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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20249A7661998-06-11011 June 1998 Safety Evaluation Supporting Amend 222 to License NPF-3 ML20249A7551998-06-11011 June 1998 Safety Evaluation Supporting Amend 223 to License NPF-3 ML20216B9401998-04-15015 April 1998 Safety Evaluation Supporting Amend 221 to License NPF-3 ML20216B8381998-04-14014 April 1998 Safety Evaluation Supporting Amend 220 to License NPF-3 ML20202C6131998-02-0303 February 1998 Safety Evaluation Supporting Amend 219 to License NPF-3 ML20199J9511998-01-30030 January 1998 SER Related to Exemption from Section Iii.O of App R,To 10CFR50,for Davis-Besse Nuclear Power Station,Unit 1 ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20203C1401997-12-0202 December 1997 Safety Evaluation Supporting Amend 217 to License NPF-3 ML20203B2141997-12-0202 December 1997 Safety Evaluation Supporting Amend 218 to License NPF-3 ML20203C2701997-12-0202 December 1997 Safety Evaluation Supporting Amend 216 to License NPF-3 ML20138L0491997-02-11011 February 1997 Safety Evaluation Supporting Amend 214 to License NPF-3 ML20128L3001996-10-0202 October 1996 SER Supporting Dbnp IPE Process of Identifying Most Likely Severe Accidents & Severe Accident Vulnerabilities ML20058M9591993-09-28028 September 1993 SE Accepting Licensee Response to GL 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants.' ML20057A3791993-08-20020 August 1993 SE Concluding That Second 10-yr Interval Inservice Insp Program Plan for Plant Has Unacceptable Exam Sample as Discussed in Encl Inel TER ML20056G4301993-08-18018 August 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Licensee Made Changes to Subj Program to Include Exercising & fail-safe Testing of Auxiliary Feedwater Valves AF-6451 & AF-6452,in Response to TER Anomaly 8 ML20126A3051992-12-0808 December 1992 Safety Evaluation Supporting Amend 176 to License NPF-3 ML20056B2721990-08-20020 August 1990 Safety Evaluation Granting Relief from ASME Code Repair Requirements for ASME Code 3 Piping ML20248H6371989-10-0303 October 1989 Safety Evaluation Supporting Amend 139 to License NPF-3 ML20248D8271989-09-29029 September 1989 Safety Evaluation Accepting Util 890228 & 0630 Submittals Presenting Proposed Designs to Comply w/10CFR50.62 ATWS Rule Requirements ML20248E2771989-09-20020 September 1989 Safety Evaluation Supporting Amend 138 to License NPF-3 ML20248B3801989-09-20020 September 1989 Safety Evaluation Supporting Amend 137 to License NPF-3 ML20247E6901989-09-0505 September 1989 Safety Evaluation of Audit of Facility Design for Resolution of IE Bulletin 79-27 Re Loss of non-Class IE Instrumentation & Control Power Sys Bus During Operation.Preventive Maint & Testing Program Should Be Developed for Bus Power Sources ML20245K1871989-08-15015 August 1989 Safety Evaluation Supporting Amend 136 to License NPF-3 ML20245F5791989-08-0404 August 1989 Safety Evaluation Supporting Amend 134 to License NPF-3 ML20245H9531989-08-0404 August 1989 Safety Evaluation Supporting Amend 135 to License NPF-3 ML20247J8731989-05-18018 May 1989 Safety Evaluation Supporting Amend 133 to License NPF-3 ML20245G0371989-04-25025 April 1989 Safety Evaluation Supporting Amend 131 to License NPF-3 ML20245F0631989-04-25025 April 1989 Safety Evaluation Supporting Amend 132 to License NPF-3 ML20244D4031989-04-13013 April 1989 Safety Evaluation Supporting Amend 130 to License NPF-3 ML20196D9601988-12-0808 December 1988 Safety Evaluation Re Util Response Concerning Auxiliary Feedwater Sys Reliability Study.Util Should Ensure That Sys Mods Do Not Result in Net Reduction in Sys Reliability ML20207K7911988-10-0404 October 1988 Safety Evaluation Supporting Operation in Cycle 6 W/O Removing Flaws in Cracked HPI Nozzle ML20207K1071988-09-19019 September 1988 Safety Evaluation Supporting Amend 120 to License NPF-3 ML20207H9271988-08-24024 August 1988 Safety Evaluation Supporting Amend 117 to License NPF-3 ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 ML20207D5171988-08-0202 August 1988 Safety Evaluation Supporting Amend 115 to License NPF-3 ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 1999-08-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
