Letter Sequence Request |
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TAC:10026, (Approved, Closed) TAC:11026, (Approved, Closed) TAC:11262, (Approved, Closed) TAC:12831, (Approved, Closed) TAC:47044, (Approved, Closed) TAC:47045, (Approved, Closed) TAC:47876, (Approved, Closed) TAC:47877, (Approved, Closed) |
Results
Other: ML19291B901, ML19291B903, ML19309G757, ML20004B639, ML20011B241, ML20011B243, ML20031C991, ML20039F146, ML20040D603, ML20041C142, ML20041C150, ML20050F889, ML20052F775, ML20052G848
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MONTHYEARML19270H4761979-07-23023 July 1979 Forwards Request for Addl Info to Be Sent to Licensee in Order to Complete Review of 770722 Submittal Re Technical Assistance Contract 10026.Response Required within 45 Days Project stage: RAI ML19254D1071979-09-18018 September 1979 Requests Addl Info Re Loss of Offsite Power on 770920 to Aid in Review of Offsite Power Sys Adequacy.Requests Reponse within 90 Days Project stage: Approval ML19250C3611979-10-30030 October 1979 Forwards Request for Addl Info on Degraded Grid Voltage Determined During Review of 770722 Submittal Re Second Level of Undervoltage Protection for Engineering Safety Feature Loads.Proposal for Tech Specs Change Required Project stage: RAI ML19291B9031979-12-0707 December 1979 Adequacy of Station Electric Distribution Sys Voltage Project stage: Other ML19291B9011979-12-0707 December 1979 Forwards Rept Adequacy of Station Electric Distribution Sys Voltage Project stage: Other ML19290E0331980-02-13013 February 1980 Forwards Request for Addl Info Re Loss of Offsite Power Events.Requests Response within 90 Days Project stage: RAI ML19312D3491980-02-29029 February 1980 Forwards Request for Addl Info Re Adequacy of Station Electric Distribution Sys Voltage to Complete Review of Project stage: RAI ML19309G7571980-04-28028 April 1980 Forwards Addl Info Re Adequacy of Station Electric Distribution Sys Voltages & Replacement Pages for 791207 Rept in Response to NRC 800229 Request Project stage: Other ML20004B6371981-05-21021 May 1981 Application for Amend of License DPR-57 to Revise Tech Spec for Instrumentation Which Initiates Disconnection of Offsite Power Sources Project stage: Request ML20004B6391981-05-21021 May 1981 Tech Spec 3.2-12 for Instrumentation Which Initiates Disconnection of Offsite Power Sources Project stage: Other ML20031C9801981-10-0202 October 1981 Application to Amend Licenses DPR-57 & NPF-5,changing Tech Specs Re Limiting Conditions for Operation & Surveillance Requirements for Degraded Voltage Relays & Loss of Offsite Power Relays Project stage: Request ML20031C9911981-10-0202 October 1981 Proposed Tech Specs Re Limiting Conditions for Operation & Surveillance Requirements for Degraded Voltage Relays & Loss of Offsite Power Relays Project stage: Other ML20011B2431981-12-0202 December 1981 Corrected Tech Spec 4.9.A.6 for Limiting Condition for Operation & Surveillance Requirements Re Degraded Sys Voltage Project stage: Other ML20011B2411981-12-0202 December 1981 Forwards Corrected Tech Specs Pages 3.9-4 & 3.9-4a Re Degraded Sys Voltage,Per 811002 Amend.Typing Error Corrected.No Wording Changed Project stage: Other ML20039A9831981-12-0707 December 1981 Forwards Request for Addl Info Re Adequacy of Electric Distribution Sys Voltages.Response Requested within 30 Days Project stage: RAI ML20039F1461981-12-10010 December 1981 Advises That Components,Including Relays,Potential Transformers,Associated Auxiliary Relays & Power Supplies Are safety-related Equipment.Util Should Propose Tech Spec Changes That Include Surveillance of Components Project stage: Other ML20041C1501981-12-31031 December 1981 Station Auxiliary Sys Offsite Source Voltage Study Project stage: Other ML20040A9471982-01-12012 January 1982 Responds to 811207 Request for Addl Info on Electric Distribution Sys Voltages.Info Includes Test Results or Vendor Certification Re Contactor Capability for Continuous Operation at 98.2 Volts.Drawings Encl Project stage: Request ML20040D6031982-01-26026 January 1982 Proposed Tech Spec Pages Re Emergency Power Sys Project stage: Other ML20040D5991982-01-26026 January 1982 Application for Amend to Licenses DPR-57 & NPF-5 Changing Tech Specs Re Surveillance of Undervoltage Relays & Associated Components of Emergency Power Sys.Response to NRC Encl Project stage: Request ML20041C1421982-02-18018 February 1982 Forwards Southern Co Svcs Hatch Units 1 & 2 Station Auxiliary Sys Offsite Source Voltage Study, Clarifying Emergency Power Sys Capabilities.Assumptions 15,21 & 24 Outlined Project stage: Other ML20050F8911982-04-0505 April 1982 Safety Evaluation Re Adequacy of Facility Electric Distribution Sys Voltages.Design Acceptable Project stage: Approval ML20050F8891982-04-0505 April 1982 Notifies That Electric Distribution Sys Voltages Comply W/ General Design Criterion 17 & Are Acceptable Per 791207, 0428,1009 & 820112 Responses Project stage: Other ML20052F7821982-05-0606 May 1982 Safety Evaluation Supporting Amends 88 & 27 to Licenses DPR-57 & NPF-5,respectively Project stage: Approval ML20052F7751982-05-0606 May 1982 Amends 88 & 27 to Licenses DPR-57 & NPF-5,respectively, Amending Tech Spec Resulting from Reanalysis & Mod of Plant Sys & Components Deemed Necessary in Order to Avoid Consequences of Degraded Grid Voltage Condition Project stage: Other ML20052G8481982-05-14014 May 1982 Requests Remittance of Class III Fee for 811002 Application Re Degraded Grid Voltage Project stage: Other 1981-12-02
