ML20040C919

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IE Insp Rept 50-219/81-17 on 810827-1019.Noncompliance Noted:Failure to Rept Release of 27,000 Uci Radioactivity Per 10CFR50.72
ML20040C919
Person / Time
Site: Oyster Creek
Issue date: 01/11/1982
From: Baunack W, Briggs L, Greenman E, Rekito W, Reynolds S, John Thomas
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20040C914 List:
References
50-219-81-17, NUDOCS 8201290374
Download: ML20040C919 (17)


See also: IR 05000219/1981017

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U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND EliFORCEMENT

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Region I

Report No.

50-219/81-17

Docket No.

50-219

C

License No. DPR-16

Priority

Category

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Licensee:

Jersey Central Pcwer and Light Company

Madison Avenue at Punch Bowl Road

Morristown, New Jersey

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Oyster Creek Nuclear Generating Station

Facility Name:

Inspection at:

Forked River, New Jersey

Intrection conducte .

August 27 - October 19, 1981

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Inspectors:

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' date signed

J. A. T oma,s, Resident Reactor Inspector

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WA

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date signed

g S. Reynolds, Reactor Inspector

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/dat'e signed

W. Rekito, Reactor Inspector

f$ $n$M

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L. Briggs, R6a'ctor Inspector

date signed

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W. Baunack, Reactor Inspect'of

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Approved by:

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E. G. . Gree. man, Cnief, Reactor Projects

dats signed

Section No.'2A

Inspection Sumary: Inspection on August 27 - October 19,1981 (Report No. 50-219/81-17)

Areas Inspected:

Inspection by one resident inspector and four region based inspectors

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plus a technical presentation by licensee management for senior NRC regional manage-

ment to review the events relating to tube failures in two shutdown cooling heat

exchangers. The inspection included a review of the sequence of events, safety

verification, evaluation of failure mechanism, evaluation of repairs, review of

corrective action, and review of applicable documents and procedures.

Results: Violations: one (Failure to make a report pursuant to 10 CFR 50.72 - detail 3).

8201290374 820115

PDR ADOCK 05000219:

G

PDR

Region I Form 12

(Rev. Ay il 77)

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OETAILS

1.

Persons Contacted

R. Arnold, Senior Vice-President, JCP&L

K. Bass, Engineer

J. Carroll, Director, Oyster Creek Operations

P. Clark, Vice-President, JCP&L

C. Cowfer, Manager, Materials Technology

D. Croneberger, Director, Engineering and Design

J. -De Blasio, Engineer

K. Fickeissen, Manager, Plant Engineering

I. Finfrock, Chairman, General Office Review Board

F. Giacobbe, Materials and Welding Manager

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E. Growney, Safety Review Manager

R. Keaten, Directc , Systems Engineering

J. Kneuble, Manager, BWR Licensing

M. Laggart, Licensing Supervisor, Oyster Creek

R. Lorenzo, Superviscr, Engineering Projects

T. Quintenz, Engineer

A. Rone, Engineering Manager

J. Sullivan, Manager, Operations

J. Thorpe, Director, Licensing and Regulatory Affairs

P. Walsh, Manager, Plant Analysis

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The inspectors also interviewed other licensee personnel during the

course of the inspection including management, clerical, maintenance

and operations personr.el .

2.

Introduction

On August 27 and 28,1981, tube failures occurred in two of three

shutdown cooling system (SDCS) heat exchangers while in service for

reactor decay heat remeval. The SDCS is a closed loop system designed

to remove decay heat from the reactor during shutdown operations by

circulating water from the 'E' recirculation loop through the heat

exchangers. The system consists of three pump and heat exchanger

combinations which share common supply and return lines connected to

the 'E' reactor recirculation loop.

Reactor water. flows through the

heat exchanger tubes and is cooled by circulation of Reactor Building

-Closed Cooling Water (RBCCW) on the heat schanger shell side. The

system provides only decay heat removal for normal shutdown operation

and performs no accident mitigating functions.

Failure of two heat

exchangers in such a short time period caused doubt about the integrity

of the remaining heat exchanger.

In addition, orie possible cause of

the failures was thought to be corrosion due to salt water contamination

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of the RBCCW system. This caused concern for the integrity of

other stainless steel components cooled by RBCCW. Additional

component failures could lead to loss of ability to keep the -

reactor in a cold shutdown condition, and inability to maintain

fuel pool cooling. TFe sequence of events leading to the SDCS

heat exchanger failures, safety concerns created by the failures, and

-licensee corrective actions are discussed in detail in this report.

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3.

Sequence of Events

On Augult 27,1981, the reactor was in a cold shutdown condition

~ with the 'C' SDCS heat exchanger in service maintaining reactor

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temperature between 1600 and 180 F.