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UNITED STATES g
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NUCLEAR REGULATORY COMMISSION 2
WASHINGTON, D.C. 20006 4001 l
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT N0. 224 TO FACILITY OPERATING LICENSE NO. NPF-3 TOLEDO EDIS0N COMPANY CENTERIOR SERVICE COMPANY MQ THE CLEVELAND ELECTRIC ILLUMINATING COMPANY DAVIS-BESSE NUCLEAR POWER STATION. UNIT NO. 1 DOCKET NO. 50-346
1.0 INTRODUCTION
By letter dated December 23, 1997, as supplemented by letter dated June 11, 1998, Toledo Edison Company, Centerior Service Company, and The Cleveland Electric Illuminating Company (the licensees), submitted a request for changes to the Davis-Besse Nuclear Power Station, Unit No.1, Technical Specifications (TSs).
The proposed amendment would revise Technical Specification (TS) Section 1.0,
" Definitions," to clarify the meaning of core alteration; would relocate TS Section 3/4.9.5, " Refuel W Operations - Communications," and the associated bases to the Techfical Requirements Manual; and would add TS Section 3.0.6 and associated bases to address the return to service of inoperable equipment.
2.0 BACKGROUND
Since several of the proposed TS changes are independent, necessary background for each is provided in the evaluation.
3.0 LICENSING BASIS The licensing basis for the systems affected by the proposed changes includes:
3.1 Davis-Besse Updated Safety Analysis Report (USAR) Section 9.5.2,
" Communications Systems" l
USAR Section 9.5.2 describes the offsite and onsite communication cystems at Davis-Besse.
Specifically, Section 9.5.2.2.3 discusses the separate loop circuit for the exclusive use of personnel directly involved with fuel handling operations.
This system provides direct communication between the control room and the fuel handling area.
l 9807090316 980630 PDR ADOCK 05000346 P
PDR L_______________________________._
3.2 USAR Section 15.4.7, " Fuel-Handling Accident."
l This USAR'section presents the analysis of a fuel-handling accident.
l Accidents inside and outside of containment are considered,' including accidents involving fuel in dry cask storage.
4.0 EVALUATION l
The licensees are proposing several TS changes.
Each proposed change is l
evaluated below..
4.1 TS Index Paae VIII The licensees are proposing to delete the word " Communications," replacing it l
with the word " Deleted." This is an administrative change consistent with the other changes in this amendment request.
Therefore, it is acceptable.
4.2 TS Index Paae XII (Bases)
The licensees are proposing to delete the word " Communications," replacing it with the word " Deleted." This is also an administrative change consistent l
with the other changes in.this amendment request.
Therefore, it is l
acceptable.
4.3 TS Definitions 1.12. Core Alteration i
The licensees are. proposing to clarify the definition of core alteration.
TS 1.12 currently reads:
CORE ALTERATION shall be the movement or manipulation of any component within the reactor pressure vessel with the vessel head removed and fuel l
in the vessel. Suspension of CORE ALTERATIONS shall not preclude completion of movement of a component to a safe conservative position.
The licensees are proposing to remove the words "or manipulation," " pressure,"
and " conservative," and to add " fuel. sources. or reactivity control" and "L" so that TS 1.12 would read:
CORE ALTERATION shall be the movement of any fuel. sources. 'or reactivity control componenth within the reactor vessel with the vessel head removed and fuel in the vessel.
Suspension of CORE ALTERATIONS shall not preclude completion of movement of a component to a safe position.
This proposed change removes terms which are redundant or could be confusing, and adds clarifying details. The staff has determined that these alterations mak6 the definition easier to understand without changing the meaning.
Therefore, this change is acceptable.
