:on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping| ML20140H112 |
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| Site: |
Point Beach  |
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| Issue date: |
05/05/1997 |
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| From: |
George Adams WISCONSIN ELECTRIC POWER CO. |
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| Shared Package |
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| ML20140H111 |
List: |
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| References |
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| LER-97-018, LER-97-18, NUDOCS 9705120341 |
| Download: ML20140H112 (6) |
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NRC FORM 3iis U.S. NUCLEAR REOULATORY COMMISSION APPROVED SY OM8 NO. 3150-0104 j
(445)
ExppgEs 04/30/gg ESTIMATED DURDEN PER RESPONSE TO COMPLY WITH 3
THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER)
REPORTED LESSONS LEARNED ARE WCORPORATED INTO THE LICENSING PROCESS AND FEO BACK TO INDUSTRY.
FORWARD CCMMENTS REGARDING BURDEN ESTIMATE (See reverse for required number of TO THE INFOHMATION AND RECORDS MANAGEMENT digits / characters for each block)
BRANCH (T-6 F33),
U.S.
NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555 0001. AND TO THE PAFTRWORK RCDUCTION PROXCT i
F ACILITY NAME (1)
DOCKET NUMBER (2)
PAGE 13) j Point Beach Nuclear Plant, Unit 1 05000266 1 OF 6 j
TITLE 14) l Potential Residual Heat Removal System Overpressure During Accidents EVENT DATE (5) l LER NUMBER 16)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
SEQUEN hAL
' REVISION FACILITY NAME DOCILET NUMBER l
MONm DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR PBNP Unit 2 05000301 i
,l l
FACILITY NAME DOCKET NUMBLR l 04 l 03 l 97 l 97 018 00 05 05 9'7 05000 I
OPERATING l THIS REPORT 88 $UBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR E: ICheck one or more) (11)
MOE,E 19)
N l 20 220iabi 20.2203(aH2)(v)
- 50. 73(aH2H,)
50.73(aH2Hvs)
POWER l
20.2203(a)(1) 20 2203(aH3Hi) 50.73(aH2)(ii) 50.73(aH2Hx)
LEVEL (10) 000 20,2203(aH2HI) 20.2203(aH3Hii) 50.73(aH2)(s) 73.71 20.2203(aH2Hii) 20.2203(aH4) 50.73(aH2Hiv)
OTHEA 20.2203(aH2)ls) 50.36(CHI)
X 50.73(aH2Hv) speed, m Absweet tweew I
20 2203(aH2)(iv) 50.36(cH2) 50.73(aH2Hvii) er in hnc Form 3esA LICENSEE CONTACT FOR THIS LER f12)
NAME TELEPHONE NUMBER (include Area Code)
Glenn D. Adams, Licensing Engineer (414) 221-4691 COMPLETE ONE LINE FOR FACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS TO NPRDS t
SUPPLEMFNTAL REPORT EXPECTED 1131 EXPECTED MONTH DAY YEAR l
Yt3 SUBMISSION i
lif yes. complete EXMCTED SUBMISSION ' ATE).
X NO DATE (15)
ABSTRACT (Umit to 1400 spaces. i.e., approximately 15 smgle-spaced typewntten lenes) [16)
On April 3, 1997, with Unit 1 in cold shutdown and Unit 2 in a defueled condition, licensee engineers discovered a potential for a section of the Residual Heat Removal (RHR) System inside containment to overpressurize during a design basis accident.
The piping section is isolated by normally-closed RHR inlet isolation valves (RH-700 and RH-701), and is normally water-filled, but is not provided with relief valve protection.
During a design basis accident which elevates containment temperature, the trapped fluid would be heated by the containment accident environment and could pressurize the isolated section.
If unmitigated, the overpressure condition could lead to pipe rupture or valve damage, which would affect the capability of the RHR System to achieve and maintain cold shutdown if required later in the accident.
This condition is a latent characteristic of the original RHR System design and is generic to both nuclear units.
Prior to the startup of a nuclear unit, appropriate overpressure protection will be provided to that unit.
