ML20199H024

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Insp Repts 50-445/97-18 & 50-446/97-18 on 970831-1011. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering
ML20199H024
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 11/21/1997
From: Tapia J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20199H018 List:
References
50-445-97-18, 50-446-97-18, NUDOCS 9711250361
Download: ML20199H024 (22)


See also: IR 05000445/1997018

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ENCLOSURL2

U.S. NUCLEAR REGULATORY COMMISSION l

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REGION IV i

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Docket Nos.: 50 440 i

50 446  !

License Nos.: NPF 87

NPF 89 ,

Report No.: 50-445/97 18 .

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50-446/97 18

Licensee: TU Electric I

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Facility: Comanche Peak Steam Electric Station, Units 1 and 2

Location: Fti 56  ;

Glen Rose, Texas

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Dates: August 31 through October 11,1997

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Inspector: H. A. Freeman, Acting Senior Resident inspector

Approved By: J. l. Tapia, Chief, Projects 8 ranch A

Division of Reactor Projects

Attachment: Supplemental Information

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EXECUTIVE SUMMARY l

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Comanche Peak Steam Electric Station, Units 1 and 2  :

NRC Inspection Report 50 445/97 18;50-446/97 18

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Operations

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  • The licensee con:inued to pay close attention to the material condition of the plant.  ;

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This was especially significant consideririg the increasing level of activity in

preparation for the Unit 2 refueling outage. The licensee took prompt corrective. i

actions on two issues outside the control room, which could have led to a reactor  ;

trip had the condition been left uncorrected (Section 01.2). l

  • Overall, conduct of operations continued to be very good. The plant operated in a }

safety conscious manner with appropriate supervisory and management oversight.

With the exception of the boron thermal reneration system leakage, good

performance by operators was noted for severalissues (Section 01.2). ,

  • A vague procedure, combined with an operating crew that did not fully review- "

. equipment status, lead to the contamination of several areas while flushing

the boron thermal reneration system. The event indicated a weakness in attention-

to detail and an overreliance on the procedure (Section 01.3).

  • - The licensee identified and took prompt, conservative actions on two issues where

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the design assumptions had not been fully implemented. These issues indicated

that the licensee continued to perform thorough reviews of plant systems and

procedures as expected by their response to 10 CFR 50.54(f) (Sections 03.1

and M1.2).

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Maintenance

  • While the standardization of sensors conducted prior to the surveillance testing of

the hydrogen recombiner did not constitute preconditioning, the activity was not

included in the procedures and was a violation of 10 CFR Part 50, Appendix B,

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Criterion V, for procedure adequacy. This lack of procedural direction lead to  ;

inconsistent performance (Section M3.1).

Enaineerina -

  • The licensee identified that two throttle valves in each unit may have minimum gap

openings which are smaller than the mesh on the emergency core cooling

system (ECCS) sumps. The licensee had previously evaluated the industry

information 'concerning the throttle valves, but the original evaluation did not

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consider the disk guide rings and f ailed to recognize that the minimum gap between

the guide rings and the valve body could be smaller than the disk to seat gap r

(Section E1.1).

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  • Surveillance procedures for the control room filtration / pressurization system failed to

implement adequate acceptance limits; and as a consequence, the as left value for

pressurization unit flow exceeded design basis limits on two occasions. This was a

violation of 10 CFR Part 50, Appendix 0, Criterion V, in th6t the licensee did not

appropriately implement design limits into the survealance tests (Section E3.1).

  • During a surveillance test of the control ro,m pressurization unit, engineers

performing the test failed to use a temperature measuring instrument which met

procedural accuracy requirements. This was a violation of Technical

Specification 6.8.1 and was caused by a lack of attention to-detail (Section E4.1).