At about 11:35 a.m., a decrease

in reactor water level was noted when one of four low water level

sensors actuated, causing a low water level half scram to be annunciated

through the reactor protection system. The control room operator

observed a simultaneous step increase in RBCCW activity and

annunciation of the RBCCW surge tank high level alarm. The operator

immediately isolated the SDCS, stopping the decrease in water level.

Reactor water level was restored to normal and the ' A' SDCS heat

exchanger was placed in service. During this event, reactor water

level dropped from 5.7 feet to 3.8 feet as indicated on the GEMAC

narrow range recorder in the control room. This drop in water level

occurred in about 10 minutes and is equivalent to a reactor leakage

rate of 400 gpm. The RBCCW system activity increased from about

1E-4 to 1E-3 microcuries per milliliter gross gamma, but no increase

in background radiation or airborne activity was detected. No release

of radioactivity to the environment occurred.

The 'A' SDC loop was used to cooldown the reactor to about 1350F.

The SDC system was then secured to perform a test to determine the

feasibility of cooling the reactor using the Reactor Water Cleanup

System (RWC'JS) nonregenerative heat exchanger (NRHX). At 8:45 a.m.,

on August 28, 1981, the 'A' SDCS heat exchanger was returned to

service with the reactor temperature at 1900F. At about 3:35 p.m.,

with the reactor temperature being maintained between 1600 and

1800F, the RBCCW surge tank high/ low level alarm annunciated. Addi -

tionally, an individual on the 95 elevation of the reactor building

reported that the surge tank was overflowing, and a slight' drop in

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reactor level was noted. These parameters were indicative of a tube

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leak in the 'A' SDC heat exchanger. The SDC-system was isolated and

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the leakage stopped. The licensee decided not to place the 'B' SDC heat

exchanger in service and began planning for alternate methods o' decay

heat removal,

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The licensee mobilized the management and technical staff in an alert

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status and notifieA the required government agencies in accordance with

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the Emergency Plan. At about 9:30 p.m. on August 28, procedure 203.3,

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" Alternate Shutdown Cooling Method", had been reviewed / approved by the

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Plant Operations Review Consnittee (PORC) and implemented. The procedure

provided for reactor cooldown by operating the Reactor Water Cleanup

Systam (RWCUS) at a flow rate of about 500 gpm and a letdown rate to the

condenser hotwell of about 300 gpm. A condensate pump was placed in

service to maintain reactor water level between 155 and 180 inches above

the top of the active fuel. The system was placed in service at a reactor

temperature of 152 degrees F and was able to maintain a cooldown rate of

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about 1.5 degrees per hour.

A review of events preceeding the failure of the SDC heat exchangers found

that there had been a previous _ tube failure in an RBCCW heat exchanger

that had. allowed salt water contamination of the RBCCW system from the

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service water system. On August 11,_1981, a four gpm leak from the

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RBCCW sytem was detected when a recently installed flow integrator on

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the make-up line was placed in service. Heat load on the system prohibited

isolation of the heat exchangers to detennine the location of the leak.

On August 19, 1981, the leak was found to be from the west RBCCW heat

exchanger into the Service Water System (operating with a pun'p discharge

pressure of about 60 psig.) The heat exchanger was isolated and the RBCCW

system was operated in a one heat exchanger /two pump mode.

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On August 23, the licensee decided to secure one RBCCW pump due to fu ther

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reduction in the system's heat load. The heat exchanger bypass valve was

throttled closed to increase system pressure to about 105 psi and to direct

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more flow through the heat exchanger in preparation for securing one pump.

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When flow was increased, tube vibration was noted .in the heat exchanger.

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One pump was secured and system pressure dropped to about 70 psi which is

lower than nonnal operating pressure. The pump was restarted to restore

pressure. Following restart of the idle pump, the RBCCW surge tank

level dropped rapidly indicating a failure of a heat exchanger tube.

The east heat exchanger was taken out of service and isolated, and the

west heat exchanger was placed back in service. A water sample from the

RBCCW system was analyzed and found to contain 72 ppm Nacl (about 45 ppm C1).

Salt water had apparently leaked into the system during the transient. An

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ion exchange column was put in service on the system to remove the salt

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contamination. On August 26, the failed tubes in the east exchanger were

repaired and the unit was returned to service.

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During the period that the system was operated with a 4 gpm leak and

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during the pump. realignment evolution when gmss RBCCW tube failure

occurred, a release of RBCCW water to the environment via the-Service

Water System occurred.

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The RBCCW system operated from August 11 to August 19, 1981, and again

from August 23 to August 26, 1981 with a known 4 gpm leak through the

west heat exchanger. This leakage was to the service water system, which

operates at a pressure about 40 psi lower than the RBCCW system pressure.

The service water systerr discharges to the cooling water. discharge canal,

thus, the leakage from the RBCCW system was ultimately to the environment.

