ML20198P803

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Forwards Agenda for Facility Isolation Condenser Pipe Cracks,Including Diagrams
ML20198P803
Person / Time
Site: 05000000, Oyster Creek
Issue date: 06/28/1984
From: Holland D
GENERAL PUBLIC UTILITIES CORP.
To: Lombardo J
NRC
Shared Package
ML20151H203 List:
References
FOIA-86-26 NUDOCS 8606060395
Download: ML20198P803 (15)


Text

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NUCLEAR REGULATORY COMMISSION SUBJECT DATE OYSTER CREEK ISO. CONDENSER PIPE CRACKS June 28, 1984

Dear Mr. Lombardo:

Enclosed hereto is the copy of the Agenda for the above referenced subject matter which f

includes various diagrams.

}.I If you have any questions or comments, pler.se do not hesitate to contact me at s

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SIGNED DREW HOLLAND

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AGENDA Oyster Creek ISO. Condenser Pipe Cracks Initial Detection of Flaws Follow up Inspection Inspection Summary 1983 Inspection Summary Analysis Repair Options Topical Report Generic Letter 84-11 m

OYSTER CREEK ISOLATION CONDENSER PIPING SIM1ARY OF EVENTS o DURING HYDRO TEST OF "A" CONDENSER, WATER SEEN DRIPPING F1t0M CONDDSATE PIPING o INSULATION STRIPPED, LEAK FOUND (NE-2-12) o ITT NE-2-12, 2 THRU-WALL CRACKS DETECTED o ITT OF ADD _'TIONAL CONDENSATE VELDS DETECTED

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ADDITIONAL FOLLOW-UP INSPECTIONS 1984 i

ISO. CONDENSER INSIDE DIW 1

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8 STEAM OUTSIDE DIW 124 TOTAL i

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61 STEAM CLEAN-UP SYSTEM CUTSIDE DIO

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L OYSTER CREEK ISOLATION CONDENSER PIPING

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INSPECTION

SUMMARY

"A" STEAM LINE CONFIRMED - 6 SUSPECT

-2 "B" STEAM LINE CONFIRIED - 9 SUSPECT

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-3 "B" CONDENSATE LINE CONFIRMED - 1 SUSFCCT

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P G OYSTER CREEK 1981 INSPECTIONS DIW Jll OUTSIDE RECIRC. SYSTEM 31 ISO. COND. SYSTEM 2 COND. 5 STEAM 3 STEAM 5 COND. CLEAN-UP SYSTEM 5 CORE SPRAY SYSTEM 5 2 SHUTDOWN COOLING SYSTEM 2 '.] t_ ,wp t g, k s- ^- -^ - ^ '(9 g, p wg + + + q W-rMwggg g 4 9

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l I OYSTER CREEK ISOLATION CONDENSER PIPING MAJOR ACTION ITEMS l l o DETERMINE FAILURE MECHANISM o RDt0VE 3 SPOOL PIECES h o GPUN/CONTRACIt)R EIAMINATION I NRC(BROOKHAVEN)EIAMINATp o .f V' 3 o CRACK GROVTH ANALYSIS l o SIZING OF INDICATIONS REQUIRED d i o SPOOL PIECE REPLACEME.T/0VERLAY V o PARALLEL PLANNING EFFORT 8- -. - - - -.,....,,,-..,,,.,.,-.4.,,, y,,, % ww ywy e, w,4-y yp,w,y.,, w

= OYSTER CREEK } ISOLATION CONDENSER PIPING I REPAIR OPTIONS o NO REPAIR - LEAVE AS-IS FOR 1 FUEL CYCLE t o WELD OVERLAY o SPOOL PIECE REPLACEMENT o LOCAL REPAIR o COMBINATION OF THE ABOVE o SYSTEM REPLACEMENT 1 i i j ._om_...x,_m.

198f4 ReDalr Program 27 Total Indications 17 Steam (A8B) 7 - Spool piece 10 --overlay s 10 Condensate (A&B) ] 2 - Spool piece 8 - overlay I e j

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g 1 lv cMito UNITED STATES o,, [ g NUCLES.R REGULATORY COMMISSION E WASHINGTON, D. C. 20$55 E o,.....,/ June 12,1984 Docket No.50-219-- MEMORANDUM FOR: Dennis M. Crutchfield, Chief Operating Reactors Branch #5, DL FROM: James J. Lombardo, Project Manager Operating Reactors Branch #5, DL

SUBJECT:

FORTHCOMING MEETING WITH GPU NUCLEAR CORPORATION (GPU) j Date & Time: Wednesday June 20, 1984 10:00 am Location: Room P-110, Phillips Building Bethesda, Maryland

Purpose:

To update the Commission on pipe cracking in the Isolation Condenser System at Syster Creek in the areas of inspection, diagnosis and repair. In addition, GPU response to Generic Letter 84-11 will be discussed. Aaenda: - detection of through-wall flaw - follow-up inspections - results of inspections - results of sample defect examinations - GPUN repair philosophy and methods - Topical Report contents (7/15) - Generic Letter 84-11 contents (7/15)

Participants:

NRC GPUNC W. Hazelton J.S. Chardos W. Koo D. Covill D. Smith D. Holland . J. Lombardo' J. Mancinelli g mes J. mbardo, Project Manager l erating eactors Branch #5 Division of Licensing \\ d el cc: See next page i eh}i', d' / y,,. %%1L A /m.

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