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Report Details

Sumtriarv of Plant Statug

Units 1 and 2 operated at essentially 100 percent power throughout the inspection period.-

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1. Operations

01 Conduct of Operations

01.1 Plant Tours

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a.- Inspection Scooe (71707)  ;

The inspectors conducted frequent plant tours to verify safe operation of plant

equipment and to inspect general plant material and housekeeping conditions. As

part of the tours, the inspectors performed routine control room observations and '

walkdowns of safety related flow paths and locked component lists.

b. Observations and Findinos

Overall, the inspectors determined that operations personnel operated the plant in a

safety conscious manner with appropriate management oversight. Safety systems

were properly aligned. Plant housekeeping and material condition of plant

equipment were excellent. The inspectors identified several minor housekeeping

and equipment material deficiencies. These deficiencies were appropriately

dispositioned by the licensee.

01.2 Plant Material Condition

a. laspection Scope (71707)

The inspector reviewed control room logs, problem identification forms, toured the

plant, and attended daily planning meetings to evaluate the licensee's ability to

identify and correct material condition problems.

b. Observations and Findinas

The inspector found that the licensee was doing a very good job of identifying and '

correcting plant material condition problems. This was evident even with the

increased level of activity due to outage preparations. Two items warranted special

recognition because either item could have led to a reactor trip if left uncorrected.

- The first example involved the identification by a plant equipment operator that a

scaffold platform erected around a Unit 2 feedwater flow control valve would have

impeded the valve movement during a downpower. The operator recognized that,

due to the unusual nature of the valve, the valve body moves outward during

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closing. This identification was timely because a downpower was scheduled for the i

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following evening. The scaffold was immediately removed.

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The second example involved the identification and reporting by an individual

responsible for the cleanliness in an area in the Unit 1 turbine building that a sink ,

drain was clogged and overflowing. The prompt team investigated and found that a  !

sampling line from primary head tank was not fully closed. The sample line was

closed and the tank refilled. Had the tank continued to drain, a generator

trip / reactor trip could have occurred due to low level.

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c. Conclusions

The licensee continued to pay close attention to the material condition of the plant.

- This was especially significant considering the increasing level of activity in

preparations for the Unit 2 refueling outage. The licensee identified two issues

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-which could have led to reactor trips had the conditions been left uncorrected. The

licensee took prompt corrective actions.

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01.3 Boron Thermal Reaeneration System Lenkaoe

a. Inspection Scope (71707)

The inspector reviewed the cause and circumstances surrounding the contamination 1

of several areas in the auxiliary building, ,

b. Observations and Findinas

On October 2, while performing a flush of the boron thermal regeneration system in

preparation for the upcoming Unit 2 refueling outage, the licensee failed to open a

discharge valve and ended up pressurizing several diaphram operated valves and

contaminating several areas. The inspector reviewed Standard Operating

Procedure SOP 106B, " Boron Thermal Regeneration System," and found the

procedure vague in that it led operators to believe that they did not have to conduct

Section 5.1 prior to conducting a flush if the system was isolated for less than 14 '

days. The inspector found that the operating crew did not meet management's

expectation in regards to verifying proper initial conditions prior to performing the

activity,

c. Conclusions

This event is an isolated example of a knowledge deficiency of system operation by [

operators.

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03 Operations Procedures and Documentation

03.1 Catalvtic Hydroaen Recombiner Procedure Chanae

a. Insucction Scope (627071

The inspector reviewed the identification and significance of operating the waste

gas processing system catalytic hydrogen recombiner with the product hydrogen

above the alarm setpoint.

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b. Observations and Findinas

On October 10,1997, the licensee informed the inspector that, during the review of

a question concerning potential preconditioning of the catalytic hydrogen '

recombiner, the system engineer had identified that the recombiner was routinely

operated above the product hydrogen high alarm setpoint and that the operating

procedure had recently been modified to allow operation with up to 2 percent

product hydrogen concentration. The alarm setpoint was set at 0.25 percent. The

licenseo initiated a operations notification evaluation (ONE) form documenting the

fact that the procedure had been changed without performing a safety evaluation

and danger-tagged the system until the issues could be resolved. The licensee had

originally performed a 10 CFR 50.59 screening and had erroneously determined that

the procedure change did not cortatitute a change to the facility description.

