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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) ML20212C0381997-10-19019 October 1997 Safety Evaluation Accepting License Request for Deviation from Commitment to Meet Section III.G.2.c of App R to 10CFR50 Re Fire Protection of Safe Shutdown Capability for Plant ML20217E3491997-09-22022 September 1997 Safety Evaluation Authorizing Licensee Proposed Alternative for Current Interval Insp Program Plan ML20133J5551997-01-15015 January 1997 Safety Evaluation Granting Licensee Request Proposing Not to Perform Increased Frequency Testing on a Charging Pump at Virgil C Summer Nuclear Station ML20128G2931996-10-0202 October 1996 Safety Evaluation Supporting Amend 135 to License NPF-12 ML20128F4221993-02-0909 February 1993 Safety Evaluation Re Nuclear Physics Methodology for Reload Design.Request to Perform Reload Analyses Approved ML20056A7931990-08-0606 August 1990 Safety Evaluation Re Capability of Plant to Meet Requirements of Branch Technical Position Rsb 5-1, Design Requirements of RHR Sys. Design Satisfies License Condition 4 ML20245F5061989-06-22022 June 1989 Safety Evaluation Re Request for Relief from Section XI Re Hydrostatic Test Requirement ML20244D7361989-06-12012 June 1989 Safety Evaluation Accepting Util Response to Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability for All Domestic Operating Reactors ML20195B4421988-10-28028 October 1988 Safety Evaluation Supporting Amend 74 to License NPF-12 ML20151K0901988-07-28028 July 1988 Safety Evaluation Supporting Util Proposed Implementation of ATWS Rule Pending Resolution of Tech Spec Issue ML20151K7771988-07-27027 July 1988 Safety Evaluation Supporting Util Request to Deviate from Recommendations of Reg Guide 1.97 Re Instrumentation to Monitor Containment Temp ML20151R8561988-04-19019 April 1988 Safety Evaluation Supporting Related Inservice Testing Program & Request for Relief of Utils ML20236R4111987-11-13013 November 1987 Safety Evaluation Supporting Conformance to Reg Guide 1.97, Rev 3 ML20236K7701987-11-0505 November 1987 SER Accepting Util 831104 & 870401 Responses to Item 2.2.1 of Genreic Ltr 83-28 Re Equipment Classification Programs ML20237H3661987-07-22022 July 1987 Corrected Page to Safety Evaluation Issued W/Amend 67, Changing Second Paragraph & Deleting Third Paragraph on Page Three ML20214S8881987-06-0303 June 1987 Safety Evaluation Rept Granting Relief from Hydrostatic Testing After Repair to ASME Code Section Xi,Class 1,reactor Coolant Pump Seal Injection Line ML20209H3331987-01-30030 January 1987 SER Supporting Util 831104 Response to Generic Ltr 83-28, Item 4.5.2 Re on-line Testing of Reactor Trip Sys Reliability ML20213A5611987-01-30030 January 1987 SER Accepting Util 831104 Response to Generic Ltr 83-28,Item 2.1 (Part 2) Re Vendor Interface Program for Reactor Trip Sys Components ML20212F2841986-12-22022 December 1986 Safety Evaluation Supporting Amend 57 to License NPF-12 ML20211M4161986-12-0909 December 1986 Safety Evalution Supporting Licensee 860123 Submittals Re Fast Neutron Fluence for Fracture Toughness Requirements for Protection Against PTS Events (10CFR50.61) ML20203N0151986-09-15015 September 1986 Safety Evaluation Re Generic Ltr 83-28,Items 3.1.3 & 3.2.3, Post-Maint Testing (RTS Components,All Other Safety-Related Components). Response Acceptable ML20199D4211986-06-0909 June 1986 SER on Util 831104 & 860423 Responses to Generic Ltr 83-28, Item 1.2 Re post-trip Review Data & Info Capabilities.Data & Info Capabilities Acceptable ML20211A2571986-05-22022 May 1986 Safety Evaluation Accepting Mods to App R,Clarified by Generic Ltrs 81-12 & 83-33,to Prevent Spurious Equipment Operation Caused by fire-induced Conductor or Cable Faults, Facilitate Operator Actions & Resolve Addl Circuit Concerns ML20154A0621986-02-24024 February 1986 Safety Evaluation Supporting 850930 & 1204 Responses to 850802 & 1104 Requests,Respectively,For Addl Info Re Generic