4 9705120341 970505 PDR ADOCK 05000266 S
PDR
i l
U.S. NUCLEAR REGULATORY COMMIS$lON (4-ess l
LICENSEE EVENT REPORT (LER) l TEXT CONTINUATION F ACILITY NAME til DOCKET NUMBER (2)
LER NUMBER 16)
PAGE(3)
Point Beach Nuclear Plant, Unit 1 05000266 NU BER NU R
2 OF 6 97 018 00 l
TE%T Uf more space de requeed, use adhtmnel copses of NRC Form 366Al (17)
~
Event Description
At 0819 CST on April 3, 1997, with Unit 1 in cold shutdown and Unit 2 in a defueled condition, licensee engineers discovered a potential for a section of the Residual Heat Removal (RHR) System inside containment to overpressurize during a design basis accident.
The piping section is isolated by normally-closed RHR inlet isolation valves (RH-700 and RH-701), and is normally water-filled, but is not provided with relief valve protection.
During a design basis accident which elevates containment i
temperature, the trapped fluid would be heated by the containment accident environment and could pressurize the isolated section.
If unmitigated, the overpressure condition could lead to pipe rupture or valve damage, which would affect the capability of the RHR System to achieve and maintain cold shutdown if required later ira the accident sequence.
This condition is generic to both nuclear units.
1 The potential condition was discovered during an evaluation of Condition Report CR 97-0683, which described a recent plant operation that led to an i
unexpected alarm from the Low Temperature Overpressure Protection (LTOP) circuit.
The evaluation determined that a brief pressure surge occurred in the Reactor Coolant System (RCS) when RH-700 was opened for the initiation of RHR operation.
From this event it became evident that the RHR valves RH-700 and RH-701 were capable of trapping fluid in the isolated section.
The fluid in the isolated section could be pressurized from leakby from the RCS during power operation, or it could be pressurized when the containment ambient temperature increase during plant startup causes the isolated water to expand.
This latter type of overpressurization was described in NRC Generic Letter 96-06, " Assurance i
of Equipment Operability and Containment Integrity During Design Basis Accident Conditions".
An evaluation determined that the trapped fluid could heat up and pressurize the pipe beyond code allowable values.
The only accidents that may require the RHR System to operate in decay heat removal mode are the Steam Generator Tube Rupture (SGTR) and the Main Steam Line Break (MSLB) accidents.
Of these, only the MSLB accident (if 3
the break is inside containment) could raise the piping system temperature above normal ambient temperature.
Therefore, the safety significance of the MSLB (inside containment) accident was evaluated as the limiting condition, and is discussed below.
In addition to thermally-induced isolated overpressure of the isolated piping section, the post-accident effects of thermal expansion were also reviewed with respect to NRC Generic Letter 95-07, " Pressure Locking and Thermal Binding of Safety-Related Power-Opereced Gate Valves".
The failure of these RHR valves to open due to pressure locking could also have affected the capability to initiate RHR for a MSLB inside containment.
In response to GL 95-07, plant modification requests were prepared to remedy the potential for pressure locking and thermal binding.
These modifications were originally scheduled for completion during the.
i 4U.S. NUCLEAR REOULATORY COMMISSION
- 4.ssi LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER is)
PAGE (3)
Point Beach Nuclear Plant, Unit 1 05000266 NU BR NU R
3 OF 6 97 018 00 TEXT Ut more space la requeed, use additional copus of NRC form 366N l11) next scheduled refueling outages for Unit 1 (U1R24) and Unit 2 (U2R23).
The IEEE Standard 803A-1983 component identifiers for this report are:
Relief Valve (RV)
Valve (v) i Component and System Description:
k The following discussion is generic to either nuclear unit.
The RHR System is an open-loop cooling system that draws reactor coolant from the hot leg of one reactor coolant loop and, after removing heat, returns the coolant to the cold leg of the opposite reactor coolant loop.
J, There is a single inlet line from the RCS and one return line, which l
indicates that there was no original design provision to meet the single failure criterion of PBNP General Design Criterion (GDC) # 41.
This decay heat removal loop of the RHR System was not originally considered an i
accident mitigating function because PBNP was generally considered a hot shutdown plant with respect to safe shutdown following accidents.
During a normal plant shutdown, the RHR System removes core decay heat and sensible heat after the secondary system has reduced reactor coolant system (RCS) conditions to approximately 350*F and 425 psig.
To initiate RHR operation, the inlet. isolation valves RH-700 and RH-701 must be opened to provide a flowpath from the RCS to the RHR pumps and heat exchangers.
