:on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124| ML20138P883 |
| Person / Time |
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| Site: |
Quad Cities  |
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| Issue date: |
02/24/1997 |
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| From: |
Peterson C COMMONWEALTH EDISON CO. |
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| To: |
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| Shared Package |
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| ML20138P874 |
List: |
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| References |
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| LER-97-002-02, LER-97-2-2, NUDOCS 9703050469 |
| Download: ML20138P883 (5) |
|
text
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LICENSEE EVENT REFORT (LER)
. s Fecahty N,me (1)
Form Rsv. 2.0 Docket Nurnber G)
Page (3)
Quad Cities Unit One/Two 0l5lol0l0l2l5l4 1 l of l 0 l 5 Title (4)
Engineering Calculanona performed in response to NRC Generic Letter 96-06 inacated that several isolable piping sections on each u UFS AR Allosables following a Loss of Coolant Accident due to inadequate original system design.
Event Date (5)
LER Number (6)
Report Date (7) l Other facilities involved (8)
Moach Day Year Year Sequential Revision Month Day Year Facihty Docks: Number (s)
Number Number Names QC Unit 2 0l5l0l0l0l2l6l5 ol1 2l7 9l7 9l7 0lO]2 ojo 0l2 2l4 9l7 ol5lojoloj l
l OPLRATING THIS REPORT IS SUBMirrED PURSUANT TO THE REQUIREhENIS OF 10CFR MODE (9)
(Check o se or more of the following) (II) 1 E 32(b) 20.405(c) 50.73(a)G)(iv) 73.71(b)
POWER
- 20. A)5(a)(1)6)
- - 50.36(c)(1) 50.73(a)C)(v) 73.71(c)
LEVEL 20.405(a)(1)6i) 50.36(c)C) 50.73(a)G)(vii)
Other (Specify (10) 1 l0l 0
20.405(a)(1)(iii)
- - 50.73(a>G)(i) 50.73(a)G)(viii)(A) in Abstract
~
20.405(a)(1)(iv)
'j("50.73(a)C)(ii) 50.73(a)G)(viii)(B) below and in l
20.405(a)(1)(v) 50.73(a)G)(iii) 50.73(a)G)(x)
Text)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Ch.rles Peterson, Regulatory Affairs Manager, ext. 3609 3
0l9 6l5l4l-l2l2l4l1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCF! RED IN THIS REPORT (13)
CAUSE
SYSTud CDMPONENT MANUFACRJRER REPORTABl.E
CAUSE
SYSTEM COMPONENT MANUFACRJRER REK)RTAB11 10 NPRD5 3
10 NPRDS I
I I
I I
l l
I I
I I
I I
I I
I I
I l
I l
I I
I I
I SUP *1 E'WNTAL REPORT EXPECTED (14)
Expeced Month Day Year 4
Submmeian yYEs Of yes, complete EXPECTED SUBMISSION DATE) 70 Dete (15) ol5 3l1 9l7 ABSTRACT (lama ao 1400 ;+=e. i.e., approsametely ftheen segle-spea W n home) (16)
ABSTRACT:
On 012797, with both Units in Mode One at 100% power, it was determined that several isolable piping sections could experience stresses above Updated Final Safety Analysis Report Allowables due to Post-Loss of Coolant Accident thermal pressurization.
In response to NRC Generic Letter 96-06, several calculations were performed to evaluate piping and containment penetrations for thermal overpressurization caused by a Main Steam Line Break (MSLB)/ Loss of Coolant Accident (LOCA).
These calculations identified five penetrations (per Unit) that could experience overpressurization under accident conditions.
The affected piping systems include: Reactor Building Closed Cooling Water, Reactor Recirculation Sample lines, Residual Heat Removal, Reactor Water Clean-up, and Clean Demineralized Water.
The affected piping sections were determined to be operable, but degraded. The cause of the event was inadequate original design.
Based on the results of the operability assessment, there is minimal safety significance to the station or the health and safety of the public as a result of this event. The affected penetrations would maintain containment integrity following an accident.
In the event of an accident, any radiological release would remain within analyzed limits. The corrective actions taken to resolve this issue are being developed and will be provided in a supplemental report.