The Final Safety Analysis Report, Section 11.3.2.1.2, states, "if hydrogen in the

recombiner discharge exceeds 0.25 percent by volume, an alarm sounds. This

alarm warns of high hydrogen feed, possible reactor malfunction, or loss of oxygen

feed." Design Basis Document ME 269, " Gaseous Waste Processing System,"

stated that the hydrogen recombiner gas analyzer high process limit was

0.25 percent based on vendor manuals. Operating with the product hydrogen

above 0.25 percent had no safety significance. The operating limits.and alarm

setpoint had originally been selected based on different detectors which could

differentiate between hydrogen and helium. Operating the catalytic recombiner with

product hydrogen above 0.25 percent ensures that the system is operating in an

oxygen deficient mode. This also ensures that a dangerous buildup of oxygen and

hydrogen cannot occur in the hold up tanks. At the end of the inspection period,

the licensee was completing a safety evaluation to change the operating procedure

and raise the setpoint.

The inspector determined that the changes to the catalytic hydrogen recombiner

operating procedure constituted a change to the facility, as described in the Final

Safety Analysis Report, and that a written safety evaluation documenting that the

change did not constitute an unreviewed safety question was not performed,

contrary to 10 CFR 50.59. This nonrepetitive, licensee-identified violation is being

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treated as a noncited violation (NCV), consistent with Section Vll.B.1 of the "NRC

Enforcement Policy" (50-445/9718-01; 50-446/9718-01) (EA 97 550).

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The it.spector concluded that the violation occurred as a result of poor

communications between radwaste operations and system engineering. The

inspector found the licensee's actions to resolve the issue were appropriate.

05 Operator Training and Qualification

a. Insr,ection Scone (71707)

The inspector attended the classroom portion of licensed operator training on

reduced inventory. The licensee was conducting the training in preparation for the

Unit 2 refueling outage,

b. Observations and Findinas

Training on midloop operations was thorough, well presented, and actively involved

the etitire crew. Topics included recent industry events and discussions on how to

avoid similar problems. The inspector concluded that the training was effective in

refreshing the operators's understanding of procedures and potential problems

involved in reduced inventory operations. The timing of *he training was

appropriate.

08 Miscellaneous Operations lasues

08.1 (Closed) Licensee Event Report (LER) 50-445/95007: Engineered safety

feature actuation caused by feedwater recirculatiori valve failing open due to a

failure in the power supply card. This event was discussed in NRC Inspection

Report 50-445/95 28;50 446/95 28. No new issues were revealed by the LER

08.2 (Closed) Violation 50-446/9715-01: Operation in excess of 102 percent thermal

power. In the enclosed Notice to NRC Inspection Report 50 445/97-15;

50-446/97 15, the NRC concluded that the information regarding the reason for the

violation and the corrective actions taken and planned were already adequately

addressed on the docket and that a response was not necessary unless the licensee

concluded that the descriptions or corrective actions did not accurately reflect their

position. The licensee did not respond and this item is closed.

II. Maintenance

M1 Conduct of Maintenance

M 1.1 Control Rqom Emeroenc. Pressurization Unit Carbon Sampie Surveillance Failure

a. insmection Scone (62707)

On September 16,1997, the licensee identified that recently drawn carbon samples

from both trains of the cont.. I toom emergency pressurization system failed a

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surveillance test for methyliodide penetration. The inspector reviewed the

Technical Specification and basis for the surveillance test, the design basis

document fc the control room emergency filtration / pressurization system, operating

procedures, and design drawings. The inspecor also consulted with NRC personnel

concerning the licensee's interpretation of the surveillance requirements.

b. Observations and Findinos

On September 16, a contractor laboratory informed the licensee that the samples

from the pressurization units drawn on August 22 and 25 had failed the methyl

iodide test with penetration results of 0.769 and 0.875 percent. The samples from

the filtration units had passed with penetration results of 0.011 and 0.023 percent.

