IR 05000269/1988005

From kanterella
(Redirected from ML20148E456)
Jump to navigation Jump to search
Insp Repts 50-269/88-05,50-270/88-05 & 50-287/88-05 on 880217-0316.No Violations Noted.Major Areas Inspected:Maint, Operations,Surveillance,Physical Security & Design Changes
ML20148E456
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 03/21/1988
From: Peebles T, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20148E450 List:
References
50-269-88-05, 50-269-88-5, 50-270-88-05, 50-270-88-5, 50-287-88-05, 50-287-88-5, NUDOCS 8803250157
Download: ML20148E456 (8)


Text

- - - - _ - _ _ - - - _ _ - - _ _ _ _-

naEteo UNITEo STATES

.

/' .

'

NUCLEAR REGULATORY COMMISSION

-[.

y * t)/q,j j

REGION 11 101 MARIETTA STREET. * i e ATLANTA, GEORGI A 30323

%

4.....$

Report Nos: 50-269/88-05, 50-270/88-05, and 50-287/88-05 Licensee: Duke Power Company 422 South Church Street Charlotte, NC 28242 ,

Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 Facility Name: Oconee Nuclear Station Inspection Conducted: bruary 17 - March 16, 1988 Inspectors- , 28 /2 c3fd}fW P. H. Ski n~~ , Senio Resident Inspector tam Signed Lh'D.~%ert,Residen

~

LInspector a/DArr Gat ( Sigried Approved by: Y //

T. Al Peebles, Section Chief

_

_J /J r [y Date' Signed Division of Reactor Projects SUMMARY Scope: This routine, announced inspection involved resident inspection on-site in the areas of operations, surveillance, maintenance, physical security, engineered safeguards features lineups, nonroutine reporting and design change Results: Of the seven areas inspected, no violations were identifie .

K

'

8803250157 880321 PDR ADOCK 05000269 O DCD

-. .. . . _ . - - - . - .__

. - _ . . - . _ - _ - . _ . . . - _ - - - - - . - - - -

  • -

. .

.

.

REPORT DETAILS Persons Contacted Licensee Employees

  • M. Tuckman, Station Manager J. Davis, Technical Services Superintendent W. Foster, Maintenance Superintendent T. Glenn, Instrument and Electrical Support Engineer
  • C. Harlin, Compliance Engineer J. McIntosh, Administrative Services Superintendent
  • F. Owens, Assistant Engineer, Compliance R. Sweigart, Operations Superintendent L. Wilkie, Integrated Scheduling Superintendent Other licensee employees contacted included technicians, operators, mechanics, security force members, and staff engineer NRC Resident Inspectors P. H. Skinner
  • L. D. Wert
  • Attended exit intervie . Exit Interview The inspection scope and findings were summarized on March 16, 1988, with those persons indicated in paragraph 1 abov The inspectors described the areas inspected and discussed in detail the inspection findings listed below. Dissenting comments were not received from the licensee. Proprieta ry information is not contained in this repor Item Number Status Description / Reference Paragraph 270/87-44-01 Closed Failure to Document Component Verification Actions LER 269/87-05, Rev. 1 Closed Potential Tripping of High Pressure Injection Pumps During Starting LER 270/86-01 Closed Turbine / Reactor Trip Due to Inadequate Communication of a Relay Design Feature LER 270/87-05 Closed Fire Wall Breached Causing Violation of Technical Specification w

-______ _ - - _ -______ - -- - _- . _ _ _ _ _ _

. . .

-

.

. ,270,287/87-48-01 Closed Correction of Potential Loss of Siphon !