The RBCCW system activity levels average about 1.1 E-4 microcuries per

milliliter, therefore, a total release of about 27,000 microcuries total

activity was discharged to the environment darIng this time period. The

licensee did not recognize the RBCCW 1eakage as an unplannM release of

radioactivity and no report was made to the NRC pursuant to i0 CFR CO.72.

Failure to report such a release is in noncompliance with 10 CFR 50.72

(219/81-17-01).

4.

Operational Safety Verification

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a.

rollowing failure of

'C' then 'A' SDCS heat exchangers, the

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licensee determined that it would not be advisable to place the

'B' heat exchanger in service until the cause of the failures

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was known. As a result of this de-ision, the normal methods of

decay heat removal while in cold shutdown were not available. At

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about 4:00 p.m. on August 28, the inspector toured the control room

and verified that adeauate safety systems were available for

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decgy heat removal . The reactor was at a temperature of about

140 F with a gradual heatup rate. The control room operators

had secured all but the 'B' reactor retirculation' pump to

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minimize the heatup rate and had left the suction and discharge

valvas of the 'B'

and 'D' loops open to insure adequate flow

between the annulus and core rec'ons of the reactor vessel. The

licensee decided to. leave one rec.rculation pump in operation to

prevent stratification ir, the core region and subsequent loss of

core temperature monitoring capability. The Core Spray System

and Isolation Condenser System were available if needed; and the

steam and condensate systems were available for decay heat removal

by drawing steam to the main condensers. The licensee technical

staff proposed the following alternate methods of decay heat

removal:

(1)

Circulate reactor. water at the maximum rate through

the reactor water cleanup system (RWCUS) and use the

nonregenerative heat exchanger for cooling. This

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method was feasible and normal RWCUS operating

procedures were adequate but only marginal cooldown

rates could be achieved.

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(2)

Circulate reactor water at the maximum rate through

the RWCUS and discharge water from the system to the-

condenser hotwell through the normal letdown path.

This method would allow additional heat removal by the

main condenser and would require operation of a

condensate pump to feed water back to the reactor.

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(3)

Flood the reactor vessel to the main steam lines and

allow reactor water to drain throuah the steam lines

to the main condenser. The water would be cooled by

normal operation of the circulating water system and

fed back to the reactor through the condensate system.

This method would require preparation cf special

procedures and a detailed review of the structural

design of the main steam system to det. ermine if the

piping supports could carry the weight of fully flooded

steam lines.

(4)

Flood the reactor vessel and the isolation condensers,

operate a recirculation pump and force circulate

reactor uter through the iso-condensers. This

method would require considerable procedural review,

development of a feed and bleed system for the shell

sides of the iso-condensers, and analysis to determine

the heat removal c::pability in this mode. This

method was later determinednot to be feasible.

(5)

Allow the reactor to repressurize and remove decay

heat by steaming to the main condensers or isolation

condensers.

Existing procedures were adequate to use

either of these methods for decay heat removal but

would require coming out of the cold shutdown condition.

The licensee chose to use method (2) above as the primary means

of decay heat removal. Procedure 203.3, " Alternate Shutdown Cooling

Method" was implemented at about 9:30 p.m. on August 28,1981.

The conditions in the RBCCW system at.the time of the SDC system

failures were such. that chloride stress corrosion cracking of

stainless steel components was possible. This created concern for

the integrity of other components in the system. Of immediate

concern were the reactor recirculation pump coclers, the RWCUS

nonregenerative heat exchanger (NRHX), and the fuel pool coolers.

The licensee needed to develop contingency plans for core decay heat

removal and fuel pool cooling in the event any of these critical

components failed.

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The alternate shutdown cooling procedure was written to include-

contingencies for failure of the NRHX and loss of the reactor

recirculation pumps.

If the NRHX tubes failed, cooling would

continue through the same flow path but the RBCCW side of the NRH.X

would be-isolated and cooling would be accomplished in the main

condenser only.

If the recirculation pump coolers failed, the

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reactor temperature would be allowed to increase to the point

of steaming to the main condenser. The licasee prepared procedures

for the operation of the augmented fuel pooi cooling system to

be.used in the event of fuel pool cooler failure. The augmented

fuel pool cooling system was installed in 1975 to provide sufficient

fuel pool cooling to accommodate a full core off-load into the

fuel pool. The system consists of two plate type heat exchangers

and a circulating pump on the 75 level of the reactor building and

can be valved into the existing fuel pool system piping.

It

was necessary to install a temporar; p wer feed from the 'C'

SDC

pump breaker to the augmented fuel pw. cooling pump and to

' jumper out the SDC pump valve interlocks. This system was made

operational and a contingency procedure was developed to provide

a feed and bleed method of cooling in the event of a complete

loss of the RBCCW system.