Technical Specification Surveillance Requirement 4.7.7.1b(2) requires that each

control room emergency filtration / pressurization system train be demonstrated

oposable at least once per 18 months, by testing a representative carbon sample to

ensure that the methyl iodide penetration was less than 0.2 percent. The limiting

condition for operation allows one train to be inoperable for up to 7 days and has no

provision for having both trains inoperable. By design, each pressurization unit

operates in conjunction with its respective filtration unit. The licensee concluded

that, while the pressurization units were inoperable for methyl iodide penetration,

thq filtration / pressurization system train was operable; and, thereforc, entry into

Technical Specific 3 tion 3.0.3 was not requireo.

Each emergency pressurization unit draws a maximum of 800 cfm of outside air

through a carbon filter bed and ditcharges into the intake of its respective filtration

unit, in the filtration unit, the air is mixed with approximately 7200 cfm of air being

recirculated from the control room environment and passed through a second

carbon filter bed. The inspector reviewed the design basis and found that the

calculation did not account for the removal efficiency of the pressurization unit filter

(99 percent) in estimating the dose to control room operators during design basis

accidents. Therefore, from a design basis standpoint, the reduced efficiency of the

pressurization units had no effect on system operation.

Through a review of the Technical Specifications and bases, tha Ni;C staff agreed

with the licensee's conclusion that the Technical Specifications did not requi'e that

each pressurization unit meet the methyl iodido penetration surveillance requirement

separate from its respective filtration unit.

The licensee replaced and tested the carbon in one unit on September 17 and

replaced and tested the carbon in the other unit the following day. Licensee

engineers along with operations and maintenance personnel met to discuss

problems concerning the pressurization unit surveillance. The licensee identified

that performing the survei' lance on both trains during the same time frame reduces

the opportunities to identifying potential common failure mode problems. The

licensee intended to have the f ailed carbon analyzed to try to determine whether the

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problem was a common mode failure. Additionally, the licensee was reviewing

other surveillance procedures to identify similar implementation problems.

c. Conclusions

The licensee correctly implemented the surveillance requirement for the control

room emergency filtration / pressurization system.

M1.2 Dutaae Prenoration

a. Insocction Scope 162707)

During routine tours of the f acility, the inspector noted that the licensee had

connected an integrated leak rate test rig to the exterior of the Unit 2 safeguards

building. The inspector questioned the licensee regarding the seismic qualifications

of the test connection and test rig,

b. Observations and Findinas

The inspector questioned the licensee as to whether the connection between the

seismically qualified Unit 2 safeguards building and the temporary equipment for the

integrated leak rate test had been appropriately analyzed. The licensee could not

identify a seismic evaluation for the connection, therefore, a ONE form to

investigate the issue was written. The licensee also disconnected the skid from the

test connection. The licensee informed the inspector that they had never connected

the equipment to the test connection prior to shutting down the unit during past

outages. This item will remain open pending review of the licencee's determination

of the seismic qualifications of the connection (50-445/97184 : 50 446/9718-02).

M3 Maintenance Procedures and Documentation

M 3.1 E,xplosive Gas Monitorina Instrumentation

a. Inspection Scone (61726)

On September 30, the inspector witnessed a surveillance test performed on the feed

gas hydrogen and oxygen analyzers for Catalytic Recombiner X-01 of the waste gas

holdup system, The inspector reviewed the surveillance test and related tests for

conformance to Technical Specifierion surveillance requirements. The inspector

reviewed whether nonproceduralized actions performed by the technicians could

precondition the recombiner and cause the detectors to pass the surveillance test.

b. Observations and Findinns

The technicians performed the analog channel operational test (ACOT) in

accordance with Procedure INC-7841X, "ACOT/CHAN CAL Catalytic

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Recombiner X 01 Feed Gas Hydrogen and Oxygen Analyzer, CM ^ 127A,"

Revision 4. The purpose of the procedure was "to verify and, if required,

re establieh the accuracies and contro! functions of the channel sensors and

associated signal processing equipment . . . ."

