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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20153A9941998-09-16016 September 1998 Safety Evaluation Denying Request to Remove Missile Shields from Plant Design ML20151U8821998-09-0808 September 1998 SER on Revised Emergency Action Levels for Gpu Nuclear,Inc, Three Mile Island Nuclear Plant Units 1 & 2 ML20237A8331998-08-12012 August 1998 Safety Evaluation Accepting USI A-46 Program Implementation at Plant,Unit 1 ML20217K4851998-04-24024 April 1998 Safety Evaluation Supporting Amend 207 to License DPR-50 ML20199G8371998-01-22022 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Three Mile Island Nuclear Station,Unit 1 ML20198K2281997-10-16016 October 1997 Safety Evaluation Supporting Amend 206 to License DPR-50 ML20211G8561997-10-0202 October 1997 Safety Evaluation Supporting Amend 204 to License DPR-50 ML20210Q9991997-08-28028 August 1997 Safety Evaluation Concluding That Since 25th Tendon Surveillance on Few Yrs Away,Adequacy of Remaining Prestressing Force Will Be Critical to Verify ML20217Q7341997-08-27027 August 1997 Safety Evaluation Supporting Amend 203 to License DPR-50 ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20149D2671997-07-11011 July 1997 SER Concluding That Exemption from Listed Fire Areas Should Be Granted & Exemption from Fire Area FH-FZ-5 Should Be Denied ML20138H6671996-12-19019 December 1996 Safety Evaluation Accepting Util IPE Submittal in Response to GL 88-20 ML20134D7811996-10-24024 October 1996 Safety Evaluation Supporting Amend 51 to License DPR-73 ML20128L6741996-10-11011 October 1996 Safety Evaluation Accepting Third ten-year Interval for Pump & Valve Inservice Testing Program for Facility ML20128K1981996-10-0808 October 1996 Safety Evaluation Supporting Amend 50 to License DPR-73 ML20094Q0301995-11-24024 November 1995 Safety Evaluation Supporting Amend 199 to License DPR-50 ML20092N2551995-10-0202 October 1995 Safety Evaluation Supporting Amend 197 to License DPR-50 ML20087G5771995-08-14014 August 1995 Safety Evaluation Supporting Amend 195 to License DPR-50 ML20086R7421995-07-24024 July 1995 Safety Evaluation Supporting Amend 194 to License DPR-50 ML20077C2901994-11-28028 November 1994 Safety Evaluation Supporting Amend 192 to License DPR-50 ML20071N3991994-08-0101 August 1994 Safety Evaluation Supporting Amend 191 to License DPR-50 ML20071K8921994-07-25025 July 1994 Safety Evaluation Supporting Amend 188 to License DPR-50 ML20071L2381994-07-25025 July 1994 Safety Evaluation Supporting Amend 189 to License DPR-50 ML20071K8741994-07-25025 July 1994 Safety Evaluation Supporting Amend 190 to License DPR-50 ML20070H2851994-07-14014 July 1994 Safety Evaluation Supporting Amend 187 to License DPR-50 ML20073S3941994-05-23023 May 1994 Safety Evaluation Supporting Amend 184 to License DPR-50 ML20059D1771993-12-28028 December 1993 Safety Evaluation Supporting Amend 48 to License DPR-73 ML20062M2481993-12-21021 December 1993 Safety Evaluation Supporting Amend 180 to License DPR-50 ML20062K1041993-12-0606 December 1993 Safety Evaluation Supporting Amend 47 to License DPR-73 ML20058F0311993-11-16016 November 1993 SE Informing That Changes to Pdms Requirements & Commitments List of 930115,does Not Constitute Unreviewed Safety Question,Nor Do They Involve Significant Hazard or an Environmental Impact ML20059K3001993-11-0808 November 1993 Safety Evaluation Supporting Amend 46 to License DPR-73 ML20057A8321993-09-10010 September 1993 Safety Evaluation Supporting Amend 178 to License DPR-50 ML20057A3641993-09-0101 September 1993 SER Denying Licensee 930216 & 0416 Requests for Relief from Certain Requirements of ISI Program ML20056F0171993-08-0505 August 1993 Safety Evaluation Accepting Proposed Changes to Pdms Requirements & Commitments List of 930115 ML20128P7321993-02-19019 February 1993 Safety Evaluation Supporting Amend 171 to License DPR-50 ML20128K0771993-02-11011 February 1993 Safety Evaluation Supporting Amend 169 to License DPR-50 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
05000289/LER-1998-009-01, :on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised1998-09-18018 September 1998
- on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised
1999-09-30
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION 4j WASHINGTON, D. C. 20555
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NO.11o TO FACILITY OPERATING LICENSE N0. DPR-50 METROPOLITAN EDISON COMPANY JERSEY CENTRAL POWER AND LIGHT COMPANY PENNSYLVANIA ELECTRIC COMPANY GPU NUCLEAR CORPORATION THREE MILE ISLAND NUCLEAR STATION, UNIT N0. 1 DOCKET NO. 50-289 INTRODUCTION A number of events have occurred at operating Pressurized Water Reac+.or (PWR) facilities where decay heat removal capability has been seriously degraded due to inadequate administrative controls during shutdown modes of operation. One of these events, described in IE Information Notice 80-20 dated May 8, 1980, occurred at the Davis-Besse Station, Unit No. 1, on April 19, 1980.