Ltr 83-28, Required Actions Based on Generic Implications of Salem ATWS Events ML20154D1921986-02-14014 February 1986 Sser 1 Re Licensee 851204 Response to Generic Ltr 83-28, Item 3.2.2 Concerning Procedures & Programs to Review Info on safety-related Equipment.Response Acceptable & Meets Intent of Generic Ltr 83-28 ML20136B2291985-11-0707 November 1985 Safety Evaluation Supporting Amend 46 to License NPF-12 ML20209H8411985-11-0404 November 1985 Safety Evaluation Re Response to Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1,3.2.2,4.1 & 4.5.1.Response to Item 3.2.2 Incomplete & Addl Info Required ML20137S5781985-09-24024 September 1985 SER Approving Licensee 831104 & 0715 Responses to Generic Ltr 83-28,Item 1.1 Re post-trip Review.Program & Procedures for Restart from Unscheduled Reactor Trip Acceptable ML20133H7321985-08-0202 August 1985 SER Re Util 831104 Response to Generic Ltr 83-28,Items 4.2.1 & 4.2.2 Concerning Reactor Trip Sys Reliability. Licensee Should Add Undervoltage Trip Attachment to Trending Program ML20128A2181985-06-21021 June 1985 SER of Util Response to Generic Ltr 83-28,Item 1.1 Re post-trip Review.Listed Addl Info Required Before Review Can Be Completed 1999-02-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D6401999-10-31031 October 1999 Rev 2 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0202, Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With ML20216J4191999-09-24024 September 1999 Part 21 Rept Re 990806 Abb K-Line Breaker Defect After Repair.Vendor Notified of Shunt Trip Wiring Problem & Agreed to Modify Procedure for Refurbishment of Breakers RC-99-0180, Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression1999-09-0808 September 1999 Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression RC-99-0183, Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With ML20211K6161999-08-31031 August 1999 Rev 2 to VC Summer Nuclear Station,Colr for Cycle 12, Dtd Aug 1999 RC-99-0168, Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed1999-08-19019 August 1999 Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed ML20210M7071999-07-31031 July 1999 Rev 1 to VC Summer Nuclear Station COLR for Cycle 12 ML20211C2201999-07-31031 July 1999 Rev 1 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0163, Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0137, Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0122, Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With ML20206H2971999-05-0505 May 1999 Part 21 Rept Re Common Mode Failure for magne-blast Breakers.Vc Summer Nuclear Station Utilizes These Breakers in Many Applications,Including 7.2-kV EDG Electrical Buses RC-99-0103, Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With ML20206K2421999-04-30030 April 1999 Rev 0 to COLR for Cycle 12 for Summer Nuclear Station RC-99-0087, Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory1999-04-15015 April 1999 Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory RC-99-0083, Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0063, Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced1999-03-26026 March 1999 Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced ML20196K5421999-03-22022 March 1999 Rev 2 to VC Summer Nuclear Station,Training Simulator Quadrennial Certification Rept,1996-99, Books 1 & 2. Page 2 of 2 Section 2.4.4 (Rev 2) of Incoming Submittal Were Not Included RC-99-0055, Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 9903121999-03-16016 March 1999 Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 990312 RC-99-0050, Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20206R5241998-12-31031 December 1998 Santee Cooper 1998 Annual Rept RC-99-0052, Vsns 1998 Annual Operating Rept. with1998-12-31031 December 1998 Vsns 1998 Annual Operating Rept. with RC-99-0004, Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With ML20206R5191998-12-31031 December 1998 Scana Corp 1998 Annual Rept ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station RC-98-0223, Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method1998-12-16016 December 1998 Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method RC-98-0222, Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams RC-98-0208, Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With ML20207J5701998-10-31031 October 1998 Non-proprietary Rev 1 to WCAP-14955, Probabilistic & Economic Evaluation of Rv Closure Head Penetration Integrity for VC Summer Nuclear Plant ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20154K7901998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15101, Analysis of Capsule W from Sceg VC Summer Unit 1 Rv Radiation Surveillance Program RC-98-0184, Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With ML20154K8041998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15103, Evaluation of Pressurized Thermal Shock for VC Summer Unit 1 RC-98-0166, Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RC-98-0153, Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0131, Monthly Operating Rept for June 1998 for VC Summer Nuclear Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for VC Summer Nuclear Station ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) RC-98-0113, Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0100, Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 1 ML20217G7411998-04-22022 April 1998 Rev 1 to VC Summer Nuclear Station COLR for Cycle 11 RC-98-0076, Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure1998-04-17017 April 1998 Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure RC-98-0084, Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 1 ML20212H1421998-03-0202 March 1998 Interim Part 21 Rept SSH 98-002 Re EG-B Unit That Was Sent to Power Control Svcs for Determination of Instability & Refurbishment of a Dg.Cause of Speed Oscillations Unknown. Completed Hot Bore Checks on Power Case 1999-09-08
[Table view] |
Text
'o,, UNITED STATES g g NUCLEAR REGULATORY COMMISSION 5 l WASHING TON, D. C. 20555
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTINGAMEN0MENTNO.74TOFACILITYOPERATINGLICENSENO.NPFg SOUTHCAR0lRAELECTRIC&GASCOMPANY SOUTH CAROLINA PUBLIC SERVICE AUTHORITY VIRGIL C. SUMMER NUCLEAR STATION, UNIT 00. 1 DOCKET NO. 50-395
1.0 INTRODUCTION
In a letter dated March 8, 1988, South Carolina Electric & Gas Company (the licensee) schmitted a request for changes to the Virgil C. Sumer Nuclear Station, Unit No. 1, Technical Specifications (TS), Section 3.9.12. "Spent Fuel Assembly Storage," Section 5.3.1, "Fuel Assemblies,"
and Section 5.6, "Fuel Storage." The changes to these TS Sections were submitted as a result of the proposed changes in reactor fuel from Westinghcuse's LOPAR (low parasitic) fuel to Westinghcuse's enhanced burnup fuel (Vantage 5).
By letters dated August 31, 1988 and September 30, 1988, the licensee provided revised source term inputs and radiological analyses of postu-lated accidents to support the utilization of the Vantage 5 fuel.
The purpose of the proposed arendment is to modify Figures 3.9-1 and 3.9-2 of Section 3/4.9.12. These figures depict the acceptable and the unacceptable values of fuel assembly exposure (i.e., burnup), as a function of fuel enrichment, to permit storage in Regions 2 and 3 of the spent fuel pool. The proposed changes to Technical Specifications 5.3.1 and 5.6.1.1 limit the maximum enrichment to 4.25 weight percent (w/o) lj-235 and require a minimum burnup of 19,000 MWD /MTU (megawatt-days per metric ton uranium) for fuel stored in Region 2 of the spent fuel pool and 39,750 MWD /MTU for fuel stored in Region 3 of the spent fuel pool.
The proposed changes to TS 3.9.12, 5.3.1, and 5.6 are to reflect revised storage limitations for the mix of LOPAR and the Westinghouse Vantage 5 fuel to be utilized in the core during the fif th cycle at the Sumer Station ind for the Vantage 5 fuel that will be used in all subsequent cycles.