During the surveillance test, an alarm at the waste gas panel could not be reset.

The technicians reperformed that section of the surveillance test and reset the

alarm. The technicians halted the test and informed the shif t manager and their

supervisor. The licensee concluded that the failure of the alarm to reset did not

affect the operability of the equipment and completed the test. The technicians

submitted a work request to troubleshoot the alarm reset function. The inspector

verified that reperforming portions of the procedurr was an accepted practice. The

inspector found that the licensee appropriately considered the impact of the alarm

reset f ailure on operability.

The inspector noted that, although the activity was not part of the procedure, the

technicians had standardized the detectors prior to the surveillance test. A

radwaste operator ir. formed the inspector that, prior to placing a recombiner in

service, the do! ,ctors usually required standardization. On October 8, the inspector

met with the licenseo to discuss potential preconditioning of the recombiners prior

to performing the surveillance tests. The licensee informed the inspector that they

were submitting a ONE form concerning potential preconditioning.

Standardization allows the detector to determine the permeability of the sensors.

The Technical Specifications define an ACOT to be, "the injection of a simulated

signal into the channel as close to the sensor as practicable to verify operability of

alarm, interlock an/or trip functions.1he ACOT shallinclude adjustments, as

necessary, of the alarm, interlock and/or trip setpoints such that the setpoints are

within the required range and accuracy." The inspector concluded that

standardizing the detectors did not affect any alarm, interlock or trip functions of

the detector and did not constitute preconditioning of the ACOT.

The licensee stated that standardization is usually performed after placing the unit in

service. While out of service, the recombiner is left with a dry purge gas flowing

through the sensors. The sensor membrane dries out by the purge which affects its

readings. When placed back in service, the sensors are in a high humidity

environment and the readings between the feed and product sensors may differ, if

the readings differ by more than 1 percent, the licensee performs a standardization.

This requirement was not proceduralized,

c. Conclusions

Since standardization prior to conducting Technical Specification surveillance tests

was not consistently performed, the ability to verify channel accuracy may have

t.een affected. The inspector concluded that Procedures INC-7841X and

INC-7845X f ailed to include instructions for performing standardization of the

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- detectors prior to performing the surveillance tests and that this represented a i

violation of 10 CFR Part 50, Appendix B, Criterion V, 150-445/9718 03; i

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50 446/9718 03h

M3.2- Containment Isolatlon Surveillance Test ,

a. Inspection Scope (617261 ,

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On October 9, the licensee conducted a slave relay actuation surveillance test using i

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Procedure OPT 484B, " Train B Safeguards Slave Relay K630 Actuation Test." The

- shift supervisor informed the inspector that this surveillance test would shut i

steam generator sample isolation valves and feedwater loop sample isolation valves, -

but that letdown containment isolation Valve 2 8152 would not shut because of 'i

a jumper installed as part of the procedure. The inspector reviewed

Procedure OPT 461B, " Train A Safeguards Slave Relay K630 Actuation Test," and

noted that it did not test letdown containment isolation Valve 2 8160.

The inspector reviewed other surveillance test procedures to verify that the letdown

containment isolation valves were, in fact, tested in accordance with Technical

Specification 4,6.3.

b. Observations and Findinas

Technical Specification Surveillance Requirement 4.6.3.2a, " Containment isolation

Valves," requires that each containment isolation valve shall be demonstrated

operable at least once per 18 months, by verifying that, on a Phase A isolation test

signal, each Phase A isolation valve actuates to its isolation position.

The inspector reviewed Test Procedures PPT S2 7414A and PPT S2 74158 and

verified that the procedures tested that the containment isolation valves would

actuate to their isolation positions on a Phase A isolation test signal. The inspector '

verified that the test procedures had been implemented, as required, by the

Technical Specification surveillance.  ;

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MS - Maintenance Staff Training and Qualification

MS.1 Breaker Refurbishment Trainina

a. Insoection Scope (62707)

The licensee established an objective of refurbishing all Breakers 480 V and 6.9 kV

on a 10 year cycle and had begun refurbishment of nonsafety relattd breakers, As

part of this initiative, the licensee had technical service representatives for both  ;

styles of breakers come to the site and provide hands on maintenance training for a .