Effect on Emergency Condenser Cooling Water (ECCW) Syste :

3. Licensee Action on Previous Enforcement Matters

'

(Closed) Violation. 50-270/87-44-01: Failure to Document Component

Verification Actions. Corrective actions as documented in the licensee's letter of December 31, 1987, have been reviewed and found acceptabl The resident inspectors have observed rigid adherence in implementation

and documentation of component verification action . Plant Operations (71707) The inspectors reviewed plant operations throughout the reporting
period to verify conformance with regulatory requirements, technical specifications (TS), and administrative controls. Control room

'

logs, shift turnover records, Unit 2 Refueling log and equipment l removal and restoration records were reviewed routinely. Discussions were conducted with plant operations, maintenance, chemistry, health physics, instrument & electrical (I&E), and performance personne Activities within the control rooms were monitored on an almott daily basis. Inspections were conducted on day and on night shifts,

>

during week days and on weekends. Some inspections were made during shift change in order to evaluate shift turnover performanc *

Actions observed were conducted as required by the Licensees Administrative Procedures. The complement of licensed personnel on i

! each shift inspected met or exceeded the requirements of TS.

'

Operators were responsive to plant annunciator alarms and were

cognizant of plant condition Plant tours were taken throughout the reporting period on a routine basi The areas toured included the following:

Turbine Building Auxiliary Building .

! Units 1,2, and 3 Electrical Equipment Rooms l Units 1,2, and 3 Cable Spreading Rooms Station Yard Zone within the Protected Area

Standby Shutdown Facility

'

Units 1,2, and 3 Penetration Rooms Unit 2 Containment Condenser Circulating Water Intake Structure f During the plant tours, ongoing activities, housekeeping, security, ,

i equipment status, and radiation control practices were observed.

! Unit 1 began the report period at 100% power. On 2/17/88, power was reduced to 65 due to a loss of one main feedwater pump due to a

, broken jack shaft gear. Af ter repairs, power was increased to 100%

,

. - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ .

.-___ ___- - _ _ _ _ _ _ __ . _ _ _ _ _

  • '

.c .

.

.

on 2/25/88 and the unit operated at 100% for the remainder of the report perio Unit 2 remained in a refueling outtT Startup is currently scheduled for 4/11/8 Unit 3 operated at 100% power for the entire report period. A small steam generator tube leak remained stable at approximately .025 gp . Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural and performance adequacy. The completed tests reviewed were examined for necessary test prerequisites, instructions, acceptance criteria, technical content, authorization to begin work, data collection, independent verification where required; handling of deficiencies noted, and review of completed work. The tests witnessed, in whole or in part, were inspected to determine that approved procedures were available, test equipment was calibrated, prerequisites were met, tests were conducted according to procedure, test results were acceptable and systems restoration was complete Surveillances reviewed or witnessed in whole or in part:

PT/0/A/0400/05 Standby Shutdown Facility Auxiliary Service Water Pump Performance Test MP/0/B/1300/66 Monthly Inspection of Conderser Circulating Water Pump Flange Boot and Equal .ition Line PT/0/A/0400/04 SSF Diesel Engine Service Water Pump Performance Test No violations or deviations were identifie . Maintenance Activities (62703) Maintenance activities were observed and/or reviewed during the reporting period to verify that work was performed by qualified personnel and that approved procedures in use adequately described work that was not within the skill of the trad Activities, procedures and work requests were examined to verify proper authorization to begin work, provisie's for fire, cleanliness, and exposure control, proper return of equipment to service, and that limiting conditions for operation were me Maintenance reviewed or witnessed in whole or in part:

WR 96164C Temporary Closure, Emergency RB Hatch (TN/2/A/TM0345/0/I Installation of Closure Plate on U-2 RB Emergency Hatch)

WR 99520B TN/2/A/2609/00 Moisture Separator Reheater 2B1 Tube Bundle Replacement and Modification

. .

,

.

.

