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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO) LICENSEE EVENT REPORT (SEE ALSO AORO)
MONTHYEARML20084P8241975-05-30030 May 1975 AO 50-249/75-28:on 750522,main Steam Line Area Temp Sensors 261-16B,261-17 A-D & 261-18D Found W/Setpoints Above Tech Spec Limit.Caused by Misapplied Switches.Switches Reset within Tech Spec Limit ML20084Q0341975-05-19019 May 1975 AO 50-249/75-26:on 780509,during Discharge test,24/48 Volt Dc Batteries Failed to Deliver Rated ampere-hour Capacity. Caused by Six Bad Cells in One Battery & Four Bad Cells in Other.Deteriorated Cells Will Be Replaced ML20084Q7331975-05-0606 May 1975 AO 50-249/75-24:on 750426,during Routine Calibr of HPCI Area Temp Sensors,Setpoints on 12 of 16 Temp Sensors Found Above Tech Spec Limit.Caused by Unsuitable Existing Temp Sensors for First Operation Surveillance Type Operation 1975-05-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station ML20217H7201997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20210V2401997-09-19019 September 1997 Rev 65g to Topical Rept CE-1-A, Comm Ed QA Manual ML20216J3781997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for DNPS ML20210H5511997-07-31031 July 1997 Monthly Operating Repts for July 1997 for DNPS IAW RG 1.16 & GL 97-02 1999-09-30
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. i M - Commonwealth Edison
// w 1 oaa r.rst bnat nera. cheaco. imncis , f,T V-
. 3
. hC Addtr'as',chy to: Post Olf:ce Box 767
?:/ Crocago, litinoi: 60690 BBS Ltr. #284-75 Dresden Nucicar Power Station. a R. R. #1 ,
I Morrio, Illinoin 60450 !
May 6, 1975 M41 h b
- /
.Mr. Jarr.es G. Koppler, Regional Director J~
Directorate'of Regulatory Operations-Region III U. S. Nuclear Regulatory Cornission ,
s 799 Roosevelt. Road y
. Glen Ellyn, 1111noia 60137 'Qf}W\\'
SUDJECT: REFORT OF l.E!OR'.'A OCCIT.BE!CE PER SETION 6.6. A OP ' DIE TFCINICl4 SPECI-'ICATIC::S
- HIGH P3ES5URE CCOLMP II'JECTION SYSTE1/JtEA TE:PF3/.TURE SUITCH S~r7. Por ? '!JCL'.TICII
References:
- 1) Regulatory Guide 1.16 Rev. 1 Appendix A
- 2) Notification of Region III of U. S. Nuclear Regulatory Cocmiccion
~~
Tclophone: R. Knop, 1.pril 28, 1975 at.1600 hourn T01 err.? J. Perpleri ^r'91 94, 1975 a.t 5646 b~~r Report Number: 50-249/1975-24
, Report Date: Fay 6, 1975-
\
Occurrence Date: April 26, 1975 Facility: Dresden Nuclear Pcwcr Station, Morris, Illinois IDEh'PIFICATION 0? CCCURR71:CE ..
_T_uelve of the hich crecsure coolar.t_injheystem (HFCI) arca temperature sencora 2370A-D, 2371A-D, 2372A-D, and 2373A-D were found with actpointa above the, 6200*P technical specification limit.
CONDITIONS PRIOR TO CCCURRD!CE Dresden Unit 3 was in the refuel modo with a refueling outage in progrecs.
DESCRIPTICM OF GCCURRE CE During the routine ocheduled calibration of the HPCI arca . temperature censors,
= the actpint;c. on twelve _of thc cixcaen te:perature censcrs were fcund to bc
.abovo the 200*P li.e.it. The reactor was in the reilici raode with the head rcmoved, .
therefore no im.cdiate corrective action uas necoscary. -
i
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B306130554 750506 . @/ '/^
sPDR ADDCK 05000249:
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J _-
- Mr. James G. Koppler - ,- ' '
hay 6,1975 DESIGNATION OF APF/REh'P CAUSE OF OCCITriRENCE (Design Error)
- The existing temperature sensors are not suited for a "first operation" surveillance type operation.
-ANALYSIS OF OCCURRCCE The -function .of the temperature censors is to isolate the HICI turbine steam supply in the event of a sto:m leak in the EPCI cubicle. The technical specifications require an isolation at or below 200*P. The "as found" sotpoints of the 16 switches involved would have provided an isolation at 202' F minimum and 249* P m: i.mun. The saturation temperature corresponding to.the mini.u:m design inlet pressure would be 360* P. It is therefore -
L Jconcluded that there would be sufficient differential temperature to '
activate the closure signal even with the inst"uments'out of tolerence.
In addition to the high temperature sensors, steam line break detection is also
.provided by differential pressure sensors. Those devices are checked monthly.
'It is thereforo concluded that no significant safety, hazard was created as a result of the high setpoint of the HPCI temperature sensors.
_ CORRECTIVE ACTION
'To prevent future occurrence, a plant rnodification (M12-3-74-143) will be made.
The modification vill-install a liquid filled tcmperature sensor which is better suited for trat trip operation than those presently installed.
FAILURE DATA Thesc' switches have been found with high notpoints many times and the j subsequent investigation has detemined that the existing switches are yd misapplied in"that an accurato first operation trip point cannot be
. consistently obtained.
The manufacturer of the_ switches (Pcnuall Inc) has investigated the problem Land has stated that the existing switches are not properly cuited uhon a Arctitrip setpoint is required. The switches involved Ere Ibnwal series .
1700 hermetically sealed thermomritch type units. ,
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v W YB. B. Stephenson.
, Superintendent ,
E .BDS: cmp '
' l Pilc/NRC, '
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