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period of 2 weeks. The service representatives instructed plant personnel on how

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to overhaul and refurbish the breakers to factory specifications. The inspector

observed a portion of this training and talked with all responsible parties,

b. Observations and findinna

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Training, maintenance, quality control, and procedure development personnel

attended this training so that all groups could interact to develop a coordinated

maintenance effort. All groups were in the training workshop and were interacting

to ensure that maintenance procedures training guidelines, and maintenance

practices were correctly developed. A adeo camera was being used to capture

information for future training classes,

c. Conclusions

The inspector concluded that this coordinated activity was an outstanding tool since

it integrated the various groups responsible for development and implementation of

the breaker refurbishment task.

Ill. Ena!nniing

E1 Conduct of Engineering

E1.1 ECCS Throttle Valves

a. Inspection Scope (3751U

On October 2,1997, the licensee initiated a 1 hout report to the NRC under

10 CFR 50.72(b)(1)(ii)(B) for being outside the design basis. The licensee had

identified that two ECCS valves in each unit may have minimum openings less than

the fine mesh opening in the ECCS sump screens. The IWo.isco estimated that the

minimum gap in the cold leg injection valves associated with the centrifugal

charging pumps could be less than 0.0625 inches while the ECCS sump screens

have a fine mesh opening of 0.115 inches.

The inspector reviewed the licensee's operability determination and the

circumstances su< rounding the identification.

b. Observations and Findinns

The licensue br9 completed a detailed review of recent industry concerns involving

ECCS throttle valves on August 19,1996, included in the reviews were the

potential clogging of ECCS throttle valves at Diablo Canyon, the potential ECCS

pump runout due to throttle valve erosion caused by high pressure drop induced

cavitation at Sequoyah, and a Westinghouse Nuclear Safety Advisory Letter

concerning erosion of globe valves in ECCS throttling applications. Using estimated

valve positions derived from flow measurements and misleading information

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supp'ied by the vendor, the licensee had determined that the minimum seat to-disk

clearance for two of the centrifugal charging pump cold leg injection lines was

greater than 0.110 inches. The ECCS sump screens are constructed of both coarse

and fine mesh. Because the openings in the fine mesh are 0.115 inches, the

licensee concluded that operability of the injection lines was unaffected by potential

clogging concerns but continued to review the erosion issue.

During a meeting with the vendor in September 1997, the licensee recognized that

the minimum gap in the throttle valve rnay not occur between the seat and the disk.

Instead, the minimum gap could occur between the valve body and the disk

antithrust guide rings. The guide rings help to position the disk within the valve

and, thereby, reduce side thrust and disk wobble problems. The licensi e

re evaluated their earlier conclusion concerning minimum clearance usin1 graduated

ball bearings and a spare valve. The licensee determined that, while the minimum

seat to disk clearance may be greater than 0.115 inches, the guido rir.g to body

clearance may be as small as 0.0625 inches.

The inspector reviewed the licensee's technical evaluation of operability. Based on

the expected low velocity of the water entering the sump, the licensee concluded

that debris likely to pass through the emergency sump screen and, which could be

larger than the throttle valve openings, would likely be fragmented by the residual

heat removal pumps and the centrifugal charging pumps prior to reaching the

throttle valves. Any unfragmented pieces reaching the valves would likely be

fragmented by the high differential pressure across the valve. Heavier objects,

which were unlikely to be fragmented, were expected to settle out of the water and

not enter the sump. The inspector found the licensee's evalJation appropriate.