In IE Bulletin 80-22 issued May 9, 1980, licensees were requested to imediately implement administrative controls which would ensure that proper means are available to provide redundant methods of decay heat removal. While the function of the bulletin was to effect immediate action with regard to this problem, the NRC considered it necessary that an amendment be made to each PWR license to provide for permanent long-term assurance that redundancy in decay heat removal capability will be maintained. By generic letter dated June 11, 1980, all PWR licensees were requested to propose Technical Specification (TS) changes that provide for redundancy in decay heat removal capability in all modes of operation.
NRC model TSs were provided as guidance.
GPU Nuclear Corporation (the licensee) responded.to the NRC generic letter by letters dated January 26, 1982, and October 10, 1984, in which the generic issue was discussed but no actual changes to the TSs were requested.
By letter dated March 8,1985, as supplemented by letter dated May 14, 1985, GPU Nuclear Corporation applied for TS changes designed to assure redundant decay heat removal capability for all modes of reactor operation for TMI-1.
In an April 24, 1986 letter, the licensee provided additional information concerning the amendment request.
DISCUSSION AND EVALUATION The proposed TSs provide for redundant means of decay heat removal in all modes of operatioa except during refueling when a large mass of water is above the core. These redundant means are outlined as follows:
Power Operation and Hot Standby (reactor critical)
These modes for TMI-1 are comparable to Standard Technical Specification (STS)
Modes 1 and 2, Power Operation and Startup.
For TM1-1, both reactor coolant (RC) 8608280194 860814 PDR ADOCK 05000289 P
.PDR
1
. loops with one reactor coolant pump (RCP) in each loop must be in operation when the reactor is critical. With less than four RCPs in operation, the TSs require a reduction in power.
Hot Shutdown (reactor sub-critical)
This mode for TM1-1 (RC temperature above 525 F) is comparable to STS Mode 3 Hot Standby (RC temperature above 305'F).
For TMI-1 in Hot Shutdown, both RC loops are required to be operable. The STS requirements for Mode 4, Hot Shutdown (RC temperature below 305 F) are essentially covered by the proposed TMI-1 TSs that require two decay heat removal means to be available with one loop in operation when the RC temperature is below 250 F, i.e., either two decay heat removal loops, two RC loops, or one of each.
The proposed TSs would allow the plant to operate in the equivalent of STS Mode 3 with one RCP operating and STS Mode 4 with no RCP operating. By letter dated January 9,1986, the NRC staff requested the licensee to verify that operation in such modes will be bounded by the conditions in the TMI-1 FSAR analysis of accidents.
By letter dated April 24, 1986, the licensee provided information by which they concluded that the proposed amendment would allow operation in a manner bounded by their FSAR analysis. This letter provided confirmatory information to the NRC staff but did not change the application for amendment as it existed in their May 14, 1985 submittal. This letter provides sufficient justification for the staff to conclude that the proposed TS changes place additional rertrictions on the licensee by designating systems which must be operational when RC temperature is between 200 F and 250 F.
Furthermore, the proposed TS changes do not allow TMI-1 to operate in any condition less restrictive than current TSs and cre therefore acceptable.
Cold Shutdown and Refueling with the Water Level Above the Core Less Than 23 Feet Two decay heat removal loops are required to be operable with at least one loop in operation.
Refueling with the Water Level Above the Core Greater Than 23 Feet At least one decay heat removal loop is required to be in operation. The other loop need not be operable. Under such conditions, the mass of water above the core provides adequate heat removal capability and therefore a redundant method is not necessary.
In addition to the above requirements for operability, the proposed TS revisions specify surveillance intervals for heat removal systems that are consistent with the STSs. The revised TSs provide an improvement over the existing ones since redundant decay heat removal will now be provided when 1
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. the plant is in the equivalent of STS Modes 3, 4 and 5.
Duringrefbelingwith a large mass of water above the core, only a single heat removal path is required. The surveillance requirements that would identify any inoperable equipment or degraded performance ~ are performed daily. The NRC staff, therefore, concludes that the proposed TSs meet the intent of the STSs with respect to redundant means of decay removal capability and are acceptable.
ENVIRONMENTAL CONSIDERATION This amendment involves a change in the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20.
We have determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public comment on such finding. Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of this amendment.
CONCLUSION We have concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will be conducted in compliance with the Commissinn's regulations and the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Dated: August 14, 1986 Principal Contributors:
G. Schwenk, J. Thoma s...
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