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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
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% EDISON ED: SON PLAZA 300MAOISON AVENUE r TOLEDO. DHlO 43652-o001 April 12, 1990 ,
KB90-0260 I Docket No. 50-346 i
-License No. NPF-3 Document Control Desk U. S_.. Nuclear Regulatory Commission ,
7920 Norfolk Avenue Bethesda, MD 20555 Gentlement +
Monthly Operating Report, March 1990 [
Davis-Besse Nuclear Power Station Unit 1 Enclosed are ten copies of the Monthly Operating Report for Davis-Besse Nuclear Power Station Unit No. I for the month of March 1990.
-If you have any questions, please contect Bilal Sarsour at'(419) 321-7384.
Very truly yours,
.' * /
Louis F. Storz Plant Manager Davis-Besse Nuclear Power Station BMS/ tid ,
Enclosures 1
! cci Mr. A. Bert Davis Regional Administrator, Region III ,
Mr. Paul Byron ;
NRC Resident Inspector Mr. T. V. Vambach l NRC Senior PicAect Manager l< :
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9004200769 900331 '
PDR' ADOCK 05000346 r R . pm p/ ;
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AVER AGE DAILY UNIT POWER LEVEL I
DOCKET NO, 50-346 ,
3.li Davis-Besse #1 April 12. M 0 DATE COMPLETED BY Bilal Sarsour ,
TELEPHONE 419-321-7384 MONTH mrch 1990-DAY. AVER AGE DAILY POWER LEVEL DAY AVER AGE D AILY P0 bid LEVEL (MWe-Net) (MWe Net) 1 0 n 17 0 0 2 lg 3 0 39 0 4 0 0 20 0
5 21 0 0
6 22 0 7 0 0 -
23 8 0 7,, o 9 n 25 0 10 0 26 0 11 0 ,, o 12 0 g 2g 13 29 0 la 0 0 30 0
15 31 0 16 0
! INSTRUCTIONS On this format hst the average dail) unit power lesel in.MWe. Net for each day in the reporting month. Compute to
- - the nearest whole megawatt.
l (9/77i
[
I
.. l OPERATING DATA REPORT !;
DOCKET NO. 50-346 l DATE April 17. 1990 ;
COMPLETED BY Riln1 Sarsour TELEPHONE 419-p21 7384 OPERATING ST ATUS OnV3R=heRRO Unit /f1 Notes
- 1. Unit Name:
- 2. Reporting Period: Mnveh 1000
- 3. Licensed Thermal Power (MWt): '777
- 4. Nameplate Rating (Grass MWe): 094 5, Design Electrical Rating (Net MWe): 906
- 6. Maximum Dependable Capacity (Gross MWe): 01R l
- 7. Maximum Dependable Capacity (Net MWe): 91^
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Lest Report. Give Reasons:
- 9. Power Level To Which Restricted. lf Any (Net MWe):
- 10. Reasons For Restrictions,If Any:
This Month Yr. to-Date Cumulative
- 11. Hours In Reporting Period 744.0 2.160.0 102,289
- 12. Number Of Hours Reactor Was Critical 0.0 608.8 54,763.4
)
.13, Reactor Reserve Shutdown Hours 0.0 0.0 5,393.7
- 14. Horus Generator On Line 0.0 608.8 52.809,2 .
- 15. Unit Reu:ve Shutdown Hours 0.0 0.0 1,732.5 _
- 16. Gross Thermal Energy Generated (MWH) .
n n' 1 6n't '4 M 126.567.245 l
- 17. Gross Electrical Energy Generated (MWH) 0, LL, . , 536.477 41,886,778,
- 18. Net Electrical Energy Generated (HWH) 0.0 508,740- 39.295,696 L
19, Unit Senice Factor 0.0 28.2 51.6
- 20. Unit Availability Factor 0.0 28.2 53.3 !
- 21. Unit Capacity Factor (Using MDC Net) 0.0 26.9 44.0 I
- 22. Unit Capacity Factor (LW3 DER Net) 0.0 26.0 42.4
- 23. Unit Forced Outage Rate 0.0 18.2 28.6
- 24. Shutdowns Scheduled Oser Next 6 Month.,(Type.Date.and Duration of Eacht
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup: June 5, 1990
- 26. Units in Test Status tPrior io Commercial Operation): Forecast - Achiesed INITlAL CRITICALITY INITI AL ELECTRICITY COMMERCI AL OPER ATION (9/771
.1
14rIT SIRffnrms AIED POWER BEDUCTICES DOCIET 153, 50-346 18817 IUWE Davis-Besse 41 care aprii 19 1990 GeEPLETED BY Bilal Sersour REPORT Materit W rch 1440 TELEPuceIE (419) 321-7384 a
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, c- e. O yg Licensee Cause & Corrective no. car. h (l p
}yj Ennt
]
y o ution to a
,ag p.rt . .r.v.at - r 3 90-02-01 S 744 C 4 NA NA NA The unit outage which began on January 26a 1990 was still in progress through the end of March.