At the exit meeting, the licensee informed the inspector that they expected to be

able to implement a design change to resolve the problems of thro *tle valve erosion

and clogging during the next Unit 1 refueling octage which was scheduled to start

during March 1998,

c. Eqnclusions

The licensee identified that two valves in each unit may have minimum gap

openings which are smaller than the mesh on the ECCS sumps. The licensee had

previously evaluated the industry information cencerning the throttle valves but their

original evaluation did not consider the disk guido rings and f ailed to recognize that

the minimum gap between the guide rings and the valve body could be smaller than

the disk to seat opening.

The licensee was committed to resolving the ECCS throttle valve issues. The

licensee expected to be able to implement a design change during the next Unit 1

refueling outage starting in March 1998.

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E3 Engineering Procedures and Documentation

E 3.1 (Closedl Unresolved item (URI) 50-445/9717 05:50-446/9717 05: control room

emergency pressurization unit left above the design basis flow rate. This item was

lef t unresolved to determine the significance of leaving the flow above the

calculation limit and to deterrnine whether the other train was inoperable during the

time period when the as left flow was greater than 800 cfm.

a. Lnspection Scone f 37551. 92903)

The inspector reviewed Calculation 058, " Control Room LOCA lloss of coolant

accident) Dose Analysis," Revision 1, to determine what effect an as ' eft value of

817 cfm had on dose. The inspector also reviewed the licensee's findings

concerning the operability of the opposite trein.

b. Observations and Findinas

The inspector fc,und that the dl a,ince in dose to control room operators during a

design basis loss of coolant accident was minimal and did not exceed 10 CFR

Part 50, Part A, General Design Criterion 19 limits. The inspector noted that the

licensee had used a value of 888 cfm (highest rneasured flow) to conclude that the

pressurization unit would not have caused control room operators to exceed dose

limits during a design basis accident. This value was chosen to encompass the two

identified time periods where the as left value for flow was 817 cim. The inspector

concluded that this was appropriate.

The inspector reviewed Surveillance Test Procedures PPT SX 7520A, " Control

Rcom Ventilation Filter Test CPX VAFUPK 21," Revision 0, and PPT SX 7522B,

" Control Room Ventilation Filter Test CPX-VAFUPK 22," Revision O. These

procedures tested the control room filtration units in accordance with Technical

Specification Surveillance Requirements 4.7.7.1b,4.7.7.1d, and 4.7.7.1g and h.

Each surveillance required pressurization flow rate to be 800 cfm plus or minus

10 percent. The acceptance requirement of 720 - 880 cfm was incorporated into

each procedure. However, because the dcsign basis calculation assumed 800 cim,

any value above 800 cfm would be outside the design basis.

10 CFR Part 50, Appendix B, Criterion V, requires, in part, that activities affecting

quality be prescribed by documented instructions of a type appropriate to the

circumstances and that the instructions include quantitative acceptance criteria for

determining that important activities have been satisfr.ctorily accomplished. The

accepta. ice criteria used in Procedures PPT-SX 7520A and PPT SX 7522B was

inadequate because the values allowed operation of the pressurization units outside

the design basis calculation and did not account for measurement uncertainty. This

was a second example of a violation (50-445/9718 03; 50-446/9718 03,

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On September 30, the licensee informid the inspector that they had determir1d ,

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that, during the time that Train A had an as left flow value of 817 cfm (September

11,1994, through January 12,1996), Train B had been inoperable seven times for i

a total of 5 days,23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />, and 10 minutes. During the time that Train B had an

as left flow valve of 817 cfm (July 15,1996, through August 8,1997), Train A bad  !

been inoperable once for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 31 minutes. The licensee informed the  !

inspector that they intended to submit a supplement to their LER 50 445/97 006 l

which described the two porlods when the flow was lef t above design values. The j

i

inspector concluded that this was appropriate. -

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c. ' Conclusions

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Failure to incorporate design basis values for the control room pressurization units  ;

into surveillance test procedures led to leav!ng the flow rates above the design basis

on two occasions. This was a violation. The allowed range for flow would not

have caused control room operators to exceed allowable dose limits during a design

basis accident.