IEJt254t97\\002.WFF 9703050469 970224 PDR ADOCK 05000254 S
PDR
LICENSEE EVENT REPCOT (LER) TEXT CONTINUATION Form R:v. 2.0
~
FACILfrY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
Year Sequintki R m aion Number Nunser Qual cities Unit Ote 0l5l0l0l0l2l5l4 9l7 0l0l2 0l0 2 lOFl 0 l 5 TEXT Energy industry identification system (Ells) codes are identified in the text as (XXI
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power..
EVENT IDENTIFICATION: Engineering Calculations performed in response to NRC Generic Letter 96-06 indicated that several isolable piping sections on each unit may experience stresses above UFSAR Allowables following a Loss of Coolant Accident due to inadequate original systein design.
I A.
CONDITIONS PRIOR TO EVENT
Unit: One Event Date: 012797 Event Time: 2100 i
Reactor Mode:
1 Mode Name:
POWER OPERATION Power Level:
100%
Unit: Two Event Date: 012797 Event Time: 2100 Reactor Mode:
1 Mode Name:
POWER OPERATION Power Level:
100%
This report was initiated by Licensee Event Report 254\\97-002.
Power Operation (1) - Mode switch in the RUN position with average reactor coolant temperature at any temperature.
8.
DESCRIPTION OF EVENT
4 On 012797, with both Units in Mode One at 100% power, it was determined that several isolable piping sections on both units could experience stresses above Updated Final Safety Analysis Report (UFSAR) Allowables due to Post Loss of Coolant Accident (LOCA) thermal pressurization. The allowable piping stresses are described in UFSAR Section 3.9.
In response to NRC Generic Letter (GL) 96-06, " Assurance of Equipment Operability and Containment Integrity During Design - Basis Accident Conditions", piping systems that penetrate cont inment were evaluated to determine if they were susceptible to thermal overpressurization. This evaluation resulted in the development of four calculations.
Calculation QDC-1600-M-0299 determined the maximum temperature change in water trapped between two closed valves during accident conditions for a variety of containment penetration configurations.
Calculation QDC-1600-M-0297 developed a methodology to i
calculate an incremental pressure increase per degree Fahrenheit (F) as a function of pipe outside diameter to wall thickness ratio and final water temperature.
Pressure changes in the isolated pipe sections could then be predicted using the pipe material and size, the pressure increase per degree F, and the calculated temperature rise.
i Calculation QDC-1600-M-298 determined the maximum permissible piping pressures for design, upset, emergency, and faulted conditions to determine the pressure retaining capability of isolated pipe sections under thermal pressurization conditions.
Calculation QDC-1600-M-0296 reviewed containment penetrations and compared the predicted pressure increase with the maximum permissible piping pressures to determine if maximum permissible pressures were exceeded.
i IIR2s&7\\002,WPF
LICENSEE EVENT REPCOT (LER) TEXT CON'rINUATION Form Rev. 2.0 FACILfTY N AME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
Year Sequentd R2 vision Nurnber Number Quad Cities Unit One ol5lol0l0l2l5l4 9l7 olol2 olo 3lOFlol5 TEXT Energy industry identification System (Ells) codes are userdified in the text as {XX)
Five penetrations (per Unit) were determined to be susceptible to the overpressurization conditions discussed in GL 96-06. The penetration and associated descriptions are as follows:
Penetration X Reactor Building Closed Cooling Water (RBCCW) Return Piping from the Drywell Penetration X Reactor Recirculation [AD] System Sample Line Piping
- Penetration X Clean Demineralized Water [KC] Piping These penetrations would be heated during a LOCA or a Main Steamline(MSL) break inside containment.
Penetrations designated by an asterisk close automatically on various group isolation signals.
An operability assessment was completed 012797 to document the basis for continued operability of the affected penetrations and systems / components.
The basis for operability of these affected penetrations includes consideration of one or more of the following:
expansion of the trapped fluid in voided areas of the isolated piping section, leakage from one of the containment isolation valves (seat, packing, or body to bonnet flange), insulation of piping to delay the temperature increase, lifting of air operated valves due to the pressure increase, and plastic straining of the affected pipe to accommodate the pressure increase. The criteria provided in ASME Section III, Appendix F was utilized to evaluate the operability of the affected piping sections.
C.
APPARENT CAUSE OF EVENT:
The cause of this event is attributed to inadequate original design. The potential for thermal pressurization of isolated containment penetrations due to elevated post accident conditions was not adequately anticipated in the original penetration / piping design.
The root cause of the original design error is unknown.
D.