The inspectors reviewed the licensee's procedures and attended

technical planning meetings and were satisfied that adequate

methods and contingency plans had been established to insure

adequate core cooling without the use of emergency core cooling

systems.

It was later determined as discussed further in this report that

the heat exchanger failures were unrelated to chloride stress

corrosion.

b.

On August 29, 1981, the licensee attempted unsuccessfully .to

isolate and drain the SDC heat exchangers. Leakage past the

RBCCW valves made draining of the shells impossible. The licensee

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planned to cooldown the reactor to 125 F, establish alternate

fuel pool cooling, and then shutdown the RBCCW system so the SDC

heat exchangers could be isolated by the installation of blank

flanges. The inspector reviewed the procedures for the evolution

and found that the intent was to cooldown the reactor and secure

the recirculation pumps during the RBCCW stoppage.

In_the eveni.

of reactor heatup, the licensee intended to draw a slight vacuum

on the reactor through the main steam lines with the mechanical

vacuum pump and steam to the main condenser to remove decay

heat. The inspector expressed concern for natural circulation

cooling of the core at sub-atmospheric pressure. The core is

analyzed for natural circulation cooling during power operation and

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for cooling at pressures down to atmospheric pressure. No

analysis is documented for sub-atmospheric conditions. The

inspector stated that a safety e'vuluation pursuant to 10 CFR 50.59

must be performed to ensure adequate core circulation to provide

adequate cooling and core temperature monitoring. The licensee

performed a safety review and submitted the results t; NRC:RI for

review. On September 2,1981, the safety review was submitted and

the RBCCW stoppage and SDC isolation procedures were completed without

incident.

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5.

Evaluation of Tube Failures

a.

Description of Affected Units:

The three SDC HX units in question were manufactured by South-

western Engineering Company (SWECO), and are SA 213 type 304

(seamless) "U" tubed horizontal units with 367, 3/4" x 18 BWG

AVERAGE (0.049 + 10%) wall tubes on a 15/16" pitch. The tubes are

welded to a. stainless clad tubesheet. The units are designed as

Section III Class C on the tube side and Section VIII on the shell

side, and are designed for 150 psig/350F on the shell side and

1250 psig/350F on the tube side. The materials are carbon steel

except the tubes and tube sheet cladding which are austenitic

stainless steel. The tubesheet is approximately four inches thick.

The tube support plates are partial " half baffles" with each tube

leg supported by two tube support plates (TSP). There are no

antivibration bars at the "U" bend area. SWEC0 drawing DM 77680-

shows the straight length of the tubes to the point of tangency

to be 76" for the short radius tubes and 79 3/4" for the largest

radius tube. The flow on the shell side of the unit enters at

the back cf the shell on the bottom near the "U" bends. SWEC0

drawing DM 77680 shows the last tube support plate to point of

tangency of the bend dimension (for the isrgest radius bend) to be

1 3/16" for the bottom legs of the tubes. The tubes are welded to

the clad tubesheet and post weld rolled (3-5% wall reduction) for

two inches starting one half inch behind the tube weld. Valve

leakage on both the primary and RBCCW sides of the units has

caused the units to become pressurized during normal reactor operation.

b.

Failure Location:

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The licensee's intention was to conduct a shell-flooding static

hydro to locate failed tubes in "A" and "C"

units; conduct

Eddy Current (EC) inspection of a portion of the tubes (47 minimum);

and remove failed tubes for metallurgical examination. The EC

procedure used was NES CONAM 42-EC-021 which was a SC XI

procedure with calibration to Article IV-3000. The calibration stan-

dard tube contained the regular drilled hole artificial defects

plus 4 OD grooves and 1 1D groove. The calibration sample was SA 249

type 304 and the single test frequency was 300 MHZ.

The licensee using CONAM personnel inspected a pattern of tubes on

units "A" and "C".

The pattern selected looked at peripheral

tubes and small radius bend tubes. The inspector witnessed the EC

testing of the tubes in HX "C" and a re-testing at higher

sensitivity level of HX

"A".

Borescopic examination indicated

probable circumferential tube failures at or near the second tube

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support plate in units "A" and "C"

on the same tube, i.e.

R31 C68.

Visual examination of unit "A" indicated a plugged

tube adjacent to the recently failed tube, i.e. R31 C64. This

tube had been plugged with an Elliot driven plug.

When the Elliot plug was removed, the tube weld appeared to be

cracked. Adjacent tube welds were given a PT test with no

evidence of additional T/TS weld cracking. The " cracked weld"

was later determined to be sound. The licensee attempted to " pull"

the failed tube in unit "C" (R31 C68) but inadvertently pulled an

adjacent tube (R31 C64) which had not failed. Approximately

12 inches of the tube was pulled through the tube sheet before

realizirig that the wrong tube had been pulled. Tube R31 C68 was

later pulled but was thought to have broken off while pulling.