RH-700 and RH-701 are located in series, inside containment.
After i
passing through the RHR heat exchangers, the coolant is returned to the RCS through return isolation valve RH-720 and a check valve.
I-RH-700 and RH-701 are motor-operated gate valves.
During power operation, RH-700 and RH-701 are closed and electrical power is removed.
When the RHR System is secured during a plant startup, the fluid in the isolated section could cool from 350 degrees F due to ambient heat losses.
j As described in PBNP FSAR Chapter 14, the RHR system is also required to operate during a Main Steam Line Break (MSLB) accident and a Steam i
I Generator Tube Rupture (SGTR) accident.
To limit the offsite dose of the limiting MSLB (break outside containment), the FSAR analysis takes credit for cessation of steam release and the initiation of RHR within six (6) hours of the postulated accident.
Similarly, the SGTR analysis in the PBNP FSAR also takes credit for the initiation of RHR within six (6) hours of the postulated accident.
A rupture of the piping between RH-700 and RH-701 would make the RHR system inoperable for use.
This condition was discovered during evaluation of CR 97-0683 where it is believed that pressure buildup between 1RH-700 and 1RH-701 was released when 1RH-700 was opened and caused a Low Temperature Overpressure Protection (LTOP) alarm actuation.
- - gU.S. NUCLE AR REOULATORY COMM18840N 14 m LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION F ACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER 16' PAGE (3)
YEAR SEQUENTIAL REVISION Point Beach Nuclear Plant, Unit 1 05000266 NUMMR NUMER 4OF6 97
- - 018 00 TEXT Uf more wace os requwed, use additionalcopies of NRC form 366Al l17)
Cause
Original design did not provide overpressure protection for the isolated piping section between RH-700 and RH-701 to accommodate the thermally-induced overpressurization that may occur during a design basis accident.
Therefore, the original design did not provide ample assurance that the RHR piping inside containment would be available for all design basis events.
I
Corrective Actions
1.
An evaluation was performed to determine the potential stresses on the isolated piping section and determine Unit 1 and Unit 2 operability at those stresses.
The predicted stresses exceeded the code allowable values.
2.
Prior to the startup of Unit 2 from the current refueling outage (U2R22), the potential for thermally-induced overpressure in the isolated RHR piping section will be remedied.
A solution under development is a plant modification (MR 95-041) to add bonnet vents to valves 2RH-700 and 2RH-701.
This modification would vent each bonnet to the upstream side of the valve.
The bonnet vent on valve 2RH-700 would also provide an overpressure relief path from the isolated section of RHR to the RCS.
This modification would require the reactor unit to be defueled with reduced coolant inventory.
This modification was initiated pursuant to NRC Generic Letter 95-07.
1 3.
Prior to the startup of Unit 1 from the current shutdown, the potential for thermally-induced overpressure in the isolated RHR piping section will be remedied.
Alternatives are presently being studied and include the installation of a relief valve on the existing vent and drain connections in the isolated RHR section.
Installation of the bonnet vents to 1RH-700 and 1RH-701 is not feasible during the current outage because defueling is not feasible.
- 4. During Unit 1 refueling outage U1R24, a plant modification (MR 95-042) is being considered to add bonnet vents to valves 1RH-700 and 1RH-701.
This modification may serve as an alternative means to provide the necessary overpressure protection for the isolated section of RUR piping.
This modification was initiated pursuant to GL 95-07.
5.
A review will be conducted to identify any other potentially isolated sections inside containment that may affect the operability of safety-related equipment that is important to accident mitigation.
NRC f ORM 366A (4 95)
m_._
.m..
1
- - e gU.S. NUCLEAR REOULATORY COMM6SSION (4 96)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION 1
FACftlTV NAME IU DOCKET NUMBER (2)
LER NUMBER (6 i
PAGE (3)
Point Beach Nuclear Plant, Unit 1 05000266 NU R
NU R
5 OF 6 97 018 00 TEXT lit more space le requeed, usa addihonal copses ofIVRC Form 366A) (17)
Reportability
A 4-hour prompt notification per 10 CFR 50.72 (b) (2) (1) was reported to the NRC duty officer at 1210 CST on April 3, 1997.
This licensee event report is being submitted in accordance with the requirements of 10 CFR 50.73 (a) (2) (v) (D), "Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident."
