ML20107D055

From kanterella
Jump to navigation Jump to search
Discusses RO Special Insp Rept 50-219/74-01 Concerning Rept of Unidentified Leakage Referenced by Telcon from State of Nj Representative.Recommends That Rept Be Forwarded to Hq for Action & Licensee Notified Re Timely Issuance of TS
ML20107D055
Person / Time
Site: Oyster Creek
Issue date: 02/07/1974
From: Greenman E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Caphton D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18039A986 List: ... further results
References
FOIA-95-258 NUDOCS 9604180117
Download: ML20107D055 (2)


See also: IR 05000219/1974001

Text

.

-.

. . -

..

_

.

- - ~ . . . . - - - .

. . -

'

, .

f,,a -

'

,

.g

^

Af ?

7 lT

d

'

, . ,

1

1

1

,

4

1

i

'.!.

'

i'

'

.

$..M .

.

i.g

i

.-

  • -

D. L. Caphton,. Senior. Reactor Inspector, Directorate of Regulatory

Operations, Region I_

.;

.,

.;

I

l

JERSEY CENTRAL. POWER AND LIGHT CCEPANY

0YSTER CREEK

RO SPECIAL' INSPECTION REPORT 50-219/74-01

,

,

This ' inspection was conducted to examine details concerning a . report of

1

unidentified leakage. referenced to RO:I in a telephone conversation from

a. State of New. Jersey representative. The increased leakage rate..was

.

. . .

! # .Li

apparently utilized in part, by JCP&L to avert a state injunction which

I

would have barred a scheduled plant outage. The inspection further-

included observations of a fish kill (predominately menhaden) which

occurred'as had been predicted by the licensee.

A.

' Unidentified' Leakage'into'the:Drywell

i

Plant records reviewed indicated that T. S. limits (5 gpm) for

i

unidentified leakage were not exceeded. The' increased' leakage

rate was measured via the floor drain sump totalizing meter, and

,

was. attributed to a leaking Isolation Condenser drain valve.

-

,

'

B.

Fish Mortalities

J

The fish population congr.egated at the discharge structure prior

,

i

to the shutdown was sizeable, and the outage clearly precipitated

.

fish mortalities. First visual evidence appeared about one-one and

one half hours following the scheduled turbine trip. Approximately

one-two dozen " snapper blues" were observed along the canal shoreline.

Oq

,

Seven hours after the trip, increasing numbers of menhaden were

a

observed to be. dead and dying.

Sea gull activity also increased

'

markedly.

Local residents were active in " cleaning up" the area

and apparently use the fish for fertilizer and bait (chum) .

Cur-

rent estimates as obtained verbally from an RO consultant place,

total number of mortalities at about 20,000.

If this number is

reasonably accurate the magnitude of the kill was considerably

.less than s similar kill which occurred last winter.

C.

Staff Position

I

'

Section 5.5.2.4 (pp 5-28) . of the Draf t Environmental Statement by DL,

reiterates the staff: position that recurrent fish kills are an unac-

-

ceptable condition'of piant operation. The statement further notes

-

s

'

\\

9604180117 960213

,

PDR

FOIA

DEKOK95-258

PDR

so

,

\\

.

.

D. L. Caphton

-2-

that the applicant will be required to install appropriate controls'

)

&

and institute operating procedures that will minimize or eliminate

4,M

such fish kills following winter shutdowns. The staff position was

further provided to the State of New Jersey.

' -

D.

' Comments and' Action' Requested

In my view just predicting additional kills at Oyster Creek is

intolerable. Reactor shutdowns are going to occur. A year has

elapsed since the last major kill and the licensee has not imple-

mented a plan other than the running of one (1) dilution pump, to

minimize the differential temperature.

.It is recommended that this report be forwarded to Headquarters for

action and that Licensing be contacted with respect to the following:

1.

Timely issuance of Environmental Technical Specifications for

Oyster Creek in recognition of the prolonged delays and slippage

concerning the full term operating license.

2.

Establishment of a schedule coordinated with the licensee

concerning a JCP&L course of action designed to mitigate the

ecological consequences of winter shutdowns and to be imple-

mented by the fall of 1974.

g

I do not believe that Regulatory should be lef t in the middle of the

particular problem area at Oyster Creek. The staff position is clear

and Technical Specifications are needed, prior to winter of 74-75.

b

'

mv

l

Edward G. Greenman

Reactor Inspector

.

t

$