E4 Engineering Staff Knowledge and Performance

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E4.1 Failure to Follow Procedures for Temperature Measurina Device Accuracy

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a. Insoection Scope (37551)

>

As part of the followup to URI 50 445/9717 05;50 446/9717 05 and Followup

ltem 50-445/9717 02; 50-446/9717 02, the inspector reviewed the completed

Surveillance Work Order 5 97 501021 AA used to implement, Procedure PPT SX-

7505A, " Control Room Pressurization Test Train A," on August 8,1997. The

inspector compared the accuracles of the test equipment to procedural

requirements,

b. Observations and Findinas

Section 7.0, " Test Equipment," of the surveillance test procedure required a

temperature indicating device with an accuracy of 12'F. Section 7.0 of

Attachment 1 listed that Thermometer IC1473 was used during the test. The

inspector found that the accuracy of Thermometer IC1473 was 12.2'C

(approximately 14.0'F). Technical Specification 6.8.1 requires, in part, that the

licensee establish,~ implement and maintain procedures covering the activities

referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February 1970.

Appendix A requires specific procedures for each surveillance test listed in the

Technical Specifications. The failure to use a temperature measuring device with

the required accuracy is a violation of these requirements (50 445/9718 04; *

50-446/9718 04).

,

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' The licensee evaluated the latest surveillance test results and concluded that the-

as lef t flow values for both pressurization trains were still below design basis limits

when the larger uncertainty was assumed in the calculation. The inspector

concluded thtt, while the failure to follow procedures had a low safety significance,

it represented poor attention to detail by the engineers.

E8 Miscellaneous Engineering losues )

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E8.1 IClosed) Violation 50-446/9715 02: failure to translate design basis into drawings l

for a containment pressure relief valve mechantcal stop, in the enclosed Notice to  !

NRC Inspection Report 50 445/9715; 50 446/9715, the NRC concluded that the

information regarding the reason for the violation and the correctNe acVons taken

and planned were already adequately addressed on the docket and that a response

was not necessary unless the licensee concluded that the descriptions or corrective

actions did not a.acurately reflect their position. The licensee did not respond and

this item is closed.

IV. Plant Suonort

R1 Radiological Protection and Chemistry (RP&C) Controls

During plant tours, the inspector determined by direct observations in selected steas

that posting and labeling was in compliance with regulations and licensee

procedures. The inspector verified, at least weekly, that chemistry samples were

within Technical Specification and industry guideline limits.

V. Man,agement Meetinas

X1 Exit Meeting Summary

The inspector presented the results of the inspection to members of licensee management

at the conclusion of the inspection on October 16,1997. The licensee acknowledged the

inspector's findings. No proprietary information was identified.

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ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensu

R. C. Byrd, Manager, Smart Team 2

J. J. Kelley, Vice President, Nuclear Engineering and Support

D. R. Moore, Manager, Operations

A. H. Saunders, Supervisor, Testing

C. L. Terry, Group Vice President, Nuclear Production

INSPECTION PROCEDURES (IPs) USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP-71750: Plant Support Activities

- IP 92901: Followup Plant Operations

IP 92902: Followup Maintenance

IP 92903: Followup - Engineering

ITEMS OPENr.D AND CLOSED

Opened

50 445(4461/9718 01 NCV Safety evaluation not performed for procedure change

50 445(446)i9718-02 IFl Review of seismic evaluation of test skid connection

50-445(446)/9718 03 VIO Inadequate procedures for hydrogen recombiner

surveillance and control roorn pressurization surveillance

50 445(446)/9718-04 VIO Failure to use temperature instrument with the accuracy

required by procedure

Closed

50-445(446)/9718-01 NCV Safety evaluatine not performed for procedure change

50-445/95007 LER Engineered safety taature ic tr 'on caused by

feedwater recirculation vana ! .,ure

j 50-446/9715 01 VIO Operation in excess of.102 percent thermal power

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50 446/9715-02 VIO Failure to translate design basis into drawings for

containment pressure relief valve mechanical stop

50 4451446)/9717 05 URI Control room emergency pressurization unit left above

the design basis flow rate

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