:on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten| ML20140C989 |
| Person / Time |
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| Site: |
Quad Cities  |
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| Issue date: |
04/15/1997 |
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| From: |
Peterson C COMMONWEALTH EDISON CO. |
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| To: |
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| Shared Package |
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| ML20140C985 |
List: |
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| References |
|---|
| LER-97-003-04, LER-97-3-4, NUDOCS 9704220051 |
| Download: ML20140C989 (4) |
|
text
o LICENSEE EVENT REFORT (LER)
Form Rev. 2.0 Fadity N:me (1)
Docket Number (2)
Page (3)
Quad Citi:s' Unit Tw'o 0l5l0l0l0l2l6l5 1 l of l 0 l 4 Title t4) 2 B Core Spray Roorn Cooler Fouled Due To Hydrolyzing Debris Ev:nt Date (5)
LLR Number (6)
Report Date (7)
Other Facihties involved (8)
Month Day Year Year Sequential Revision Month Day Year Facibry Docket Numberts) 4 Number Number Names 0l5l0l0l0l l
l 0l3 2l1 9l7 9l7 0l0l3 0l0 0l4 1l5 9l7 0l5l0l0l0l l
l OPERATING THis REPORT is SUBMrITED PURSUANT TO THE REQUIREMENTS OF 10CFR MODE (9)
(Check one or more of the following) (11) 4 20.402(b) 20.405tc) 50.73(a)(2)(iv) 73.7)(b)
POWER 20.405(a)(1)(i) 50.36(c)(1)
- - 50.73(a)G)(v) 73.71(c)
LEVEL
- - 20.405(a)(1)(ii) 50.36(c)G) 50.73(a)C)(vii)
Other (Specify (10) l l
0
- - 20.405(a)(1)(iii) 50.73(a)G)0) 50.73(a)C)(viii)(A) m Abstract 20.405(a)(1)0v) x 50.73(a)G)0i) 50.73(a)C)(viii)(B) below and in 20.405(a)(1)(v) 50.73(a)G)0ii) 50.73(a)G)(x)
Text)
LICENSEE CONTACT FUR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Ch:.rles Peterson, Regv!atory Affairs Manager, ext. 3609 3
0l9 6l5l4l-l2l2l4l1 COMPLLTE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPON ENT MANUFACIURER REPORTABLE
CAUSE
SYSTEM (x)MPONEt4T MANUF#CrV RER REPORTABLE
'!D NPRDS TO NPRDS I
I I
I I
I I
I I
I I
I I
I I
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I l
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I SUP 'LEMENTAL RDORT EXPEL.it.u tl4)
Expectoi!
Mumb Day Year Subminsk>n lYES Of yes. canplete EXPECTED SUBMIS$10N DATE)
~k"]NO Date (15) l l
l ABSTRACr (lamit to 1400 spaces. i.e., appronunniely firteen sinsk space typewnuen imes) (16)
ABSTRACT:
On 032197, significant fouling was discovered in the 2B Core Spray Room Cooler (CSRC) during the a pre-cleaning inspection. This condition may have existed from June 1996.
During this time period the 1/2 Emergency Diesel Generator (EDG) had been made inoperable for planned maintenance under a 7 day' Limiting Condition for Operation (LCO). Although the normal power supply for the 2A CS pump was available, the 1/2 EDG which is the emergency power supply was unavailable and the CS Technical Specification requirement was not met.
Assuming a design basis accident both CS pumps were inoperable unknowingly for a period of approximately 6 days.
The room cooler was declared inoperable and at 1952 hours0.0226 days <br />0.542 hours <br />0.00323 weeks <br />7.42736e-4 months <br /> a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> ENS phone call was made.
The apparent cause of the event was a plugged cooler caused by debris stirred up by hydrolyzing performed during Q2R13 on the EDG Cooling Water System. A contributing cause of the event was the lack of proper trending of the differential pressure (dP) data taken on the Emergency Core Cooling System (ECCS) Room Coolers.
Corrective actions completed include cleaning of the 2B CSRC and the other Unit 2 ECCS Room Coolers.
Unit 1 Room Coolers were cleaned less than a year ago. A new procedure will address future trending and analysis of room cooler dP and flow data. The risk to the health and safety of the public is reduced with the use of Station Blackout Power.
LER265\\97\\003.MTF 9704220051 970415 PDR ADOCK 05000265 S
PDR
~
e 7j LICENSEE EVEt(T REPORT (LER) TEXT CONTINUATION Form Rav. 2.0 I'ACILrrY N AME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
'PAGE (3)
Year Sequential Revimon Number Number l Quad CitiIs Unit Two 0l5l0l0l0l2 6l5 9l7 ol0 2 lOFl 0 l 4 0l0l3 i
TEXT Energy industry Idera26 cation System (E!!$) codes are identi6ed in the text as L(X)
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power.
EVENT IDENTIFICATION:
28 Core Spray Room Cooler Fouled due to Hydrolyzing Debris.
A.