WR 14038C Repair SSF-CCW 284 WR 55280A PM on 2KI Inverter per IP/0/A/3C11/01 WR 98344B TN/2/A/2174/00 Installation of Nuclear Station Modification to Emergency Power Switching logic (NSM-2174)

No violations or deviations were identifie . Resident Inspector Safeguards Inspection (71881)

In the course of the monthly activities, the Resident Inspectors included review of portions of the licensee's physical security activities. The performance of various shifts of the security force was observed in the conduct of daily activities which included; protected and vital areas access controls, searching of personnel, packages and vehicles, badge issuance and retrieval, escorting of visitors, patrols and compensatory post In addition, the inspectors observed protected area lighting and protected and vital areas barrier integrity, and verified interfaces between the security organization and operations or maintenanc Mo violations or deviations were identifie . Inspection of Open Items (92701)

The following open items are being closed based on review of licensee reports, inspection, record review, and discussions with licensee personnel, as appropriate:

(Closed) LER 269/87-05, Revision 1: Potential Tripping of High Pressure Injection Pumps During Startin This revision provided additional information on the analysis that was performed including graphical results of engineering calculations. There were no changes to the corrective actions as a result of this revision, therefore this item is closed as discussed in IR 269,270,287/87-3 (Closed) LER 270/86-01: Turbine / Reactor Trip Due to Inadequate Communication of A Relay Blocking Switch Design Featur This turbine / reactor trip occurred as a result of a communication breakdown between transmission personnel and operation The corrective action for this event has been performed and reviewed by the inspecto Based on this review this item is close (Closed) LER 270/87-05: Fire Wall Breached Causing Violation of Technical Specification. This LER was concerned with two five inch holes that were cut into the fire wall between the turbine building and the auxiliary building. Due to an interruption of the work, the breach was not recognized for 105 day The corrective action was to conduct training of Construction and Maintenance Division personnel that perform this work in administrative controls and work controls on fire barrier The inspector reviewed records to

- - -_____ _

' '

. .

.

.

indicate all training had been completed as of February 10, 198 Bated on this review, this item is close (Closed) Inspection Followup Item 50-269,270,287/87-48-01: Correction of potential loss of siphon effect on emergency condenser cooling water (ECCW) system. The inspector reviewed the corrective actions taken by the licensee for agreement with commitments as documented in Inspection Report 50-269,270,287/87-48; The inspector observed an inspection of the Unit 2 condenser circulating water (CCW) flange rubber boots and drain tube Lake Keowee level was just above the aqualization line quick disconnects (about 790 f t.) and a small inflatable raf t was utilized in each CCW pump bay to inspect the boot and drain tube Maintenance procedure MP/0/B/1300/66 was utilized to complete the inspectio The inspector feels that this inspection (scheduled monthly) is satisf actory to ensure no lines or couplings are broken or disconnected until the permanent corrective action is complete i The inspector observed thi.t on the Unit 2 CCW pumps the licensee has installed flexible connectors from the drain tube couplings, around a lower pump flange and connected to conduit which is attached to the pump's suction lin This is expected to prevent any future failure of the tubes or couplings in the disconnect area by minimizing any vibration at the coupling due to turbulence in the suction wel This action is expected to be taken on the other CCW pumps within a few months, ii After a close examination of the actions involved, the licensee has decided not to change the Emergency Operating Procedures to require an immediate inspection of the pressure equalization lines in the event of a loss of power to the CCW pump The event which would require the ECCW system siphon effect to be relied upcn is a station blackout. By the time operators could get down to the CCW flange boot and drain tubes to inspect them, air in leakage through any broken or disconnected tubes would have adversely effected the ECCW siphon effect, it should be noted that this er. tire situation is only a possible problem if Keowee lake level is below the equalization line disconnect Station procedures require that anytime events occur which require the Safe Shutdown Facility (SSF) to maintain any unit in hot shutdown then actions will be taken to install the SSF dedicated submersible pump to supply water to the Unit 2 CCW inlet piping for extended SSF operation if the ECCW siphon effect fails, i Provisions are on hand at the CCW pump area for rapid sealing or repairs of any broken conduit that is discovered during an inspectio The inflatable raft, foot air pump and other required material is stored in a box on the CCW pump structur _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ ______~

-

.