1990.
See Operational Summary for further details.
I I F: Forced aeason: Method: 'Eshibit G - Instructions for Preparation of Lata S: Sche & led A-Equipment Failure (Esplaia) 1-Manual Entry Sheets for Licensee Event Report (IER) 6-Maintenance or Test 2-Manual Scram File (Nutgo-0161)
, ,C-Refuellag 3-Autcastic Scrsa IHtegulatory sentriction 4-Continuation from
_. E-operator Traintag & Licens. Ementaatica Previoua Month 'Eshibit I - Some Source F-Mainistrative 5-14ad Reduction
- Report challenges to Pouer operated a.11ef valves G-operational Error (Emplain) 9H)ther (Explain) (Poavs) and Pressurizer Code Safety 7tives (PCSva)
. NH>ther (Esplalal
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_ _[__________
. O Operational Summary tiarch 1990 The unit outage, which began on January 26, 1990, was still in progress through the end of March 1990.
The following are the more significant outage activities performed or still in progress during the months of February and March 1990.
I 1) The reactor core was successfully defueled. Control components had been shuffled. There vere five assemblies found with broken hold-
-down springs on the upper-end fitting. These assemblies vill be repaired and reinserted in the core.
2). An ultrasonic testing of the upper core barrel bolts was completed.
Only two bolts shoved indications. !
- 3) The inspection of the upper pressurizer manvay was successtally completed.
- 4) Surveillance spe:.imen activities were successfully completed. Four specimens vere shipped to B&V for analysis.
- 5) Ultrasonic testing on high pressure injection nozzle HP-59 vas completed.
- 6) The installation of all four cold leg-nozzle dam rings was completed.
- 7) Steam Generator #2 eddy current testing was completed. There are nineteen tubes to be plugged or replugged. Steam Generator #1 eddy i current testing is still in progress.
- 8) Completed auxiliary feedvater nozzle and header ring inspection and repair in both OTSGs.
- 9) The Reactor Coolant Pump 2-2 motor rotor has been removed and shipped to Veatinghouse for inspection and repair.
- 10) Eddy current testing of feedvater heaters was completed. The testing reveals some indications of possible through-vall cracks. Analysis of the results is in progress,
- 11) Turbine control valves and the #1 combined Intercept Valve have been removed for inspection and repair.
- 12) The steam generator bubble test and core flood tank check valve tests were successfully completed.
- 13) Completed the heat load test for containment air coolers, decay h'est coolers, and component cooling water heat exchangers.
Operational Summary
-March 1990 Page 2
- 14) The inspection of the #1 Main Feed Pump, #1 Booster Feed Pump, and #3 Condensate Pump is still in progress.
- 15) The turbine-generator and moisture separator' reheater inspection is still in progress.
- 16) An Automated Reactor Inspection System (ARIS) inspection of the reactor vessel is still in progress.
- 17) Eddy current testing of the high-pressure condenser tubes 8.s still in progress.
- 18) The inspection of the steam jet air ejector and turbine plant cooling vater heat exchanger is still in progress.
i e
k 1
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e- s -
=e REFUELING INFORMATION Date March 1990
- 1. Name of facility: Davis-Besse Unit 1 1
- 2. Scheduled date for next refueling outage? September 1991
- 3. h.heduled date for restart from current refueling: June 1990
- 4. Vill refueling or resumption of operation thereafter require a technical specification change or other license amendment? If answer is yes, what in general vill these be? If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Committee to determine whether any unreviewed safety questions are associated with the core reload (Ref. 10 CFR Section 50.59)?
Ans A license amendment request to remove cycle-specific values from Section 3 of the Technical Specifications was submitted to the NRC on June 16, 1989, based on Generic Letter 88-16, and was approved in January 1990. No Cycle ? Technical Specification changes to the Technical Specification, except for Bases changes.
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information: Changes to the bases were submitted on February 2, 1990.
- 6. Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures,
- a. Sixty Batch Reload 3.38% enriched.
- b. New fuel design Mark B8A (Reconstitutable, removable upper end fitting, Zircaloy grid spacer, debris resistant lower-end cap, lover prepressurization, and annealed guide tubes).
- 7. The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool, and (c) the new fuel storage areas. I (a) 0 (b) 505 (c) 0
- 8. The present licensed spent fuel pool storage capacity and the slee of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
Present: 735 Increased size by: approximately 900 by 1994 is planned
- 9. The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
Date: 1996 - assuming ability to unload the entire core into the spent fuel pool is maintained i
i
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