SAFETY ANALYSIS OF EVENT:
There is minimal safety significance to the station or the health and safety of the public as a result of this event.
The results of the operability assessment concluded that the affected penetrations were Operable, but degraded. The affected penetrations would maintain containment integrity following an ar.cident.
In the event of an accident, any radiological release would remain within analyzed limits.
Additionally, it should be noted that for three of the penetrations, it is unlikely that the conditions needed for a thermal overpressurization condition to develop would be present following an accident.
j IIR25A97\\M2.WPF l
LICENSEE EVEt(T REPC%T (LER) TEXT CONTINUATION Form R:v. 2.0 f ACILfrY N AME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE0)
Year Sequ:nual R; vision Number Number Quad Cities Unit One ol5l0l0l0l2l5l4 9l7 0lol2 0l0 4 lOFl 0 l 5 TEXT Energy industry idenafication system (Ells) codes are idenufied in the text as [XX) i l
The penetrations associated with RWCU(X-14) and the Reactor Recirculation System i
Sample Line(X-41) normally contain " hot" process flow and would not experience thermal heat-up during an accident.
These penetrations are only susceptible to thermal overpressurization if the lines are isolated during operation.
The valves associated with these penetrations are currently open.
The penetration associated with the RBCCW piping (X-24) is normally open, and must remain open during operation because it supplies cooling water to the Reactor Recirculation Pumps.
RBCCW is a closed loop system and does not interface with the Reactor Coolant Pressure Boundary (RCPB). This penetration is only susceptible to thermal overpressurization if the lines are water solid and isolated following an accident. The valves associated with this penetration do not have an automatic isolation signal and are procedurally isolated if a break in the RBCCW piping is detected. Therefore, in order for thermal overpressurization to occur, the LOCA event, a RBCCW system breach, and water solid conditions between the isolation valves must occur concurrently.
E.
CORRECTIVE ACTIONS
Corrective Actions Completed /In proaress:
1.
An Initial Operability Evaluation was completed on 012797 which concluded that the affected penetrations were operable and containment integrity was intact.
2.
On 013097, the Operability Evaluation was revised to address additional corrective actions that will be taken.
3.
During 1996, Quad Cities performed several reviews intended to assure conformance with the UFSAR.
A comprehensive UFSAR Compliance / Design Basis Review Initiative is under development.
Corrective Actions Scheduled:
1.
Alternative solutions to resolve the potential thermal overpressurization will be evaluated. The specific corrective actions and implementation schedule for each affected penetration will be provided to the NRC in an Update to the Quad Cities Generic Letter 96-06 response by 053197.[NTS 2541809700201; Engineering]
2.
Quad Cities will evaluate the acceptability of partially draining the piping associated with penetrations X-12 and X-20.
This action will be complete by 022897. [NTS 2541809700202; Engineering) 1 3.
Subject to the above approval (Item 2), the piping associated with penetrations 1
X-20, Clean Demineralized Water to the Drywell, will be partially drained.
1 Provisions will be made to ensure that this piping is drained prior to Unit start-up in the future.
This action will be complete by 032897.
[NTS2541809700203;0perations]
i IIR254\\97s002.MTF J
LICENSEE EVEffT REPCOT (LER) TEXT CONTINUATION Form Rsv. 2.0 FACILTTY NAME Og DOCKET NUMBER (2)
LER NUMBER to)
PAG E (3)
Year Sequ:nhal Rwision Number Number Qwd Cities Unit Ome ol5l0l0l0l2l5l4 9l7 0l0l2 ol0 5lOFl0l5 TEXT Energy Industry idenufication System (EUS) codes are idenufied in the text as (XXI 4.
Subject to the above approval (Item 2), the piping associated with penetrations X-12, RHR Shutdown Cooling Suction piping, will be partially drained.
i Provisions will be made to ensure that these actions remain in place until final actions to resolve this concern are implemented. Appropriate procedure changes will also be made to ensure the RHR Shutdown Cooling is filled and vented prior to operation. -This action will be completed during the next cold shutdown for Unit 1 and prior to startup from refueling outage, Q2R14 for Unit 2. [NTS 2541809700204; Engineering]
5.
The modification process will be evaluated to ensure that future modifications account for overpressurization concerns.[NTS 2541809700205; Engineering]
l 6.
A discussion covering the issues raised by NRC GL 96-06 will be included in the training program for Engineering personnel.[NTS 2541809700206; Engineering]
F.