CONDITIONS PRIOR TO EVENT
Unit: Two Event Date: March 21, 1997 Event Time:
1620 Reactor Mode:
4 Mode Name:
COLD SHUTDOWN Power Level:
0
}
This report was initiated by Licensee Event Report 265\\97-003.
Cold Shutdown (4) - Mode switch in Shutdown position with average reactor coolant temperature 5212 degrees F.
B.
EVENT DESCRIPTION-On 032197, System Engineering performed a pre-cleaning inspection on the 2B Core Spray (CS)[BM) Room Cooler (CSRC)[CLR). During that inspection significant fouling of the first (lower elevation) pass of the 8-pass heat exchanger was noted.
10 of 18 tubes were completely plugged with corrosion products, with 6 additional tubes being significantly but not completely plugged in this pass.
With this many tubes plugged, the 2B CSRC was declared inoperable.
l Historical differential pressure (dP) trending data reveals that this condition of fouling may have existed from June 1996. Differential Pressure on the 2B CSRC exceeded the set high dP limit in June 1996 and then returned to normal levels the following month.
During this time period, the 1/2 Emergency Diesel Generator
~
(EDG)[EK] had been made inoperable for planned maintenance under a 7 day Limiting Condition for Operation (LCO). Although the normal power supply for the 2A CS pump i
4 was available, the 1/2 EDG which is the emergency power supply was unavailable and the CS Technical Specification requirement was not met. Assuming a design basis accident both CS pumps were inoperable unknowingly for a period of approximately 6 days.
On 032197 at 1952 hours0.0226 days <br />0.542 hours <br />0.00323 weeks <br />7.42736e-4 months <br /> a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> ENS phone call was made.
i The 1/2 EDG was also inoperable in January 1997 for 1 day.
System Engineering instructed maintenance to clean the fouled cooler under existing NWR 960039336-01.
i The Unit 1 Emergency Core Cooling System (ECCS) Room Cooler dPs were also reviewed in reference to this event.
There is no indication that any of the Unit 1 ECCS Room Coolers are experiencing the same type of fouling.
l trausteme3.wrr
2 LICENSEE EVENT REPORT (LER) TEXT COffrINUATION Form Rev. 2.0
@CILfrY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
Year Sequential Revision Number Number Quad Cities Unit Two 0l5l0l0l0l2l6l5 9l7 0l0 3 lOFl 0 l 4 0l0l3 TEXT Energy industry identification System (E!!S) codes are identified te the text as lXX)
C.
APPARENT CAUSE OF EVENT:
The root cause of this event was inadequate flushing of debris following the hjdrolyzing during Q2R13. The fouling of the 2B CSRC was caused by debris loosened by hydrolyzing performed on the Unit 2 EDG Cooling Water [LB] piping during Q2R13 refuel outage.
This hydrolyzing was required due to the plugging experienced in the system. During that time, pipe corrosion products, clam shells, sticks and debris were dislodged by the hydrolyzing, but were not flushed from the system.
During Q2R13 all the ECCS Room Coolers had to be cleaned and inspacted twice because of the amount of debris found from the hydrolyzing. To assure that debris flushed from the system during Q2R13 was removed, the EDG Cooling Water System was run at full flow for several days before the second set.of cleanings were performed on the ECCS Room Coolers.
A contributing cause to this event was the lack of proper trending and analysis of the dP data, i.e. a cognitive personnel error, throughout the cycle.
In October 1996, during an NRC inspection it was discovered that trending of the Room Cooler dP was not performed for about a year.
During this period the first adverse trend on the 2B CSRC appeared.
If trending had been performed properly then a PIF or a ultrasonic flow reading would have followed up the suspect dP reading.
In October 1996, a review of the previous dP data was performed but at that time the high dP in l
June 1996 was not thought to be significant.
Ihe dP was only 0.8 psi above the high dP limit and it returned to normal the next month.
D.
SAFETY ANALYSIS OF EVENT:
)
Previous calculation on the ECCS Room Coolers have shown that the 2B CSRC can meet its design cooling function with a flow as low as 30 gallons per minute at 95 degree Fahrenheit (F) river water temperature.
Direct correlation from dP to flow does not exist due to the fact that fouling results in a variable orifice. Therefore, it is impossible to know what the actual flow was through the cooler at the time of the adverse fouling.
With both loops of Core Spray inoperable, Low Pressure Cooling Injection (LPCI) mode of Residual Heat Removal (RHR) system would be the only source of water into the core. Calculations show that the CS Room temperature without any cooler will rise continually.
The equipment qualificathn (EQ) temperature of 185 degrees F will be reached in approximately 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br />. Therefore, we can assume that the B CS loop would operate for the first day.