Later examination determined that a measurement error had been

made upon pulling and the entire section of the failed tube had

in fact been removed. The inspector examined the fracture face

of the tube and observed the following:

1.

The tube support plate ring from rotation of the tube

support plate hole was observed. The location of the

circumferential failure was adjacent to the tube

support plate (TSP) on the "U" bend side.

2.

The failure can be categorized as a " brittle failure"

of a ductile material. There was essentially no

evidence of plastic deformation associated with the

fracture.

3.

The fracture face showed no immediately apparent " fresh"

fracture face. The entire fracture face was covered

with sufficient corrosion products to appear like an

old fracture.

The fracture face from tube R31 C68 was sent to a metallurgical

laboratory and the results of the analysis are documented in

GPU NUlear Materials Technology Laboratory Report 80128. This

report indicates the rost probable cause of failure to be fatigue.

The proximity of the. failure location to the tube support plate

left the single frequency EC test in question for this general

location. (A multi-frequency technique was later required for

detecting defects within the magnetic disturbance area of the

tube support plate).

c.

Evaluation of Stress Corrosion Cracking Potential:

The inspector analyzed the corrosion characteristics of the SDC

HX units. The heat exchangers must be analyzed in accordance

with their actual service conditions rather than the design

conditions.

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The valves on the tube side and the shell side leak. When the

plant is operating, the valve leakage produces a 1000 psig

pressure on the tube side with the shell full of water which will

build up to the pump pressure of approximately 100.psig. The

heat flux direction in this mode of operation has the highest

temperature on the tube side. The water in the shell will be

essentially stagnant with only a convection current due to heating

and possibly steaming of the water on the shell side. The tube

to tube hole crevice will be a concentrating crevice due to the

higher heat on the tube side. This condition (RV power operation)

produces the highest service induced hoop stress.

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Assuming the thinnest wall and the largest ID, the service induced

hoop stress is 6735 psig. The minimum yield strength f5r SA 213

Grade 304 tubes is 30,000 psi, but the expected yield strength is

35-50,000 psi (nominally 35-40,000). The fabrication (straightening)

residual stresses could be greater (possible YS level) than the

service induced stresses. Whea the unit is being operated as a

cooler, the pressure difference across the tube wall was estimated

to be 65 psig. This would result in an applied hoop stress of

less than 500 psig.

The only two methods of producing a " brittle" failure in a

ductile material such as the 304 stainless steel tube are by

fatigue or SCC. The most probable SCC mechanisms affecting the

304 are IGSCC and chloride ion SCC.

IGSCC would normally be

expected to be an ID to 0D failure mechanism on the oxygenated

side of the unit. This mechgnism ig temperature dependent with

The mechanism also

maximum failure rates at 200 C.(392 F).

requires a tensile stress and a sensitized pertion of the tube.

The only possible sensitized areas are the area adjacent to the

T/TS weld and the HAZ from the electric resistance return bend

solution annealing operation. The stress pattern in the T/TS

weld area could give longitudinal and/or circumferential cracks,

but the crackt would be short and limited to this area. The

stress pattern from the solution annealing of the bends could

give a similar limited crack pattern. The EC testing inspected

the area of the return bend which would contain any sensitized

microstructure from solution annealing but could not inspect

behind the T/TS weld. There is no evidence to suggest failures

within the tubesheet.

IGSCC can be ruled out as a failure mode.

Assuming that chloride ion SCC were a problem, the chlorides would

affect the OD of the tubing. The reported chloride concentration

due to intrusion of salt water was 75 ppm (as NaCli. The tube

metal temperature during exposure to C1 was estimated to be 140-

160F. SCC is temperature dependent with minimal effects even

with high chloride levels below 150F. The tensile stress on the

OD of the tubes would be caused by the mechanical expansion (rolling)

transition from the rolled tube to the unrolled tube (this is within

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the tubesheet) or by unstress-relieved return bends. The only

other significant tensile stress in the tubing would be the

possible residual stress from straightening operations. The

roll transition stress pattern is complex, but the tensile stresses

run out so there could only be short cracks (if they did occur)

with minor leakage. The hoop stress from tube straightening

would result in a longitudinal crack in the tubing.

It would stop

at the solution annealed bends at the HAZ from the thermal process.

This type of cracking should be readily apparent by single or

multiple EC testing. Unstress-relieved return bends would

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preferentially fail at the small radius bends.

Evaluation of

the data indicated the tube failures were not caused by chloride

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stress corrosion cracking.

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d.

Evaluation of SDC HX Tubing Reliability:

The licensee's. program to evaluate the reliability of the SDC

HX's tubing consisted of static shell side flooding hydrotest,

single frequency and multi-frequency ID probe eddy current

testing, borescopic ID examination of selected tubes, macro and

micro metallographic analysis of selected tube samples, and shell

side and tube side hydrostatic tests.