PREVIOUS EVENTS:
A review of previous Licensee Event Reports (LER) at Quad Cities Station Units One and Two, since 010195 concerning primary containment issues or deficiencies related to plant design identified the following previous events:
LER Number Descriptio6 1-95-002 POTENTIAL PROBLEM WITH THE SIZING OF THE THERMAL OVERLOADS ON THE B0OSTER FANS FOR THE CONTROL R00M HVAC 1-95-003 TIP SYSTEM RESPONSE TO A PCIS SIGNAL l-95-007 RPS SCRAM DISCHARGE VOLUME LOGIC CIRCulT IS DESIGNED SUCH THAT A SINGLE COMP 0NENT FAILURE WOULD PREVENT A FULL SCRAM l-96-002 DRESDEN STATION NOTIFIED THE STATION THAT OUR CONTROL ROOM VENTILATION ISOLATION MAY BE DEFICIENT.
1-96-009 DEGRADED V0LTAGE CONCERNS DUE TO MCC 29-2 CABLE LENGTHS 1-96-011 NRC IN 92-18 DESCRIBES A CONDITION WHERE MOVS CAN BE DAMAGED DUE TO HOT SHORTS DUE TO FIRE l-96-015 PIPE WHIP RESTRAINT J1HP-3 1-96-016 REACTOR BUILDING BLOWOUT PANELS 1-96-020 CONTROL R00M B0OSTER FANS 1-96-022 B CONTROL ROOM HVAC REFRIGERATION UNIT HEATER l-96-025 ECCS SUCTION STRAINERS HEAD LOSS VALUE IS INCORRECT.
2-95-006 U-2 MCC 29-2 TRIPPED ON OVERLOAD.
G.
COMPONENT FAILURE DATA
There is no component failure associated with this event. There have been no penetration failures at Quad Cities Station attributed to thermal overpressurization.
LER254\\97\\002.WPF
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| | | Reporting criterion |
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| 05000254/LER-1997-001, :on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed |
- on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed
| 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-001-01, :on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personne |
- on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personnel
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000265/LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-001-07, :on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine |
- on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-002-02, :on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124 |
- on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124
| | | 05000254/LER-1997-002, Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000265/LER-1997-002-05, :on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897 |
- on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897
| | | 05000265/LER-1997-002-01, :on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass |
- on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass
| | | 05000265/LER-1997-002, Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000254/LER-1997-003, Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000265/LER-1997-003-04, :on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten |
- on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-003-05, :on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve |
- on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve
| | | 05000265/LER-1997-003-01, Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-004, Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | 10 CFR 50.73(a)(2) | | 05000265/LER-1997-004-06, :on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed |
- on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-004-03, :on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced |
- on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-005-03, :on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated |
- on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-005, Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000265/LER-1997-005-01, Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-005-02, :on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts |
- on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000265/LER-1997-006, Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000265/LER-1997-006-01, :on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1 |
- on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1
| | | 05000254/LER-1997-006-03, :on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker |
- on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker
| | | 05000254/LER-1997-006, Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-006-06, :on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed |
- on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed
| | | 05000254/LER-1997-007-03, :on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan |
- on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-008, Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-008-01, :on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged |
- on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-008, Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-008-05, :on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable |
- on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-009, Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-009-03, :on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled |
- on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled
| | | 05000265/LER-1997-009-05, :on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas |
- on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(s)(2)(v) | | 05000254/LER-1997-010-02, :on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily |
- on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily
| | | 05000265/LER-1997-010-05, :on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled |
- on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled
| | | 05000265/LER-1997-010, Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-010, Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-011-01, :on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause |
- on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause
| | | 05000254/LER-1997-011, Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-011-05, :on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals |
- on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000265/LER-1997-012-06, :on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted |
- on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted
| | | 05000254/LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000254/LER-1997-013-01, :on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch |
- on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch
| | | 05000254/LER-1997-014, Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-014-01, :on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure |
- on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure
| | | 05000265/LER-1997-015-05, :on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time |
- on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time
| | | 05000254/LER-1997-015, Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | | | 05000254/LER-1997-015-02, :on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test |
- on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test
| | | 05000254/LER-1997-016-01, :on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1 |
- on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1
| | | 05000254/LER-1997-016, Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | 10 CFR 50.73(a)(2)(1) |
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