2.0 EVALUATION The ifcensee has proposed that fresh fuel racks used for Vantage 5 fuel assemblies be limited to a maximum enrichment cf 4.25 w/o U-235. The present TS allow fuel with an enrichment of 4.3 w/o U-235. The spent fuel racks are divideo into three regions. All regions contain stainless 8811020020 DR 001020 p ADOCK 05000395 PNV
2 steel cells, one for ea:h stored assembly. The licensee has proposed that Region 1 accept freshly discharged fuel assemblies with enrichments up to 4.25 w/o U-235 while Regions 2 and 3 accept assemblies with up to 4.25 w/o U-235 initial enrichment provided they have burnups sufficient to meet criticality limits. These burnups are proposed as 19,000 MWD /MTV and 39,750 MWD /MTU for Regions 2 and 3, respectively. Regions 1 and 2 are poisoned, i.e., contain fixed boron absorbers. Present TS Section 5.6 allows fuel with an enrichment of 4.3 w/o U-235 and requires a minimum burnep of 20,000 MWO/MTV for Region 2 and 42,000 MWD /MTV for Region 3 of the spent fuel ecol.
The licensee has performed criticality analyses for Regions 1, 2 and 3 for standard Westinghouse and Vantage 5 fuel assemblies using approved computer codes. The results meet the NRC criteria of a spent fuel peak of k,ff less than 0.95 (for unborated water) including uncertainties. ;
)
The licensee also pcrformed criticality analysis of fresh fuel racks in a l full range of moderator densities using approved computer codes. The i results shew that rack k,ff values are less than 0.95 inclu: ling uncertain- l ties.
The staff tas reviewed the criticality analyses for both the spent fuel racks of Regions 1, 2 and 3 and for the fresh fuel racks. Since the results mest the staff's criteria for a spent fuel peak of k less than 0.95(forunbaratedwater)includinguncertaintiesandthesbf's less than or equal to 0.98 in the low criteriamoderator density for fresh fuel racks region and k(k,f,less than or equal to 0.95 in the high densityregion),thestaffconbdesthattheproposedchangestoFigures 3.9-1 and 3.9-2 of TS 3.9.12 and the proposed changes to TS 5.3.1 and 5.6 are acceptable.
3.0 DESP.GN BASIS ACCIDENT ANALYSIS RELAT!VE TO EXTENDED FUEL BURNUP The licensee's intent to utilize Vantage 5 fuel will result in the lead fuel rod having an average burnup as high as 60,000 MWO/MTU. In an August l 31, 1988 submittal, the licensee provided their evaluation of the reactor I
roolant and core source terms for the vantage 5 fuel. In the licensee's September 30, 1988 submittal, they provided their assessment of the radiological consequences, based upon the utilization of Vantage 5 fuel, for the design basis accidents presented in Chapter 15 of the licensee's FS3 The licensee concluded that the radiological consequences of postulated accidents as a result of the utilization of the Vantage 5 fuel, when compared to operation with the present LOPAR fuel, would result in a decrease in the gamma and' beta skin doses but an increase in the thyroid dose.
The staff reviewed the licensce's subms.tals and also reviewed a publica-tion which was prepared for the NRC entitled, "Assessment of'the Use of Extended Burnup Fuel in Light Water Reactors," NUREG/CR 5009, February 1988. The NRC contractor, the Pacific Nortnwest Laboratory (PNL) of Battelle Memorial Institute, examined the changes that conld result in the
NRC Design Basis Accident (DBA) assumptions, described in the various Standard Review Plan (SRP) sections and/or Regulatory Guides, that could result from the use of extended burnup fuel (up to 60,000 MWD /MT). The staff agrees that the only DBA that could be affected by the use of extended burnup fuel, even in a minor way, would be the potential thyroid doses that could result from a fuel handling accident. PNL estimates that I-131 fuel gap activity in the peak fuel rod with 60,000 MWD /MT burnup could be as high as 12%. This value is approximately 20% higher than the value normally used by the staff in evaluating fuel handling accidents (Regulatory Guide 1.25. "Assumptions Used for Evaluating the Potential Radiological Consequences of a Fuel Handling Accident in the Fuel Handling and Storage Facilities for Boiling and Pressurized Water Reactors").