.

'..

n 6' Unit 2 End of Cycle Refueling Outage (71700) (Unit 2)

Unit '2 remained in the refueling outage (which began on February 3)

throughout this report perio With just over_ half of the scheduled

-

outage days elapsed, the shutdown work war, far enough ahead of schedule that the startup date has been moved up three days. The inspectors i witnessed portions of a number of jobs in progress including the i following: Defueling operations, chemical cleaning of steam generators

,

(SG), replacement of :SG feedwater nozzles, cleaning of Low Pressure

-

. Injection Coolers and Reactor Building Cooling Units, installation of

Reactor Coolant System cold leg dams, extensive electrical generator rotor work, rework of valves, feedwater pump rebuilding, replacement of

,

noisture separator reheater tube bundles, and installation of several

,

major nuclear station modification Chemical cleaning of the SG's has been completed. Approximately 4700

~

pounds of material was removed from the 'B' SG, about 4100 pounds from the 'A' SG. Sludge lancing is in progress and is expected to remove an additional 500-700 pounds of material from each generato . Nonroutine Reporting Program (90714)

The inspector reviewed the licensee's administrative control programs for review, evaluation and reporting of nonroutine events or issue The

,

Administrative Policy Manual (APM) (Section 2.8) and the Oconee Nuclear Station (ONS) Compliance Manual (Sections 4.9, 5.1 and 5.3) outline the key responsibilities and processes of this progra The Problem

. Investigation Reporting (PIR) program as described by the APM and ONS

Station Directive 4.5.5 serves as the basis for the process of i documenting an evaluation and resolution of any identified problem. The PIR process includes provisions for recognition and reporting of events i

covered by 10 CFR Part 21 as well as 10 CFR 50.73 and other reporting requirements. The resident inspectors review PIRs on a daily basis. The i investigation, resolution and corrective actions of PIRs of interest are

! closely followed by the inspectors.

!

l The inspector also reviewed the licensee's administrative controls for i review, evaluation and resolution of vender bulletins and circulars.

l Duke Power Company's (DPC) Nuclear Production Department Directives

Manual describes the Operating Experience Program carried out primarily I by DPC Generai Office personnel. This program includes the review and

! evaluation of Vendor Information Letters, Information Notices (NRC), INP0

Good Practices and Significant Operating Experience Reports. The program i clearly sets forth the processes to be used and defines implementation j responsibilities.

l No violations or deviations were noted in this area.

!

I i

}

[

_ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ .

' *

, ,

~

.

1 Design, Design Changes, and Modifications (37700)

The inspectors reviewed various design changes to ascertain that the changes were reviewed and approved in accordance with 10 CFR 50.59, lechnical Specifications and established QA/QC controls, controlled by approved procedures and that changes to the inservice inspection and test program were updated as required by the cnange. In addition, records were reviewed to assure that the modifications were tested by appropriate procedures and the results of the test reviewed by management personne The inspector also reviewed as-built drawings, operating procedures, surveillance procedures and training associated with the modificatio The specific modifications reviewed were the following: NSM - ON 12493 - Unit 1 - This modification extended the suction of the Motor Driven Emergency Feedwater Pumps to within 12 inches of the bottom of the hotwell, NSM - ON 22680 - Unit 2 - This modification changed the BTU Limits associated with the Integrated Control Circuits to inactivate the limit if power is greater than 25% and activate the limit if power is less than 25%. This modification is a B&W Owners Group recommendation as discussed in NUREG 1231, Safety Evaluation Report Related to Babcock & Wilcox Owners Group Plant reassessment Program, NSM - On 1782 - Unit 3 - This med;fication replaced the electro-mechanical operators on valves 2HP-409 and 2HP-41 NSM- ON 32460 - Unit 3 - This modification involved a change to the RC Makeup Pump to increase the capacity of the pum At the conclusion of this report period, the review of these modifications was still in progress. This review will be concluded during a subsequent reporting period.