The intent of the eddy current testing was to determine the axial

location of through wall failures and to inspect the tubing for

partial wall failures.

Due to lack of imediate availability of

multi-frequency eddy current (EC) equipment, the licensee

initially conducted tests with single frequency EC equipment. A -

sampling pattern of tubes was selected which maximized inspection

of Row 31 (and other peripheral tubes), the small radius bend

tubes and tested a few tubes in the body of the tube bundle.

Approximately 10% of the tubes were single frequency EC tested in

Units A and C.

All tubes were tested with a 300 KHZ differential-

coil technique and approximately 5% of the tubes were also tested

with an absolute coil technique. The tests showed no reportable

indications with the differential coil and no reportable wall

thinning. The failure location was determined (physically) to be

adjacent to tube support plate #3 (bottom leg closest to the U bend

end ) . The proximity of the failures to the tube support plate

indicated that if this were the only failure location, single

frequency techniques could not be used for partial tube wall

defect detection (due to tube support plate perrneability).

Once the axial location on tube R31 C68 in the C Unit was determined,

the licensee attempted to remove this tube for metallurgical

evaluation. Due to a communications error, the licensee started to

remove tube R31 C64 rather than R31 C68. When approximately 12 inches

of R31 C64 was pulled through the tubesheet, the licensee discovered

the error. Attempts to remove the defective tube (R31 C68) in Unit C

were unsuccessful apparently due to tube / tube hole interference within

the tube sheet.

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The licensee obtained multi-frequency EC testing equipment and

tested sample tubes in all three SDC HX's. The equipment employed

2 - 300 KHZ and 1 - 75 KHI differential coils and one 10 KHZ

absolute ' coil . Analysis was performed and reviewed by qualified

EC testing experts. The tubes (entire length) tested were as

follows:

SDC HX

R0W

TUBES

A

B

C

31

72, 68, 64, 60, 58,

X

X

X

54, 50, 46

29

82, 78, 74, 70, 66

X

X

X

.

62, 59, 44, 40, 36

'

29

56, 52, 48

X

X

27

88, 84, 34, 30

X

X

X

27

80, 76, 72, 68, 64

X

X

60, 58, 54, 50, 46

42, 38

25

90, 28

X

X

X

23

96, 92, 26, 22

X

X

X

21

98, 20

X

X

X

19

104, 100, 60, 58, 14

'X

X

X

17_

106, 59, 12

X

X

X

15

108, 60, 58, 10

X

X

X

13_

110, 90, 86, 82,

X

X-

X

78, 74, 44, 40,

36, 32, 28, 8

>

11

112, 6

X

X

X

9

11 0.8

X

X

X

7-

112, 6

X

X

X

5

114, 4

X

X-

X

.

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4

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13

3

116, 60, 58, 2

X

X

A

1

114, 94, 74, 44,

X

X

X

24, 4

Note:

R31 C64 "A" unit terted af ter removal of the plug.

The analysis of the multi-frequcrey testing indicated non-rejectable

" dings" and " unresolved luw '(vel indications" in all three units.

Only one significant indication was noted in Unit A and none were

noted in Unit C.

The siunificant indication in Unit A was

reported as a "cracklike'(circumferential) indication" estimated

to be equivalent to a 63% through wall crack in tube R31 C46 located

at tube support plate #3. Analysis of the data obtained from

Unit B resulted in 17 reportable indications. These indications

were reported as " partial through wall cracklike indications".

The indications were all, but two, in the bottom leg of Row 31.

The indications are reported at tube support plates, predominantly

tube support plate #3. The circumferential "cracklike

indications" are reported to vary from 31-60% through wall. Two

tubes in Row 29 (R29 C70 and R29 C78) are reported to have crack-

like indications at tube support plate #3.

The borescopic examination of the failed tubes (R31 C68 in Units

A & C and R31 C64, Unit C) indicated the fracture faces to be

located at TSP #3 on the bottom legs. Borescopic examination of

other tubes in areas not known to be failure areas resulted in

data of questionable value due to anomalus appearance of ID

films.

e.

Evaluation of Additional Tube Sections:

The following 3 " long tube segments were removed for visual

inspection:

-- Tube R31 C46 at TSP #3.

-- fube R31 C46 at TSP #4.

-- Tube R31 C64 at TSP #4.

These tube segments were chemically decontaminated prior to visual

inspection. Tube R31 C46 at TSP #3 was previously reported to have

a 63% through wall EC "cracklike indication" . Visual inspection

of these tubes by the NRC inspector indicated the following:

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14

The tubes were rotating in an elliptical pattern in

--

the TSP and had burnished areas in a pattern eccentric

to the OD cf the tube.