}
Safety Assessment
1 An evaluation has shown that an increase in containment ambient temperature from shutdown temperature to the peak accident temperature could cause the water in the isolated section of piping between RH-700 and j
RH-701 to expand and cause a pressure that results in pipe stresses
- 4 exceeding code allowable values.
Of the two events that may require RHR operation post-accident, only the MSLB event (inside containment) would cause this thermal overpressure condition.
The offsite dose consequences of this event would be small since there is no fuel failure from the event and any radionuclides released to the secondary would be retained in the l
containment.
The FSAR analysis of the MSLB accident considers the break
)
outside containment to be most radiologically limiting.
The initiation of I
RHR operation may have been delayed indefinitely by the rupture of the isolated section (or by the pressure-locking of the isolation valves).
In that case, core heat could have been removed by continued operation of the intact steam generator.
4 j
If the thermally-induced overpressure caused by a MSLB-inside-containment led to a rupture of the isolated piping section, it would not have led to a loss of coolant accident, because, by definition, isolation valve RH-700 would have to have been shut.
Inadvertent opening of RH-700 in this condition is precluded by the normal isolation of power from the MOV.
Therefore, it is not credible to postulate that the potential overpressure condition could have led to a MSLB and LOCA; an event for which the plant was not designed.
I There would be no effect of this condition on the steam generator tube
'l rupture (SGTR) accident because the SGTR accident does not cause the containment temperature increase that drives the thermally-induced overpressure condition.
Similar Occurrences:
Latent design flaws in the original design that affected the capability of safety-related equipment were reported in the following LERs:
1 LEB Q.escription 266/97-006-00 Potential Refueling Cavity Drain Failure Could Affect>
e NRC FOrtM 366A 4
U.S. NUCLEAR REOULATORY COMMISSION
{4 951 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION F AC8tlTV NAMt i O DOCKET NUMBER (2)
LER NUMBER (6)
PAOE (3)
YEAR SEQUENTIAL REVISION Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 6 OF 6 97 018 00 TEXT lit more space is requeed, use addormal copies of NHC Form 366A) l1 T)
Accident Mitigation 266/97-002-00 Potential To Overpressurize Piping Between Containment Isolation Valves During A Design Basis Accident 266/97-001-00 Safety Injection Delay Times Exceed Design Basis Values 266/96-005-00 Potential Service Water Flashing in Containment Fan Coolers l
I I
k l
a NHC FORM 366A (4 95)
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| 05000266/LER-1997-001, :on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation |
- on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-001, Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | | | 05000301/LER-1997-001-01, :on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment |
- on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000266/LER-1997-002, :on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed |
- on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-002-01, :on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping |
- on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-003, :on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results |
- on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results
| 10 CFR 50.73(a)(2)(1) | | 05000301/LER-1997-004-01, :on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable |
- on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-004, :on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers |
- on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-005-01, :on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump |
- on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-005, :on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed |
- on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-006, :on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake |
- on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-007, :on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes |
- on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-008, :on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage |
- on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-009, :on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised |
- on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-010, :on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed |
- on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-011, :on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested |
- on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-012, :on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results |
- on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-013, :on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved |
- on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-013-01, Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-014, :on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves |
- on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000266/LER-1997-015, :on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced |
- on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-016, :on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests |
- on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-017, :on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised |
- on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-018, :on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping |
- on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-019, :on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use |
- on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-020-01, Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-021, :on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a |
- on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-022, :on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition |
- on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition
| 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-023, :on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed |
- on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-024, :on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits |
- on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits
| | | 05000266/LER-1997-025, :on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised |
- on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-026, :on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp |
- on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-027, :on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material |
- on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material
| | | 05000266/LER-1997-031, :on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design |
- on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-032, :on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches |
- on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-034, :on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked |
- on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000266/LER-1997-035, :on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate |
- on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000266/LER-1997-036, :on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure |
- on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure
| | | 05000266/LER-1997-037, :on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing |
- on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing
| | | 05000266/LER-1997-038, :on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service |
- on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039-01, :on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored |
- on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039, Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-040-01, Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-041, :on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables |
- on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables
| | | 05000266/LER-1997-042, :on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear |
- on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-043-01, Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000266/LER-1997-044, :on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures |
- on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures
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