage control System shortly after a LOCA. leakage from l
- ontainment out through the MSIVS and MSIVLC valve'would have l been zero. The "as-found" containment leakage ~ rate with the- l HSIVLC system operating would be 0.405 wt%/ day which is below l the TS 3.6.1.2.a limit of 0.5 wt%/ day. Following an accident. 1 Standby Gas Treatment System (SGTS) would filter the gaseous 1 effluent from the Reactor Building' prior to its release, which I would significantly reduce the potential off-site doses- l attributable to leakage from primary containment. l l
Type B and C LLRT is performed to detect degradation of l penetration and valve sealing characteristics which would l L adversely affect primary containment: integrity. Any degrada- l tion discovered through testing is corrected so that1 potential- l degradation of conteinment or containment penetrations does not l occur between the Type A. B and C testin8 Periods. While the' I combined B and C leakage exceeded.the 0.60 La maximum allowed. I by T.S., the net containment leakage with the-MSIVLC system in- .I operation was less_than the maximum allowable containment leak- l age rate of 0.5 wt%/ day. l-Two valves were primarily responsible for exceeding both T.S. .I requirements (TS 3.6.1.2.d and 3.6.1.2.9) for water leakage. 'l One valve was the Residual Heat Removal (RHR) "A" minimum flow l' :!'
isolation valve and the other was the: Torus Water Management l' System (TWMS)-inboard isolation. valve. RHR is considered a l~
l closed system outside of containment and is also running l f~ post-LOCA. Any water leakage through the isolation valve would l l be contained-in the RHR process piping. I i
The TWMS isolation valve had a second isolation valve down-- l stream of it that was leaktight. This second isolation valve l
' would have contained any Torus water from leaking out of l-containment. Therefore, substantive barriers existed to prevent l 1eakage from both Primary Containment-water leakage paths. l ;
l .
~l
~ "'aY * * "** '
L eenC f ere 34A U.S. NUCLEI 2 Et1ULATORY COMMrBS60N '
' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION A*enovto ove No aiso-oio.
Excints: mm FActLatyesaast m . DoceLET NUMetR m Lth NUMeth (81 Pact (3
'8"" v -
EvaN Fermi 2 TEXT & more asses de segurog use ^ J 44C Form tads /(1h o is lo lo lo l31411 49 -
~ 0l2l1 -
0l1 0l5 OF 0l5
.3 Corrective Actions: ,
All 35 containment isolation valves that exceeded their I administrative individual allowable leakage rate, including l B21-F434 were cleaned, reworked and/or refurbished. The valves l were then retested and leakage verified to be in compliance- l with Technical Specification Surveillance Requirement 4.6.1.2. l The f our outboard MSIVS were- disassembled. refurbished. _ l reassembled. and successfully retested. The four inboard MSIVs l ,
were modified during the current refueling outage using the -l manufacturer's latest design modification kit. This MSIV l modification has been endorsed by the BWR Owner's Group and the !
NRC. and consists of-:hanges that include an elongated poppet l- .
and pilot poppet assembly (" nose cone"). addition of an l anti-rotation device and a2 inch diameter stem with associated' I machining of the valve cover / bonnet. These modifications-are l' intended to improve LLRT performance and' valve reliability. l The MSIVLC is designed to eliminate leakage from_ containment l 1 '
through the MSIVS. The MSIV leakage was within'the capacity of l the MSIVLC system, therefore, even though the valves-exceeded I their T.S. leakage limit, potential off-site doses dueEto this _l 1eak path were eliminated. l The following table summarizes the present condition and test I results of the primary containment isolation valves and I penetrations. l Technical l Type of_ Test As-Left Condition Specification Limit l l
Type B and C
- 86.09 SCFH 178 SCFH (0.3 wt%/ day) l (0.145 wt%/ day) l l
MSIVs 24.98 SCFH 100 SCFH l l
Hydrostatic 1.22 GPM 5 GPM l 0 For all containment isolation valves exclusive of the MSIVs and l Hydrostatically tested valves. l 1
Provious_Similar Occurrences:
Licensee Event Report 86-011-01 " Excessive Leakage from MSIV" and Licensee Event Report 88-008-01 " Leakage In Excess of the Allowable Found-During LLRT".
gl * *^ .u.s. croi m..no-m, coo ro