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Similar Documents at Hatch |
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'Gotag A fom Compry "n3 Pedwt Avenue At:anta. Ge(npa 30306 T& phone J04 $2G 7025 Maing AMren Prat O!!re Dox 4545 AHarta Gersg.a 30302 Georgia Power W""
W. A. Widner qQ;\\ 61 E Na N,,*o N In"""d" October 2, 1981 4
4 Ocr [8 /.9g Director of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission pg Washington, D. C.
20555 b-NRC 00CKETS 50-321, 50-366
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OPERATING LICENSES DPR-57, PPF-5 U-7 EDWIN I. HATCH NUCLEAR PLANT UNITS 1, 2 EMERGENCY POWER SYSTEMS Gentlemen:
On July 22, 1977, Georgia Power Company proposed Unit 1 Technical Specifications for the disconnection from offsite power in the event of loss of offsite power or a
sustained degraded system voltage at the interconnection to offsite power.
Our submittal was then amended on May 21, 1981, in order to meet the tRC position stated in item 1 of the attachment to your October 30, 1979, letter for providing surveillance requirements for a second level of undervoltage protection.
This amendment refines the trip settings, corrects the number of required operable channels, and deletes note (c) on Table 3.2-12 of the Unit 1 Technical Specifications.
Additionally, the surveillance requirements for the Logic System is corrected to reflect the need to test both sets of
- relays, i.e.,
degraded voltage relays as well as loss-of-offsite-power relays.
Additionally, Georgia Power Company (GPC) has performed an assessment of the current design of the Plant Hatch Unit 2 emergency power systems in accordance with the staff positions contained in your letter of June 2, 1977, to determine the suscerM L11ty of safety-related electrical equipment to 1) sustained degraded voltage conditions at the offsite power sources and to 2) interaction between the offsite and onsite emergency power systems.
In accordance with staff position 1 of the referenced letter, GPC proposes to modify our existing Technical Specifications to include a second level of undervoltage protection.
The proposed changes include limiting conditions for operation and surveillance requirements for both degraded voltage relays and loss-of-offsite-power relays.
Our system protection personnel determined that additional protection against the degraded system voltage condition could be achieved by a revised combination of settings of the bus undervoltage relays.
Accordingly, the relay values were changed such that two relays on each aus are set to the 105 volt tap, time dial 5, and two relays on each bus are set to the 93 volt tap, time dial 2.
The logic tests are amended to assure that both degraded voltage relays and loss-of-offsite-power relays are tested, ft $
00{
6*5 8110090178 811002 PDR ADOCK 05000321 g
GeorgiaPower A Director of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission October 2, 1981 Page Two The Plant Review Board and the Safety Review Board have reviewed and approved the proposed changes to the Technical Specifications and have determined that the probability of occurrence or the consequences of an i
accident or malfunction of equipment important to safety are not increased since the proposed changes impose additional requirements to assure proper l
cperation of the onsite power system.
The possibility of an accident or malfunction of a new or different type than those previously analyzed are not created since the only plant modifications involved the changing of the logic in order to increase the level of protection of the emergency
'lectrical distribution system.
Hence, the margin of plant safety is not reduced.
The proposed Unit 1 and Unit 2 Technical Specifications are attached.
The Unit 1 Technical Specifications are changes to a previous submittal.
The Unit 2 Technical Specifications constitute a category 1 submittal for fee class determination.
j If you have any questions, please contact this office.
]
W. A. Widner states that he is Vice President of Georgia Power Company and is authorized to execute this oath on behalf of Georgia Power Company, and that to the best of his knowledge and belief the facts set forth in this i
letter are true.
GEORGIA POG1 COMPANY t
h.
j By:
d6 d! db/Mf,
/
2 W. A. Widner I
Sworn t and subscribed before me this 2nd day of October,1981.
'S my s En 1 3 Notary Public i
OLT/mb Attachment b
xc:
M. Manry
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R. F. Rogers, III l
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