The burnished area appeared to be severly cold worked

--

on the tube OD surface.

-- The edge of the burnished area on at least one of the

tubes showed a worn-in or plastically deformed

circumferentially oriented ridge.

-- There was no visually observable crack in tube R31 C46

at TSP #3.

f.

Previous Failures of SDC HX Tubing:

The NRC Inspector reviewed the documents for Maintenance Job

Order 7158 QASL 964 dated 3/1/77 written to locate and plug

leaking tubes in SDC Unit A.

Procedure 713.1.002, Revision 1,

dated 2/19/76 was used for inspection and repair. Tube

R31 C64 was found leaking on the bottom leg and was plugged with

an Elliot plug. The axial location of the plug was not determined.

The Elliot plug was removed from tube R31 C64 and the location of

the failure was determined to be at TSP number 3.

The SDC HX's at Nine Mile Point, Unit 1 are duplicates of the

Oyster Creek units, and were also manufactured by SWECO. Two

of the three units each had one tube found to be leaking on tests

conducted on an outage in March and April 1977. Coincidentally,

the tubes that leaked were the lower leg of Row 31. The axial

leak location was not determined. These tubes were plugged with

tapered driven plugs. The units have been operable since the tube

plugging.

6.

Post Repair Test Activities

a.

Scope and Acceptance Criteria:

'

The inspector reviewed the Special Test procedures and test

results data to ascertain that the leak-tight integrity of the

repaired Shutdown Cooling System Heat Exchangers was adequately

demonstrated. The acceptance criteria for this review included

the facility Technical Specifications, ASME Boiler and Pressure

Vessel Code, and inspector judgment.

b.

Findings:

A

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15

With the exception of the items below, the objective of demonstrating

the leak-tight integrity of the repaired heat exchangers was

accomplished and the inspector had no further questians in this area.

1)

Technical Specification 6.15, Integrity of Systems

Outside Containment, requires leakage tests be performed

for the Shutdown Cooling System.

In response to

=

NUREG 0578, item 2.1.6a, the licensee comitted to

performing periodic inter-system leakage tests

past heat exchanger tube boundaries, as part of the

ongoing Leakage Reduction Program.

The inspector noted that the Leakage Reduction Prccedure

665.5.009 did not address the possible leakage past

.

heat exchanger tubes but was satisfied that the commitment

was met at this time by the conduct of Special

Procedure 81-135. The 1icensee representative

acknowledged that the existig formal leakage reduction

program procedures do not check. inter-system leakage

past heat exchanger tubes. He stated that applicable

procedures would be changed -to satisfy this comitment.

The inspector stated that this matter is unresolved

pending NRC review of revised leakage reduction program

procedures for the Shutdown Cooling System. (219/81-17-02).

2)

The Safety Evaluation of Tube-Plugging Methods stated

that installed mechanical plugs leak-tight integrity would

be demonstrated by a heat exchanger shell-side pressure

test with no visible leakage as the acceptance criterion.

The inspector noted that the purpose of both Special

Procedure 81-114 and 81-135, " Shutdown Cooling Heat

Exchanger Tubeside Hydrotest" was to demonstrate the

leak-tightness of tubes and installed mechanical plugs.

The licensee representative acknowledged this omission

and stated that the Safety Evaluation would be

revised to include demonstrating leak-tightness of the

mechanical plugs in both directions with no visible

leakage as the acceptance criterion.

7.

System Operating and Emergency Response Procedure Changes

The inspector reviewed revisions to procedures associated with the Shut-

down Cooling and Reactor Building Closed Cooling Water Systems which

resulted from the heat exchanger failure events. The acceptance

criteria for this review included Technical Specifications,

,

applicable regulatory guidance, and inspector judgment for adequacy of

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measures established to;

1) prevent system operation in the manner

believed to be the cause of failures; 2) detect similar failures as

soon as possible; 3) respond to similar failures by bringing the

plant to a shutdown condition in a safe and orderly fashion.

As a result of this review, no unacceptable conditions were identified

and the inspector had no further questions at this time.

8.

Document Review

The following documents were reviewed during this inspection:

-- Procedure SP 81-111, Failure of RBCCW to Recirculation Pump Seal

Coolers and Motor Bearing 011 Coolers

Procedure SP 81-112, Augmented Spent Fuel Pool Cooling System

--

-- Procedure SP 81-113, SDC HX Shell Side Isolation

-- Procedure SP 81-114 SDC HX Isolation, Tube Inspection and Repair

Procedure SP 81-116, Alternate Means of Removing Reactor Decay

--

Heat Utilizing the Main Condensers

Procedure SP 81-117, SDC HX Tube Plugging

--

Procedure SP 81-118, Fuel Pool Cooling System Feed and Bleed

--

-- Procedure SP 81-119, RBCCW System Removal and Contingencies for

Addition of Line Blanks

-- Procedure SP 81-120, Recirculation Pump Operation Without RBCCW

-- Procedure SP 81-121, NDE of Shutdown Heat Exchangers

Procedure SP 81-122, Tube Removal from Shut Down Heat Exchanger

--

A and C

Procedure SP 81-127, Opening the Shell Side of SDC HX

--

Procedure SP 81-129, Re-Installation of the Shutdown Cooling Heat

--

Exchanger NUO1-A Shell Dished Head

Procedure SP 81-134, Shutdown Cooling HX Isolation Valve Leak Test

--

-- Procedure 5P 81-135, Shutdown Cooling HX Tubside Hydrotest

-- Procedure SP 81-136, Shutdown Cooling HX Shell Side Valve Replacement

Procedure 203-3, Alternate Shutdown Cooling Method

--

Procedure 305, Revision 12, Shutdown Cooling System

--

Procedure 530, Pavision 3, Loss of the Reactor Shutdown Cooling System

--

Procedure 515.4, Revision 5, Small Pipe Break Outside Drywell

--

Procedure 309.2, Revision 4, Reactor Building Closed Cooliag Water

--

System

-- Procedure 507.1, Revision 7, Reactor Building Closed Cooling Water

System Failure

Procedure 665.5.009, Revision 0, Reactor Shutdown Cooling Leakage

--

Reduction Procedure

SWECO Dwg DM 77680, Revision 3, Bundle Assembly

--

SWECO Dwg DM 77367, Revision 6, Shell

--

-- SWECO Dwg DM 77678, Revision 3, Head and Cover Details

SWECO Dwg DM 77683, Revision 1, Gasket

--

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SWECO Dwg M 77681, Tube Sheet Drilling Template

SWECO Dwg M 77676, Revision 2, Tube Schedule

--

SWECO.Dwg S-247, Thimble Plug Details

--

EWECO Dwg FS-452, Solid Plug Details

--

SVECO BT-8TS-M-TIG, WPS for T/TS Welding

--

-- SWICO Spec Sheet, Job 5-5026, File 26496, SDC HX type 6C-42-72H

- , Job Order 7158, QASL 964, dated March 1,1977, SDC HX Tube Leak

Inspection

GPU Nuclear Materials Technology Laboratory Report 80128, Preliminary

--

Analysis of the Oyster Creek "A" SDC HX Failure, dated September 28,

1981

GE SDC HX Equipment Specification 21A1507, Revision 0, dated

--

October 26, 1964

GPU Nuclear Interoffice Memo dated July 3,1981, RBCCW System Review

-

--

-- CONAM EC Test Procedure 42-EC-021

CONAM EC Test Procedure 42-EC-043

--

Letter from JCP&L to NRC dated January 4,1980, NUREG 0578

--

Implementa tion

-- Safety Evaluation of tube plugging methods for Oyster Creek Shutdown

Heat Exchanger Failures

Safety Evaluation of using the main condensers to remove reactor

--

decay heat to maintain reactor coolant temperature less than 2120F.

9..

Conclusions

The most probable cause of the shutdown cooling heat exchanger tube

failures is flow induced vibration resulting in circumferential

fatigue failures adjacent to the third tube support plate. Although

this cannot be verified by metallurgical evidence,-it best fits all

of the existing data. Modifications to the RBCCW system have provided

improved flow monitoring instrumentation. The plugged tubes will

act as flow impingement baffles for the other tubes and revisions to

system orerating procedures should preclude operation at flows that

would cause tube vibration.

Repairs to the 'C' SDC heat exchanger were impractical, partially due

to potential damage to the tube bundle caused by the " pulling" of an

intact U-tube. The remaining units will provide adequate decay heat

removal capability to maintain the reactor in cold shutdown under

worst case conditions.

10.

Unresolved Items

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptatle items, items of

noncompliance, or deviations.

The unresolved item identified during

this inspection is discussed in paragraph 6.

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18 is

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'll. : Technical Presentation

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-GPU a'nd JCP&L Corporate and site personnel presented data, evaluations

and ccnclusions regarding the events related to failures of tubes in

two shutdo'wn cooling heat exchangers including proposed corrective

' actions. tir. P.- R. Clark, Vice President; Nuclear and members of his

staff and Mr. J. M.tAllan, Deputy Regional Administrator, Region I and

members of the Region I staff participated.

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12.

Exit Interview

'

- At piriodic intervals during the inspection, meetings were held with

senior facility and corporate management to discuss inspection scope

and. findings. -In addition,' a meeting between senior NRC:RI and licensee

manasement was held on September 10, 1981 to discuss the sequence of events

leading to the SDC heat exchanger failures, current plant status, and

licensee plans for maintaining the plant in a safe condition.

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