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Category:NRC TECHNICAL REPORT
MONTHYEARML20005E6741989-12-29029 December 1989 AEOD/T927, Followup on Steam Binding of Auxiliary Feedwater Pumps, Technical Review Rept ML20245F9401989-04-26026 April 1989 AEOD/T907 Component Degradation Due to Indiscriminate Painting, Technical Review Rept ML20148B3291988-03-14014 March 1988 Headquarters Daily Rept for 880314 ML20237F6221987-08-27027 August 1987 LER Quality Evaluation for Catawba Units 1 & 2 During Period from Oct 1986 - Jul 1987 ML20137N9071985-11-22022 November 1985 Significant Change Analysis ML20209G4011985-09-0404 September 1985 AEOD/T510, Xenon-Induced Power Oscillations at Catawba, Technical Review Rept.No Further Action by AEOD or Other NRC Ofcs Necessary ML20138Q0831984-06-0707 June 1984 Rept of 840523 Interview W/Jp Oreilly Re Allegations of NRC Mgt/Personnel Improprieties Concerning Facility ML20138Q0431984-02-16016 February 1984 Rept of 840202 Interview W/Lr Davison Re Qa/Qc Program at Plant & Oct 1980 Meeting W/Gf Maxwell Re NRC Insp ML20080D4321983-10-31031 October 1983 Handwritten Notes & Calculations Re Facility Const.Related Info Encl ML20138Q0761983-09-0101 September 1983 Rept of 830824 Interview W/Ge Ross Re Recrimination by Util for Employee Contacting NRC Concerning Qa/Qc Welding Program.Qa/Qc Problems of Secondary Importance to Mgt. Related Documentation Encl ML20138Q0721983-08-31031 August 1983 Rept of 820823 Interview W/R Irby Re Possible Falsification of Documents & Possible Harassment or Intimidation of Util Employees.Nrc Position on Nonconforming Items Should Be Stronger ML20138Q0691983-08-31031 August 1983 Rept of 830823 Interview W/He Eubanks Re Problems Concerning Util & NRC Handling of Employee/Employer Problems.Employees Never Threatened W/Transfers/Terminations as Potential Retaliatory Weapon by Util ML20080D3811983-08-0101 August 1983 Handwritten Notes & Graph Re Tests Concerning Const Activities & Fuel Load Dates ML20065K8461980-08-31031 August 1980 Systematic Assessment of Licensee Performance Notes Re Facility Evaluation for Sept 1979-Aug 1980 ML20080D3921980-04-23023 April 1980 Handwritten Notes & Calculations Re Const & Fuel Load Preparation 1989-04-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212A6271999-09-30030 September 1999 Rev 0 to WCAP-15243, Anaylsis of Capsule V & Capsule Y Dosimeters from Duke Energy Catawba Unit 2 Reactor Vessel Radiation Surveillance Program 05000414/LER-1999-004-01, :on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled1999-09-27027 September 1999
- on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled
05000413/LER-1999-015, :on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully1999-09-27027 September 1999
- on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully
ML20212G2511999-09-22022 September 1999 Safety Evaluation Supporting Amends 180 & 172 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-008, :on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With1999-09-21021 September 1999
- on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With
05000414/LER-1999-005-02, :on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure1999-09-20020 September 1999
- on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure
05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service1999-09-15015 September 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service
ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 05000414/LER-1999-004, :on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc1999-09-0101 September 1999
- on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc
05000413/LER-1999-014, :on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed1999-09-0101 September 1999
- on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed
ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate 05000414/LER-1999-003, :on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal1999-08-31031 August 1999
- on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal
05000413/LER-1999-012, :on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With1999-08-26026 August 1999
- on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With
ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210U8341999-08-13013 August 1999 Safety Evaluation Supporting Amends 179 & 171 to Licenses NPF-35 & NPF-52,respectively ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service1999-07-19019 July 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service
05000414/LER-1999-004-02, :on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status1999-07-15015 July 1999
- on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status
ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation 05000414/LER-1999-003-02, :on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed1999-07-0808 July 1999
- on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed
ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 05000414/LER-1999-002-03, :on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested1999-06-0303 June 1999
- on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested
ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected 05000413/LER-1999-004, :on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With1999-04-12012 April 1999
- on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With
ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML20205N2381999-04-0909 April 1999 Safety Evaluation Supporting Amends 178 & 170 to Licenses NPF-35 & NPF-52,respectively ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205B3101999-03-26026 March 1999 Safety Evaluation Supporting Amends 176 & 168 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-001-01, :on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups1999-03-17017 March 1999
- on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups
1999-09-07
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AE0D TECHNICAL REVIEW REPORT UNIT:
Catawba 1 TR REPORT NO.:
AE00/T510 DOCKET NO.: 50-413 DATE: September 4, 1985 LICENSEE:
Duke Power Company EVALUATOR / CONTACT:
R. Freeman NSSS/AE:
Westinghouse / Duke Power Company
SUBJECT:
XENON INDUCED POWER OSCILLATIONS AT CATAWBA EVENT DATE: March 18, 1985
REFERENCES:
(1)
U.S. Nuclear Regulatory Commission Inspection and Enforcement Inspection Report No. 50-413/85-12, Duke Power Company, Catawba Unit 1, Docket No. 50-413, dated April 26, 1985.
(2)
U.S. Nuclear Regulatory Commission, Regulatory Guide 1.68, Rev. 2, Initial Test Programs for Water-Cooled Nuclear Power Plants, dated August 1978.
SUMMARY
On March 18, 1985, with Catawba Unit 1 at approximately 50% power, during initial startup physics testing, severe core power tilts and oscillations occurred as a result of control rod insertion testing.
Because of unex-pected equipment problems and lack of procedural guidance, a control rod remained inserted in the core for an extended period of time. Upon withdrawal of the control rod to its fully withdrawn position, severe xenon induced power oscillations were experienced which resulted in a reduction in reactor power operation and the delay in the completion of startup physics testing. The corrective actions taken by the licensee were judged to be appropriate. Testing procedures which restrict the maximum allowable time of control rod misalignment could signicantly reduce the likelihood of inducing severe power tilts and oscillations. However, it may no longer be necessary for plants to perform some of the physics tests the licensee was conducting when the power oscillations occurred.
It may be appropriate to consider referencing the results of control rod insertion tests at plants with identical cores in place of the plant-specific tests.
Such referencing would reduce the potential for xenon induced power oscillations, which when combined with a power transient, could result in exceeding local departure from nucleate boiling (DNB) limits.
DISCUSSION Reference 1 describes the circumstances surrounding a xenon induced power oscillation event that occurred on March 18, 1985 at the Catawba Unit I nuclear facility. As part of Catawba's initial startup test program, control rod in-sertion testing was being performed from 50% reactor power in accordance with Regulatory Guide 1.68, Appendix A, Sections 5.F and 5.I (Ref. 2). This testing was designed to demonstrate:
(1) core thennal and nuclear parameters are in agreement with predictions with a single high worth control rod fully inserted during ano following return of the rod to its bank position and, (2) the 1/
This report supports ongoing AE00 and NRC activities and does not represent the nosition or recuirements of the responsible NRC program office.
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capability for the. facility design to detect a control rod misalignment equal to or less than the maximum allowed by plant technical specifications.
The particular testing conducted by the licensee on March 18, 1985 was to J
measure the maximum flux perturbation expected from a dropped control rod.
This test requires having the reactor at approximately 50% power. A core flux map is initially performed using the incore movable flux detectors.
A high worth peripheral control rod is then fully inserted into the core, and then another flux map is conducted.