I l
l L____________________
l 4.4 TS 3/4.0. "Limitina Conditions for Operation and Surveillance l
Requirements - Acolicability" and Associated Bases The licensees are proposing to add TS 3.0.6, which reads:
i l
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l Equipment removed from service or declared inoperable to comply with ACTIONS ray be returned to service under administrative control solely to perform testing required to demonstrate its OPERABILITY or the OPERABILITY of other equipment. This is an exception to Specification l
3.0.2 for the system returned to service under administrative control to l
perform the testing required to demonstrate OPERABILITY.
The licensees are also proposing to add TS Bases 3.0.6, which reads:
Specification 3.0.6 establishes the allowance for restoring equipment to service under administrative controls when it has been removed from l
service or declared inoperable to comply with ACTIONS.
The sole purpose.
l of this Specification is to provide an exception to Specification 3.0.2 (e.g., to not comply with the applicable Required Action (s)) to allow the performance of required testing to demonstrate:
a.
The OPERABILITY of the equipment being returned to service; or j
b.
The OPERABILITY of other equipment.
The administrative controls ensure the time the equipment is returned to service in conflict with the requirements of the ACTIONS is limited to the time absolutely necessary to perform the required testing to demonstrate OPERABILITY. This Specification does not provide time to l
perform any other preventive or corrective maintenance.
An example of demonstrating the OPERABILITY of the equipment being returned to service is reopening a containment isolation valve that has been closed to comply with Required Actions, and must be reopened to perform the required testing.
l An example of demonstrating the OPERABILITY of other equipment being returned to service is taking an inoperable channel or trip system out of the tripped condition to prevent the trip function from occurring i
l_
during the performance of required testing on another channel in the other trip system.
- f. similar example of demonstrating the OPERABILITY of other equipment is taking an inoperable channel or trip system out of the tripped condition to permit the logic to function and indicate the appropriate response during the performance of required testing on l
another channel in the same trip system.
Davis-Besse TS 3.0.2 states:
(
Adherence to the requirements of the Limiting Condition for Operation
[LC0] and/or associated ACTION within the specified time interval shall J
constitute' compliance with the specification.
In the event the Limiting l
l
Condition for Operation is restored prior to expiration of the specified time interval, completion of the ACTION statement is not required.
This TS defines compliance for each TS LC0 and/or associated action. By this definition, if an LC0 has been entered due to a faulty component, and as part of the associated action, the component is removed from service and repaired, and if the component is returned to service prior to being demonstrated operable, then the licensees are in violation of the TSs.
Often, the only reasonal,le way to demonstrate operability is to put the component in service and test it, in violation of the TSs. The licensees are proposing to add TS 3.0.6 to provide an exception to TS 3.0.2, as described in the proposed TS 3.0.6 and bases quoted above. This exception would only be valid for necessary testing to demonstrate operability, and administrative controls would be in place to ensure that the time for this testing would be minimized and no other actions would be taken.
The NRC staff position on this. issue was stated in a letter to Niagara Mohawk Power Corporation dated November 21, 1996. This letter states:
It is not the intent of TS 3.0.2 to preclude the return to service of a component that has been replaced or repaired when it can reasonably be considered operable except for the completion of surveillance testing to confirm its operability. The NRC staff has addressed this existing ambiguity in TS 3.0.2 by adding TS 3.0.5 [ identical in wording to the above proposed'TS 3.0.6] to the Standard Technical Specifications (STS) for BWR/4, Revision 1 (also added to the Babcock and Wilcox STS, Revision 1].
This letter goes on to state:
In addition to providing this clarification, the Bases for TS 3.0.5
'[ identical to wording to the proposed TS 3.0.6 Bases, with the exception noted below] also notes that the administrative controls are to ensure that the time during which the component-is under manual control of the operator before operability is demonstrated is to be limited to the minimum time necessary to perform the allowed surveillance (i.e., this is not to include time for other preventive or corrective maintenance).
As. stated above, the proposed TS 3.0.6 and Bases text is identical to the STS, Revision 1, text, with one exception. The licensees have included the NRC-approved change to the Bases (Traveller for STS Revision 2 Changes, TSTF-165 dated May 5, 1997) to refer to " required testing" and "to demonstrate operability."
