ML20107D174
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.To:
James P, O'Reilly Directorate of Regulatory Operations Region I 631 Park Avenue King of Prussia, Pennsylvania 19406 From:
Jersey Central Power 4 Light Company Oyster Creek Nuclear Generating Station Docket #50-219 Forked River, New Jersey 08731
Subject:
Abnormal Occurrence Report No. 50-219/74/ 3 The following is a preliminary report being submitted in compliance with the Technical' Spe'cifications parap.r5ph6,6,2, j
i Preliminary Approval:
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gf4gd 1/ 14 / 74 g/ J. T. Carroll, Jr.
Date ec: Mr. A. Cionhusuo N
9604190157 960213 PDR FOIA DE).OK95-258 PDR
kPPARENTCAUSE Osi n ere>>urc OP OCQ)RRENCE; Manufccture.
Unusual Service Condition i
Installation / '
Inc. Environmer*ai Construc' tion Component Failure operator Other (Specify)
The cause of snubber inoperabli'ity was due to a f oss of hydraulic fluid. 'the cause of fluid loss is presently
,un' der investigation.
ANA1,Y$l$ OF
'The safety sinnificance of this occurrence was a partial OCCURRENCE:
loss of the scismic restraining ability for the two affected systems'.
liad the plant suffered a design bases earthquake, the probability that these two systems would have suffered structural damage was increased, W RRECTIVE The failed units were replaced with units that wore rebuilt ACTION:
with ethylene propylene (Parker Grade E652-90) seal naterial.
FAILURE DATA:
Manufacturert Bery.cn Paterson Type: HSSA-10 Serial Nos.: 487517 487487 477376 470924 469D62
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Prepared by:, /f[ AL.
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Date:
1/14))4_
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Initial Telephone Date of.
Deport Date:
!i1/14/74 Occurrence:
1/13/74 Initial Written Time of
' ' Report ' Date:
1/14/74 Occurrence:
1700___
0YSTER CREEK NUCLEAR ' GENERATING STATION
' FORKED RIVER, NEW JERSEY,08751 q
Abnormal Occurrence Report No. 50-219/74/ 3 IDENTIPiCATION Vloistion of the Technical Specifications, paragraph ' N/A OF OCCURRENCE:
Failure, of flydtnulic Shock and Sway Arrestors on one Core Spray System and two isolation Condenser systems.
1his event is cohs'idered to be an abnormal occurrence as de-fined in the Technical Specifications, paragraph _1.15D CON 0tT!ONS PRIOR TO OCCURRENCE:
Steady State Power Routine Shtitdown
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Hot Standby Operation A
Cold Shutdown Load Changes During
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Refueling! Shutdown Routine Power Operation j
Routine Startup Other (Specify) operation l
The plant was shutdown with reactor-coolant at '.212 F.
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J DESCRIPTI(N During the required inspection of.the Bergen Paterson RSSA-10 OF OCCURRENCE:
units in the primary containment, fivo units were discovered to be dcyoid of fluid. They were located v. follows:
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- 1 3. "A" 1.$olntion condenser 1
"B" Isolation Condensor 1 - Core Spray System #2
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