During this phase of startup testing, the high flux reactor trip setpoints are reduced from the normal 109% value to 70%.
l During the performance of the test, unexpected equipment problems were encountered causing the second flux map to be delayed. After 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> had elapsed, the plant staff decided to abort the test and return the control rod to its fully withdrawn position. The total time the control rod was inserted into the core was approximately 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The long period of control rod insertion compared to the xenon half-life of 9.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, induced a severe power tilt and oscillation. When the licensee recognized that the core was undergoing xenon induced power oscillations, core power i
was reduced and the reactor vendor (Westinghouse) was consulted and the situation reviewed by the licensee manacement.
It was determined that no limits were in danger of being exceeded and power operation could continue while attempting to dampen the power oscillations. The worst observed power tilt occurred with a reactor thermal power of 48.5%. Power in core quadrants 1 and 3 was indicated to be 45.5% and 46.8%, respectively, while quadrants 2 and 4 were 73% and 30.5%, respectively. After 5 days, the xenon induced power oscillations dampened out such that physics testing could resume.
ANALYSIS l
Operation with core power tilts is an undesirable condition, but is allowed by plant technical specifications for reactor power levels below 50% because the quadrant power tilt limits are only applicable for reactor power levels i
above 50%. Even though the high flux trip setpoints are reduced during the control rod insertion testing phase of the startup test program, automatic core protection may not be sufficient to prevent localized DNB to occur in i
the unlikely event of a power transient occurring during a peak power tilt.
1 This is because it requires two out of four power range channels to activate t
l the reactor protective system high neutron flux power range trip. DNB could occur during severe power tilts because the power in the core quadrant near a second detector channel would not be expected.to reach the trip setpoint prior.
i i
to the power in the core quadrant near the first tripped detector being eisove
.the local power leve) analyzed for DNB.-
Because the amount of power tilting is dependent on the length of time a control rod is misaligned, limiting the duration of misalignment woulii minimize the amount of power tilting. Testing procedures which address the maximum allowable time of control rod misalignment could significantly
-reduce the likelihood of inducing severe power tilts.and oscillations'. Such i
guidance could help in the preparation for conducting such tests and allow for early determination in aborting the tests when unforeseen ~ problems develop.
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In view of the potential for producing severe power tilts, performance of some physics tests at power may no longer be necessary, particularly if previous tests at reactor facilities of similar design can provide sufficient data to verify the adequacy of the physics analysis. Discussion with members in the Core Performance Branch, Office of Nuclear Reactor Regulation (NRR) have confirmed that the information obtained from the particular testing Catawba was performing on March 18, 1985 yielded little new information on the reactor nuclear physics analysis compared to existing information avail-able at similar reactor facilities. Since existing information available at other reactor facilities with identical cores may be applicable, the testing i
outlined in Regulatory Guide 1.68, Appendix A, Sections 5.F and 5.I may not have had to be performed.
Thus, allowing licensees to reference the results of tests conducted at plants with identical cores could be a viable option in lieu of performing the plant-specific tests. Such an option would reduce the potential for xenon induced power oscillations which would enhance reactor
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safety as well as shorten the duration of low power physics testing.
CONCLUSION Because of unexpected equipment problems and lack of procedural guidance,.
a control rod was left inserted in the core for an extended period of time. The extended period of the control rod insertion induced a severe l
power tilt and power oscillations. The corrective actions taken by the licensee were judged to be appropriate. However, the need to perform some of the physics tests outlined in Regulatory Guide 1.68, Rev. 2, Appendix A, Sections 5.F and 5.I appear to be no longer necessary because the results of tests conducted at plants with identical cores could be referenced in place of performing the actual testing. Minimizing the testing would reduce the potential for xenon induced power oscillations and, thereby, l
minimize the likelihood of exceeding DNB limits.
l Discussions held with NRR representatives (Core Performance Branch) indicate that NRR would be willing to consider including in the next revision of Regulatory Guide 1.68 the option to allow referencing of test results conducted at plants with identical cores in lieu of performing the plant-specific tests. Allowing licensees this option should reduce the amount of testing, and, thereby, reduce the potential for xenon induced power oscilla-tions to occur.
No further action is deemed necessary by AE00 or any other NRC office.
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