The staff has determined the proposed change to include TS 3.0.6 and its bases clarifies an ambiguity in the TSs, and is consistent with the current staff
. position on this TS, including the May 5, 1997 change. Therefore, the proposed change is acceptable.
i 4.5 TS 3/4.9.5. "Refuelina Operations - Communications" and Associated Bases j
The licensees propose to relocate TS 3/4.9.5 and the associated bases in their entirety to the Davis-Besse Technical Requirements Manual (TRM), a licensee-controlled document referenced in the USAR and controlled through the 10 CFR 50.59 change process.
The licensees committed to complete the relocations to the TRM concurrently with the removals from the TSs.
This TS currently states:
LIMITING CONDITION FOR OPERATION 3.9.5 Direct communication shall be maintained between the control room and personnel at the refueling station.
APPLICABILITY:
During CORE ALTERATIONS.
I ACTION:
When direct communications between the control room and personnel at the refutling station cannot be maintained, suspend all CORE ALTERATIONS.
The provisions of Specification 3.0.3 are not applicable.
SURVEILLANCE RE0VIREMENTS 4.9.5 Direct communications between the control room and personnel at the refueling station shall be demonstrated within one hour prior to the start of and at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> during CORE ALTERATIONS.
The bases currently state:
The requirement for communications capability ensures that refueling station personnel can be promptly informed of significant changes in the facility status or core reactivity condition during CORE ALTERATIONS.
Guidance to evaluate the scope of the technical specifications is provided in 10 CFR 50.36, as follows:
Criterion 1:
Installed instrumentation that is used to detect, and indicate in the control room, a significant abnormal degradation of the reactor coolant pressure boundary.
Criterion 2:
l A process variable, design feature, or operating restriction that is an l
initial condition of a Design Basis Accident or transient analysis that either assumes the failure of or presents a challenge to the integrity of a fission product barrier.
I
)
Criterion 3:
A structure, system, or component that.is part of the primary success 4
path and which functions or actuates to mitigate a Design Basis Accident or transient that either assumes the failure of or presents a challenge to the integrity of a' fission product barrier.
Criterion 4:
A structure, system,.or component which operating experience or probabilistic safety assessment has shown to be significant to public health and safety.
Requirements that are in the existing TSs, but do not meet the guidance set forth in 10 CFR 50.36 for inclusion in TS, can be relocated to appropriate licensee-controlled documents.
i i
criterion 1. The communication system is not instrumentation. Therefore, this criterion does not apply.
Criterion 2 The communication system is not a process variable, design.
feature or operating restriction. Therefore, this criterion does not apply.
Criterion 3 The communication system is not a structure or a component. As a system,.it does not function or actuate to mitigate a design basis accident or transient. Therefore, this criterion does not apply.
Criterion 4 The communication system is not a structure or a component. As a system, it has not been shown by operating experience or probabilistic safety assessment to be significant to public health and safety. Therefore, Criterion.4 does not require the inclusion of the communication system in TSs.
Since TS 3/4.9.5 and the associated bases do not satisfy any of the four criteria from 10 CFR 50.36, they may be proposed for. removal.
Further, the
= facility and procedures described in the FSAR TRM (to which the TS and bases would be relocated) can only be revised under the provisions of 10 CFR 50.59, which ensures an auditable and appropriate control over the relocated requirements and future changes to these provisions.
The staff has determined that relocation of TS 3/4.9.5 and the associated bases to the TRM.is consistent with the criteria in 10 CFR 50.36, with the 10 CFR 50.59 process providing appropriate controls for future changes.
Therefore, the proposed. relocation is acceptable.
5.0 STATE CONSULTATION
In accordance with the Comission's regulations, the Ohio State official was notified of the proposed issuance of the amendment. The State official had no
. comments.
6.0 ENVIRONMENTAL CONSIDERATION
This amendment changes a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 or changes a surveillance requirement. The staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluent that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration, and there has been no public comment on such finding (63 FR 4327).
Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9).
Pursuant to
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10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendment.
7.0 CONCLUSION
The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner; (2) such activities will be conducted in compliance with the Commission's regulations; and (3) the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor:
A. Hansen Date: Jime 30,1998
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