PNL concluded in their report that for fuel damage accidents, "The percentage of fission-product inventory released from the fuel would not likely change as a result of the extended burnup; however, the fission-
, product inventory in the fuel would change for the long half-life fission l products and actinides ...." PNL also concluded that the actinides would only minimally contribute to doses compared to the fission products and that the main concern for thr! actinides would be from the long-term effects of inhalation (vegetables, (lung) milk, and meatdose) andin,ingestion raised or fed onoffood foodgrown products in, con-taminated soil. PNL concluded that the inventory of fission products, cesium-137 and strontium-90 would iecreasa by a factor of almost 2 in the extended burnup fuel. However, the staff has concluded that their contribution to dose would be minimal.
For the fuel handling accident, PNL concluded that the use of Regulatory l Guide 1.25 procedures for the calculation of accident doses for extended burnup fuel may be utilized. These procedures give conservative estimates for noble gas release fractions that are above calculated values for peak rod burnups of 60,000 MWD /MTV. lodine-131 inventory, however, may be up to 20% higher than that predicted by Regulatory Guide 1.25 procedures.
l The staff, therefore, reevaluated the fuel handling accidents for the Summer Station assuming an increase in iodine gap activity in the fuel damaged in a fuel handling accident which was 20% higher than that assumed using Regulatory Guide 1.25. Table 1 presents the fuel handling accident thyroid doses. The assumptions, which were utilized in the staff's evaluation, were the see as those presented in Table 15-5 of the V. C.
Sunser NW1 ear Station. Unit No.1 Sa'ety Evaluation Report (NUREG-0717),
February 1951, with the following oceptions:
pcwer Peaking Factor l = 1.68 Number of fuel rods assumed failed a 264 l
J
g- -
. e
~
+ .-
Table 1 Thyroid Doses as a Consequence of DBA Fuel Handling Accidents r
Exclusion Area low Fopulation Zone Thyroid Dose (Rem) Thyroto Dose (Rem) I Fuel Handling Accident ,
In Fuel Building 17 2.1 In Reactor Building 115 14 The staff concludes that the only potential increased doses potentially resulting from OBA with extended fuel burnup to 60,000 MWD /MT is the thyroid dose resulting from fuel handling accidents and these doses I remain well within the 300 Rem thyroid exposure guideline values set forth in 10 CFR Part 100 and that this small calculated increase above '
i the present calculated dose presented in Table 15-4 of the V. C. Suseer SER (NUREG-0717) is not significant.
4.0 ENVIRONMENTALCONS10 ERAT!g Pursuant to 10 CFR 51.21, 51.32, and 51.35, an environmental assessment and finding of no significant impact have been prepared and published in the Federal Register (53 FR 43486) on October 27, 1988. Accordingly, based upon the enITUonmental assessrent, the Cossission has determined that the issuance of this amendrent will not have a significant effect on -
the quality of the human environment.
5.0 CONCLUSION
The Commission has issued a "Notice of Consideration of Issuance of r Amendment to Facility Operating License and Proposed No Significant .
Hazards Consideration published in Determination the FEDERAL REGISTER and1,Opportunity on Jur,*/ 1988 (53 FR 20046) andfor Hearin consulted with the State of South Carolina. No public coceents or ;
requests for hearing were received, and the State of South Carolina did not have coseents.
The staff has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the !
public will not be endangered by operation in the proposed manner, and (2) such activities will be conducted in compliance with the Coesnission's regulations and the issuance of this amendment will not be inimical to the conson defence and security or to the health and safety of the public.
Principal Contributors: John J. Hayes, Jr. :
Shi Liang Wu !
Dated: October 28, 1988 i
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