Station Blackout (SBO) Diesels would have been available to supply power to the 2A CS loop before the EQ temperature was reached in the 2B Core Spray Room. Therefore, the risk to on-site personnel and to the health and safety of the public is minimized.
ixaustmoo3.wer
i LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rce. 2.0 IRCILTTY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
Year Sequential Revision Number Number Quad Cities Unit Two 0l5l0 0l0l2 6l5 9l7 0l0l3 0l0 4 lOFl 0 l 4 TEXT Energy industry identification System (EHS) codes are identifim in the text as (XX) 1 E.
CORRECTIVE ACTIONS
Corrective Actions Completed The 2B CS Room Cooler was cleaned under NWR 960039336-01.
QCTP 1110-12, "ECCS Room Cooler Trending Program," has been recently written to give direction to the System Engineer on how to trend and analyze Room Cooler dP and flow data.
The 2A CS, Unit 2 High Pressure Coolant Injection (HPCI), 2A and 2B RHR Room Coolers have been cleaned and inspected during Q2R14.
Similar fouling of a lesser magnitude has been seen in some of these coolers.
Both 2A and 2B RHR Room Coolers had 10-11 tubes partially plugged and are allowed 32 tubes completely plugged. The 2A Core Spray had all tubes completely clear of debris. The HPCI Room Cooler has flow indication which assured us that it could perform its design function.
Corrective Actions to be Completed A predefine (electronic reminder) is being set up in Electronic Work Control System (EWCS) to track completion of QCTP 1110-12. (NTS 254-201-96-284901)
Modification Design Change Package (DCP) #9500060 is being installed during Q2R14 to add flow indicators to the RHR and CSRCs. These flow indicators will assist engineering to ensure that these coolers are able to perform their design function.
(NTS # 265-180-97-00301; Mod Design Engineering.)
Modification DCP 95000L is also planned to be installed on Unit 1 during Q1R15.
(NTS # 265-180-97-00302; Mod Design Engineering)
F.
PREVIOUS EVENTS:
A search was performed for a 3 year history of Level III investigations with the keyword of clogged / plugged. The following events were found:
LER 2-92-007 2A and 2B RHR Room Coolers plugged due to. insufficient cleaning.
I LER 1-94-007 HPCI Restricting Orifice Found 95% Plugged with Weld Slag.
LER 1-94-011 During Scram Timing, Control Rod Drive Failed to Scram due to Pipe Plug Inserted into Solenoid Valve PIF 96-3272 Toxic Gas Analy2.er Sample Flow Low Because of Worn Out Pump or Line Restrictions.
G.
COMPONENT FAILURE DATA
NONE 1XR265\\97WO3.WFF
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| | | Reporting criterion |
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| 05000254/LER-1997-001, :on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed |
- on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed
| 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-001-01, :on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personne |
- on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personnel
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000265/LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-001-07, :on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine |
- on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-002-02, :on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124 |
- on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124
| | | 05000254/LER-1997-002, Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000265/LER-1997-002-05, :on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897 |
- on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897
| | | 05000265/LER-1997-002-01, :on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass |
- on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass
| | | 05000265/LER-1997-002, Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000254/LER-1997-003, Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000265/LER-1997-003-04, :on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten |
- on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-003-05, :on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve |
- on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve
| | | 05000265/LER-1997-003-01, Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-004, Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | 10 CFR 50.73(a)(2) | | 05000265/LER-1997-004-06, :on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed |
- on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-004-03, :on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced |
- on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-005-03, :on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated |
- on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-005, Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000265/LER-1997-005-01, Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-005-02, :on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts |
- on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000265/LER-1997-006, Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000265/LER-1997-006-01, :on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1 |
- on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1
| | | 05000254/LER-1997-006-03, :on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker |
- on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker
| | | 05000254/LER-1997-006, Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-006-06, :on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed |
- on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed
| | | 05000254/LER-1997-007-03, :on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan |
- on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-008, Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-008-01, :on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged |
- on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-008, Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-008-05, :on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable |
- on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-009, Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-009-03, :on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled |
- on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled
| | | 05000265/LER-1997-009-05, :on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas |
- on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(s)(2)(v) | | 05000254/LER-1997-010-02, :on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily |
- on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily
| | | 05000265/LER-1997-010-05, :on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled |
- on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled
| | | 05000265/LER-1997-010, Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-010, Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-011-01, :on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause |
- on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause
| | | 05000254/LER-1997-011, Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-011-05, :on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals |
- on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000265/LER-1997-012-06, :on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted |
- on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted
| | | 05000254/LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000254/LER-1997-013-01, :on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch |
- on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch
| | | 05000254/LER-1997-014, Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-014-01, :on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure |
- on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure
| | | 05000265/LER-1997-015-05, :on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time |
- on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time
| | | 05000254/LER-1997-015, Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | | | 05000254/LER-1997-015-02, :on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test |
- on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test
| | | 05000254/LER-1997-016-01, :on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1 |
- on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1
| | | 05000254/LER-1997-016, Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | 10 CFR 50.73(a)(2)(1) |
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